05000316/LER-1985-018-01, :on 850820,ESF Actuation Occurred.Caused by Opening of Reactor Trip Breakers During Instrumentation Checks.Surveillance Test Procedure Thp 4030 STP.180 Revised

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:on 850820,ESF Actuation Occurred.Caused by Opening of Reactor Trip Breakers During Instrumentation Checks.Surveillance Test Procedure Thp 4030 STP.180 Revised
ML20135J021
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/19/1985
From: Blind A
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20135J018 List:
References
LER-85-018-01, LER-85-18-1, NUDOCS 8509250141
Download: ML20135J021 (1)


LER-1985-018, on 850820,ESF Actuation Occurred.Caused by Opening of Reactor Trip Breakers During Instrumentation Checks.Surveillance Test Procedure Thp 4030 STP.180 Revised
Event date:
Report date:
3161985018R01 - NRC Website

text

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LICENSEE EVENT REPORT (LER)

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ON AUGUST 20,1985, AT 2250 HOURS WITII UNIT 2 IN MODE 3 (HOT STANDBY), AN ESF ACIUATION OLUummu h11EN THE REACIOR TRIP BREAKERS OPENED hyTTR CONDUCTING INSTRLHEtEATION CHECKS PRIOR 'IO S'IARTUP.

NORMAILY THE REACIOR TRIP BREAKERS ARE OPEN WHTTR PEREORMING 'IIIIS SURVRTTJANCE TEST, HOWEVER, IN THIS INSTANCE THEY WERE CIOSED AND SUBSEQUENTLY OPENED UFCN PECEIPT OF A TRIP SIGNAL.

'IO PREVENT REGRRENCE, THE APPLICABIE SURVEILIANCE TEST PROCEDUPE (THP 4030 STP.180) HAS BEEN REVISED 'IO REQUIRE 'IIIE N(7fIFICATION OF OPERATIONS PERSONNEL 'IllAT A REAC'IOR TRIP SIGNAL WIIL BE GENERATED DURIIK; THE COURSE OF THE TEST.

A SIMILAR OLUumtNCE KAS REPOICED IN LER 50-316/84-32.

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