ML20136B694

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Monthly Operating Rept for Aug 1985
ML20136B694
Person / Time
Site: Callaway Ameren icon.png
Issue date: 08/31/1985
From: Goodenow R, Miltenberger S
UNION ELECTRIC CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
ULNRC-1170, NUDOCS 8511200265
Download: ML20136B694 (6)


Text

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MONTHLY OPERATING REPORT DOCKET NO.

50-483 UNIT NAME 6 DATE SEPTEMBER 6, 1985 COMPLsTu BY R.

R.

GOODENOW TELEPHONE (314) 676-8460 PART A OPERATIONS

SUMMARY

AUGUST 1985 Power operations were resumed from the 7/31 Reactor Trip on 8/1.

Full power operations continued until 8/17 when the Axial Flux Difference was discovered to be beyond Technical Specification limits. Power was reduced below 50% until penalty points expired.

Full power operations then continued until 8/20 when a

the unit tripped due to generator loss of field. Unit was put back on line but tripped again on 8/20 due to Hi-Hi Moisture Separator Reheater level. Unit was back on line on 8/21 and returned to full power for the remainder of the month.

PART B PORV AND SAFETY VALVE

SUMMARY

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NONE e

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h 850831

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CA-#804 05/09/84 QDP-ZZ-04204 Page 1 of 4

Part C AVERAGE DAILY UNIT POWER LEVEL 50-483 DOCKET NO.

j UNIT Callaway DATE SEPTEMBER 6.1985 COMPLETED BY R. R. GOODENOW TELEPHONE (314) 676-8460 MONTH AUGUST 1985 a

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe Net) 538 3

364 37 1020 759 2

3, 1111 1110 3

39 1101 24 4

5 21 6

1081 472 22 1097 1054 7

23 g

1100 1101 24 1073 1109 g

5 1102 1109 10 26 1100 1109 33 p

12 1080 3

1106 1095 13 1094 29 1104 1100 14 y

1108 1099 15 3

16 1081 l

0 [0 84 l

Page 2 of 4 QDP-ZZ-04204 r

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A Part D OPERATING DATA REPORT 50-483 DOCKET NO.

Callaway UNIT SEPTEMBER 6, 1985 DATE R. R. GOODN COMPLETED BY (314) 676-8460 TELEPHONE OPERATihG STATUS 744 AUGUST 1985 Gross hours IN REPORTING PERico:

1. REPoRTimo PERico:

3411 max. DEPENO. CAPACITY (MWo.Ned:

1120

2. CURRENTLY AUTHORIZED POWER LEVEL (MWts:

DESIGN ELECTRICAL RATING (MWo.Ned: 1171*

At Stretch reactor power level which is not currently authorized under the operating license.

a

3. POWER LEVEL TO WHICM RESTRICTED lip ANY) (MWo.Nett:
4. REASONS FOR RESTRICTION IIP ANYl:

THIS MONTH YR TO DATE CUMULATIVE 731.5 5332 5634.5

5. NuMcER op McVRS REACTOR WAS CRITICAL 0

0 0

6. REACTOR RESERVE SMUTDOWN MoWRS 708.5 5214.3 5516.8 7 MOURS GENER ATOR ON LINE 0
8. UNIT RESERVE SHUTDOWN McVMS
9. GROSS TMERMAL ENERGY GENER ATED tMWHI

,2.??6.770 16.166.769 17.168.294 748,661 5,467,697 5,806,877

10. GROSS ELECTRICAL ENERGY GENERATED (MWM).
11. NET ELECTRICAL ENERGY GENER ATED tMWM) 710.251 5,185,216 5.508.239 98.37 91.47 91.95
12. REACTOR SERVICE P ACTOR 98.37 91.47 91.97
13. REACTOR AVAILABILITY P ACTOR 95.2%

89.47 R9.q?

14 UNIT SERVICE PACTOR IS. UNIT AVAILA51LITY PACTOR

, 95.2%

89.47 R9.97 85.27 79.47 90 vr

18. UNIT CAPACITY PACTOR IUmas MDC) 81.5%*

75.9%*

76.77*

17. UNIT CAPACITY P ACTOR (Uwne Doogn MWel.

4.8%

5.87

~5.57

18. UNIT PORCED OUTAGE RATE
19. SMUTDOwneS SCHEDULED OVER NExT S MONTHS (TYPt. DATE. ANO DURATION OF EACMI:

NONE

20. IF SMUT DOWN AT END OF REPORT PERIOD. ESTIMATED OATE OF STARTUP:

CA-804 05/ 9/84 Page 3 of 4 gep_gg.04204

o s

I e:

  • Part E DOCKET NO.

50-483 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Callaway DATE SEPTEMBER 6, 1985 COMPLETED BY R. R. GOODEN0W TELEPHONE (314) 676-8460 REPORT MONTH AUGUST 1985 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO.

DATE S: SCHEDULED l HOURS)

REASON REDUCING POWER CORRECTIVE ACTIONS #nanasNTS 15 850731 Forced 3.2 C

3 Reactor Trip from 100% power due to inadvertent closure of MF1V.

LER 85-036-00 16 850817 Forced 0

G 1

Load reduction in accordance with Technical Specifications due to Axial Flux Difference Cumulated Penalty Time Limit exceeded. LER 85-037-00 17 850820 Forced 19.6 A

3 Turbine Trip from 10D% power due to generator voltage regulator problem.

LER 85-038-00 18 850820 Forced 12.7 G

3 Reactor Trip from 25% power due to incorrect valve line-up for.noisture separator reheater. LER 85-039-00 SURAGARY:

CA-#804

  • 05/09/84 Page 4 of 4 QDP-ZZ-04204

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' U NION ELECTRIC COMPANY CALLAWAY PLANT MAILING ADDRESSt P. O. SOM S BO FULTON. MO. GS3 50 September 9, 1985 Director, Rescurce Management Nuclear Regulatory Commission Washington, DC 20555 ULNRC-Il70

Dear Sir:

DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT AUGUST 1985 The enclosed Monthly Operating Report for August 1985 is submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications.

k vtd Lv,A-S. E. M11tenberger-

' Manager, Callaway Plant

. DC#Wt-MET /WRC/

/dra Enclosure

- cc: Distribution attached

. - 4 ?,

4 cc distribution for ULNRC-1170 with enclosures Mr. James G. Keppler

. Regional Administrator, Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, DC-20555 NRC Resident Inspector

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