:on 960730,non-conservative Primary Grade Water Flow Rates Was Used in Boron Dilution Safety Analysis. Caused by Loss of Control of Tracking Appropriate Design Basis Calculations.Calculations Will Be Updated or Deleted| ML20134K997 |
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Millstone  |
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| Issue date: |
11/20/1996 |
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| From: |
Laudenat R NORTHEAST NUCLEAR ENERGY CO. |
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| To: |
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| Shared Package |
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| ML20134K986 |
List: |
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| References |
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| LER-96-026, LER-96-26, NUDOCS 9611200118 |
| Download: ML20134K997 (6) |
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text
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t NRC FORM 366 U.s. WUCLEAR REGULATORY COMMisslON APPROVED BY oM6 NO. 3150-0104 j
(0 95)
EXPIRES 04/30/98 l
fN O OL E T"K REO EST?50 IO RS E
D 0
s'[c"['So'"do$rR"YMOR[ARD 70 "RGkNG R
L!CENSEE EVENT REPORT (LER) l5"du'? TucttinYoTt&"482$ "s'o"e '"We^n"&
s
!Ec'SU20osEIn"'lNo"e"E8E"r" "'*EI87"oA."f8Ss$'"
4 (See reverse for required nurnber of digits / characters for each block)
FACGfrY NAME (1)
DOCKET NUMBER (2)
PAGE (3)
Millstone Nuclear Power Station Unit 3 05000423 1 of 7 TITLE (4)
Non-conservative Primary Grade Water Flow Rates Used in Boron Dilution Safety Analysis 1
EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7) oTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQUENTIAL REvlsloN MONTH DAY YEAR FACluTY NAME DOCKET NUMBER NUMBER 07 30 96 96 026 02 11 20 96 I
OPERATING THis REPORT is SUBMITTED PURSUANT To THE REQUIREMENTS oF 10 CFR 5: (Check one or more) (11)
MODE m 5
20.2201(b) 20.2203(a)(2)(v)
So.73(a)(2)(i)
So.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(n So.73(a)(2)(ii)
So.73(a)(2)(x)
LEVEL (10) 000 20.2203(a)(2 Hit 20.2203(a)(3)(ii) 50.73(a)(2)(iii)-
73.71
<x 20.2203(a)(2)(ii) 20.2203(a)(4)
So.73(a)(2)(iv>
X oTHER
""""+s" "
" " ' """ g+. ""~.20.2203(a)(2)(iii)
So.36(C)(1) 50.73(a)(2)(v) specify in Abstract below my?
or in NRC Form 366A s
LICENSEE CONTACT FOR THis LER (12) j EME TELEPHONE NUMBER linclude Area Codel R. T. Laudenat, Nuclear Licensing Supervisor (860)444-5248 J
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS TO NPROS SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR SUBMISsloN f
]
(if yes, complete EXPECTED submission DATE).
YES No ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) 1 On July 30,1996 with the unit in mode 5 of an extended cold shutdown, it was determined that the maximum Primary Grade Water System (PGS) flow rate to the charging pumps assumed in the boron dilution safety analysis contained within Chapter 15 of the Unit's Final Safety Analysis Report (FSAR) may not have been conservative.
The use of potentially non-conservative values was the result of modifications to the normal dilution pathway and inadequate review and assessment of the impact on the Boron Dilution event analysis during the design control process. Therefore, this event was reported on August 29,1996 pursuant to 10CFR50.73(a)(2)(ii)(B) as a condition outside the design basis of the unit.
The valves used to isolate the dilution pathways are currently administratively tagged closed for Technical Specification 4.1.1.2.2. Therefore, there is no safety significance associated with the present condition while the plant is maintained in Mode 5.
A detailed analysis was performed to determine the maximum system flows. Based on the results of this analysis the plant did not operate outside its design basis or in an unanalyzed condition. The programmatic conditions which initiated this event were investigated and-are identified along with appropriate corrective actions.
The FSAR will be updated to clarify the design basis dilution flow paths and the major assumptions of the boron dilution event. The justification for excluding deliberate dilutions will be added to the FSAR.
