ML20135F986

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Monthly Operating Rept for Aug 1985
ML20135F986
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 08/31/1985
From: Scott A
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20135F982 List:
References
NUDOCS 8509180047
Download: ML20135F986 (4)


Text

2 n.

Page 1 of g P&L CO PLANT PERFORMANCE DATA SYSTEM PAGE i

UN DATE 09/05/85 OPERATING DATA REPORT RPD36 UN TIME 09:41:49 ROBINSON UNIT 2 DUCKET NO. 050-0261 COMPLETED BY A.

E.

SCOTT OPERATING STATUS TELEPHONE (803)383-4524

i. UNIT NAME: ROBINSON UNIT 2 f

OTE There are presently 222 l

2. REPORTING PERIOD.: AUGUST 85 l

fuel assemblies in the Spent Fuell

3. LICENSED THERMAL POWER (MWT)- 2300 l

Pool.

I 4.

NAMEPLATE RATING (GROSS MWE) 739.0 l

[

5. DESIGN ELECTRICAL RATING (NET MWE): 700.0 l

l

6. MAX DEPENDABLE CAPACITY (GROSS MWE): 700.0 1 1
7. MAX DEPENDABLE CAPACITY (NET MWE): 665.0 8.

IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THRU 7) SINCE LAST REPORT, GIVE REASONS:

9. POWER LEVEL TO WHICH RESTRICTED IF ANY (NET MWE)

NONE

10. REASONS FOR RESTRICTION IF ANYi N/A THIS YR TO CUMUL MONTH DATE ATIVE
1. HOURS IN REPORTING PERIOD 744.00 5831.00 127061.00
2. NUMBER OF HOURS REACTOR CRITICAL 718.07 4962.75 89160.05
3. REACTOR RESERVE SHUTDOWN HRS 25.13 841.57 2778.64
4. HOURS GENERATOR ON LINE 716.42 4837.68 86903.63
5. UNIT RESERVE SHUTDOWN HOURS

.00

.00 23.20

6. GROSS THERMAL ENERGY GEN. (MWH) 1553675.76 10505261.04 173380495.20
7. GROSS ELEC. ENERGY GEN. (MWH) 508132.00 3441237.00 55786113.00 8.

Ni i ELEC. ENERGY GENERATED (MWH) 483147.00 3265239.00 52674900.00

9. UNIT SERVICE FACTOR 96.29 82.96 68.40 0.

UN1; AVAILABILITY FACTOR 96.29 82.96 68.41

1. UNIT CAP. FACTOR (USING MDC NET) 97.65 84.21 62.34
2. UNIT CAP. FACTOR (USING DER NET) 92.77 80.00 59.22 3.

UNIT FORCED OUTAGE RATE 3.71 13.97 15.10

4. SHUTDOWNS SCHED. OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)

Refueling outage beginning February 01, 1986, for 49 days.

$5. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP: N/A

96. UNITS IN TEST SIATUS (PRIOR TO COMMERCIAL OPERATION)

FORCAST ACHEIVED INITIAL CRITICALITY JCL---

22'----

INITIAL ELECTRICITY JCL---

22L---

COMMERCIAL OPERATION JCL---

JT'----

l 8509180047 850910 l

PDR ADOCK 05000261 9' h g R

PDR 1.16 - 9 s\\ s

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Page 2 of 8 3

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~

pP&L CO PLANT PERFORMANCE DATA SYSTEM PAGE i

4UN DATl OY/04/05 APPENDIX B - AVERAGE DAILY POWER LEVEL RPD39 g

AUN TIME 10:16:53 ROBINSON UNIT 2 DOCKET NO. 050-0261 COMPLETED BY A.

E.

SCOTT TELEPHor!:

(003)383-4524

%UGUST 1985

AY AVG. DAILY POWER LEVEL L)AY AVG. DAILY POWER LEVEL (MWE-NET)

(MWE-NET) 1 712 17 710 2

701 18 722 3

4S9 19 720 4

698 20 719 5

7 '. ?

21 719 6

713

,22 311

\\

7 723 23 372 8

722 24 696 9

714 25 709 00 83 26 711 Di 437 27 713 02 703 28 688 03 720 29 684 94 717 30 715 95 67'/

31 725 06 719 i.16 - 8 9

s Enclosure to Serial: RNPD/85-2877 Page 3 of 8 050-0261 DOCKET NO.

tlNII SilU1 DOWNS AND POWER REDUCilONS UNIT NAME 11. B. Robinson DATE 09-05-85 COMPLETED BY Ani t n _ F _ knt t RI PORT MONill AUGUST TELEPHONE 801-181_as7a c

Licenwe j -+,

f.

Cause A Corrective 5g 3

j 7 ".;

Date i

3g

(

2gy Event gy el Attiim to

]'

Prevent Recurrente fI 5

g p, Repori=

in U H

6 ZZ TURBIN Load was reduced to perform a turbine 0801 850802 S

B 1

valve test, maintenance on the feed-1 water pumps and two condenser water boxes. The Unit was returned to full power following the work.

0802 850810 F

18.28 A

3 85-16 TA INSTRU The Loop 3 Overtemperature AT Circuit was taken out of service for calibra-tion.

Before calibration could be performed, a concurrent signal from the Loop 2 Circuit caused a reactor trip from 100% power. The cause of the loop 2 signal was a loose connec-tion from the pressurizer signal input.

l l

I 2

1 4

I l'.uted Reasim; Metinnl:

Exhibit G Instructions S Stheduled A Lquipem Failure (Laplain) 1 Manual for Preparatiim of Data R Mai '

.e or lest 2 Manual Sciam.

Entry Sheets los Licensee.

1 Automatic Stram..

Event Report ILI R1 File INURI G-C P-g D-

..sory Resteittion 8 Othe 11 splain) 016lI sur Training A licenw I samination b

e As..elllMtf JilvC I thobit I - Same Source G-Operatrimal I ison il splain) ps/77) 11 Other 11: splam t 4

" '~

Page 4 of 8 DOCKET NO.

050-0261 UNIT SHUllK)WNS AND POWER REDUCTIONS UNIT N AME 11.

B-Rnhinann DATE 09-05-85 COMPLETED BY Anita E.

Scott REPORT MONill AUGUST TELEPHONE 803-383-4524 E

E

.5 ?

3 j5'y Licensee

,E-r, je, Cause & Corrective No.

Daic g

3y j

js&

Event

{y 93 Action to j=

4 3g=

Report u mV E'

Prevent Recurrence y

v e

c5 0803 850822 F

9.3 G

3 85-17 Hit INSTRU An operator inadvertently isolated LT-485 (steam generator level) mechan-ically prior to disabling the electri-cal circuitry, causing the Unit to trip. The Unit was returned to full load.

I 2

3 4

l' Forced Reason:

Method:

Exlubit G - Instructions S St hed uled A Lquipinent Failure (Explain)

1. Manual for Preparation of Data B-Maintenance or Test 2-Manual Scrain.

Entry Sheets for Licensee C Refueling

.I Autornatic Stram.

Event ReporiILER) File INURLG-D-Regulatory Restriction 4-Ot her I Explain) 01611 1.-Operator Training & License Exainination F-Adnunist rative 5

G-Operational Ee ror (Explain)

E sinbit I - Sarne Source 19/77)

Il Ot her (E xplain)

.