ML20135G061

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Monthly Operating Rept for Aug 1985
ML20135G061
Person / Time
Site: Nine Mile Point 
Issue date: 08/31/1985
From: Lempges T, Roman T
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF ADMINISTRATION (ADM)
References
NMP-13807, NUDOCS 8509180097
Download: ML20135G061 (5)


Text

T NIAGARA N0llAWK POWER CORPORATION NINE b1ILE POINT NUCLEAR STATION UNIT #1 NARRATIVE OF OPERATING EXPERIENCE The station operated during the month of August 1985 with a Unit Availability Factor of 95.0 and a Net Design Electrical Capacity Factor of 84.1.

There was 1 challenge to Electromatic Relief Valves as a result of the Rx Scram 8/19/85. Reductions in Capacity Factor were due to seasonally high circulating water temperatures, control rod pattern adjustments and one automatic reactor shutdown due to equipment failure and one automatic reactor shutdown due to personnel error.

CLASS I WORK - MECilANICAL MAINTENANCE - AUGUST 1985 hR# 33929 DG 102 Water Pump - Checked for Icaks.

hR# 32886 38-H21 Ilanger - Replaced hanger parts.

hR# 34414

  1. 11 FW Pump - Seal welded union hR# 32859 Spare valve for Inst. air comp - Rebuilt and resurfaced valves hR# 34513 CRD 14-39 foot valve #111 - Replaced 'O' rings, replaced broken handwheel hR# 32994 Valve 72 Removed nuts, cleaned and neverseized bolts.

CLASS 1 WORK - ELECTRICAL MAINTENANCE - AUGUST 1985 hR# 34214 122 Containment Spray System - Replaced spring charging motor.

hR# 34005 MG-162 Control Cabinet Protection Relay 27 Replaced relay Cover.

hR# 33472 201.2 Reactor Containment N2 Purge and Fill System - Cleaned panel and replaced covers, hR# 34007 50-11 Feedwater Pump Motor - Cleaned air inlet screens.

hR# 34416 Reactor Core Spray,40-112 - Reconnected motor heater leads hR# 34415 Reactor Core Spray,40-111 - Reconnected motor heater leads hR# 34431 202-4-110 Reactor Building Emer. Ventilation System. - Replaced burned out coil on relay 4-11b/202.

CLASS I WORK - INSTRUMENTATION 6 CONTROL - AUGUST 1985 hR# 33957 Rx. Bldg. Vent. Rad. Monitor #12 spiked upscale - twisted cabic, hR# 32820 Rx. Recire Pump #11 - recalibrated flow transmitters hR# 33756 Feedwater Pump #12 Flow Control Valve loose feedback spring.

hR# 33955 Control Room Vent. Rad. Monitor - upscale spike recalibration.

hR# 34208 Control Rod Drive flow transmitter - crronious reading - purged air from transmitter, hR# 33783 Post Accident sample system - replaced irratic solenoid.

hR# 33768 Instrument Air Compressor - replaced sticking solenoid.

hR# 33659 11 FW Control Valve replaced range spring and lock, stroked valve for operation.

8509180097 850831" PDR ADOCK 05000220 R

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OPERATING DATA REPORT DOCKET NO. 50-220 DATE 9/5/85 g

CONIPLETED BY 'lN Roman 9

TELEPHONE (3151349-2422 OPERATING STATUS i

1. Unit Name: Nine Mile Point tinit i Notes
2. Reporting Period:

8/01/85 to 8/31/85

3. Licensed Thermal Power (MWt):

1850 4

i

4. Nameplate Rating (Gross MWe):

640

5. Demon Electrical Rating (Net MWe): 620 630
6. Maximum Dependable Capacity (Gross MWe):

610 i

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

+

i

9. Power Level To Which Restricted,If Any (Net MWe):
10. Reasons For Restrictions. If Any:

This Month Yr..to.Date Cumulatise i

i1. Hours In Reporting Period 744 5831 139,896.2

12. Number Of Hours Reactor Was Critical 717 5774 98,489.8 j
13. Reactor Reserve Shutdown Hours 0

0 1,204.3 1

14. Hours Generator On-Line 706.7 5749.0 9,554.3
15. Unit Reserve Shutdown Hours 0

0 20.4 1

16. Gross Thermal Energy Generated (MWH) 1,244,646 10,368,353 159,657,803
17. Gross Electrical Energy Generated (MWH) 402,122

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18. Net Electrical Energy Generated (MWH) 388.131,

3,478,876 52,359,664 3.373,850 51,203,844

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19. Unit Service Factor 95.0 98.6 68.3
20. Unit Availability Factor 95.0 98.6 68.3
21. Unit Capecity Factor (Using MDC Net) 85.5 94.9 60.0
22. Unit Capacity Factor (Using DER Net) 84.1 93.3 59.0 1
23. Unit Forced Outage Rate 5.0 1.4 15.7 l
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each t:

l i-i

25. If Shut Down At End Of Report Period, Estimated Date of Startup:
26. Units in Test Status (Prior to Commercial Operation 1:

Forecast Achieved i

INITIAL CRITICALITY INITIAL ELECTRICITY 1

COMMERCIAL OPERATION i

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AVER \\GE D AILY UNIT POhER LEVEL 1

a DOCKET NO, 50 220 UNIT 9 hfile Pt. #1 DATE 9/5/85 CO\\tPLETED tly TW Roman 4

(315)349-2452 TELEPJIONE StONTH August.1985 l

DAY AVERACE DAILY POWER LEVEL, DAY AVERACE DAILY POhER LEVEL (MWe Net)

(alWe-Ne,i 582 g7 567 2

582 572 33 582 3

39 184 j

4 581 20 128 j

5 581 21 317 j

6 579 483 7

575 21 a

569 t

456 9

574 25 563 10 571 26 582 569 27 579 l

12 576 578 582 4

I3 29 579 14 576 30 580 is 561 3:

593 16 559 l

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INSTRUCTIONS l

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UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-220 UNIT NAME 9 Mile Pt. #1 DATE 9/5/85 m

o REPORT MONTil August 1985 COMPLETED RY TW Romnn )rL E

'IELEPflONE f319 340-24 0 "i

.! E 3

)sE Ek Licensee E r, E.%

Cause & Corrective No.

Date E?

s 2

Event u'g f'?

Action to S

$E 5

j di g Report a NU Prevent Recurrence d

85-12 850815 F

27 11 1

Load Reduction To 92.6% Duc To liigh Cire. Water Temperatures 85-13 850819 F

90 G

3 Auto Scram Due To Ground In The Generator Voltage Control Circuits 85-14 850823 F

30.3 A

3 Auto Scram (LO Rx Water Level) Due To Failure Of #11 FW Flow Control Valve I

2 3

4 F: Forced Reason:

Method:

Exhibit G-Instructions S: Schedufeil A Equipment Failure (Explain) 1 -Manual for Preparation of Data B-Maintenance of Test 2-Manual Scram.

Entry Sheels for Licensee C-Refueling

3. Automatic Scram.

Event Report (LER) File (NUREG-D-Regulatory Restriction 4.Other (Explain) 0161)

E-Operator Training & Ucense Examination F-Administrative 5

G-Operational Eiror (Explain t Exhibit 1 - Same Source 19/77)

Il Other (Explain)

o NMP-13307 NIAGARA MOHAWK POWER CORPORATION NIAGARA MOHAWK 300 ERIE BOULEVARD, WEST SYR ACUSE. N. Y.13 202 Septembet 5, 1985 Dh ec. tor Office of Ittspection and Enforcemestt U.S. Nuclear Regulatory Commbsion h'ashistgton, DC 20555 Attn:

Document and Corttrol Desk Re: Docket No. 50-220 DPR-63 Deat Sit:

Submitted herewith h the Report of Operating Statistics and shutdown for August 1985 for the Nine Mile Poirst Nuclear Station Unit 91.

Also included b a nartative report of Operathg Experience for August 1985.

Very truiy yours,

?

-nAL n vc Thomas E. Lempges Vice Presidentt Nacicar GeneAation TEL/tg Attachments cc: Dhec. tor, Of fice of ISE (10 copies)

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