9611200118 961115 PDR ADOCK 05000423 S
PDR
,U.s. NUCLEAR REGULATORY Commission (4-95)
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL Revision Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 2 of 7 96 026 02 TEXT (If more space is required, use additional copies of NRC Form 366A) (11) 1.
Description of Event
=
On July 30,1996 with the unit in mode 5 of an extended cold shutdown, it was determined that the maximum Primary Grade Water System (PGS) flow rate to the charging pumps used in the boron dilution safety analysis contained in Chapter 15 of the Unit's Final Safety Analysis Report (FSAR) was in error. The flow rate value utilized in the boron dilution safety analysis was non-conservative. Therefore, this event was reported on August 29,1996 pursuant to 10CFR50.73(a)(2)(ii)(B) as a condition outside the design basis of the unit.
The original plant design calculation utilized 147 gpm as the maximum possible PGS flow rate. This flow rate was achieved via the emergency boration pathway. A calculation was performed in December 1983, to determine the maximum potential unborated water flow rate to the Reactor Coolant System (RCS) via the Chemical and Volume Control System (CVCS) for use in the boron dilution analysis. This calculation determined that the maximum possible PGS flow rate for two PGS pumps was 130 gpm.
A plant design change completed April 16,1986 replaced a check valve in the normal dilution pathway with one of a different size and type because of the inability to attain the design flow (120 gpm). This problem occurred during initial startup testing when using the normal dilution flow path. In addition, a procedure change was implemented at that time to allow the use of the attemate dilution pathway whenever make up of greater than 115 gpm was required.
The calculation performed in support of this design change indicated that the modification lowered the flow resistance in this pathway. The supporting calculation determined that maximum boron dilution flow for this pathway, using one pump, would be 138 gpm.
Currently the boron dilution analysis contained within Chapter 15 of the unit's FSAR is based in a Westinghouse calculation (FSE/SS-NEU 1481, " Millstone Unit 3 Boron Dilution Input," dated 7/30/90). This calculation uses the one PGS pump case with the normal make-up path it provides a maximum PGS flow of 150 gpm upon which the boron dilution analysis was based.
On July 1,1996, during the performance of system reviews plant personnel identified this discrepancy in boron dilution flow rates between the normal dilution pathway and the emergency boration pathway. During the resolution of this discrepancy, it was also determined that a potentially higher flow pathway existed. This pathway, the attemate dilution pathway, would be capable of providing greater PGS flow than had previously been considered. This pathway had not been evaluated during the boron dilution analysis. Additionally, because of several modifications to the dilution pathway, including the change out of a check valve (which decreased the path's resistance to flow) and reduction in the orifice diameter for a flow instrument (which increased the path's resistance), the actual value for the maximum dilution flow for both the one and two pump cases was uncertain. A detailed analysis was undertaken to determine the maximum system flows. This analysis was reported within the previous License Event Report (LER) supplement, submitted on October 11,1996, as having been completed. A subsequent document verification determined that at the time the LER was submitted the calculation had been prepared and was being reviewed. The calculation was approved by management on October 21,1996. The approved calculation did not change the results of the analysis nor the earlier conclusions. Based on the results of this analysis the plant did not operate outside its d: sign basis or in an unanalyzed condition.
The valves used to isolate the dilution pathways are currently administratively tagged closed for Technical Specification 4.1.1.2.2. Therefore, there is no safety significance associated with the present condition while the plant is maintained in Mode 5.
- - NRC FORM 366A U.S. NUCLEAR REGULATORY CoMMisSloN W95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVislON Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 3 of 7 96 026 02 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
11. Cause of Event
As a result of procedure changes and plant modifications to the normal dilution pathway, the flow path required to be utilized in the boron dilution safety analysis changed. This invalidated the previous boron dilution safety analysis calculations. Additionally, no calculations were performed for this pathway utilizing the two PGS pump case. In addition, the most conservative boron dilution path (altemate dilution mode flow path) was not used in the boron dilution analysis. Furthermore, because of several modifications to the dilution path, including the change out of a ch ck valve (which decreased the path's resistance to flow) and the reduction in orifice diameter for a flow instrument (which increased the path's resistance), the actual value for the maximum dilution flow in the one and two pump cases is not certain. Contributing to this situation was an incomplete description of the applicable dilution paths relative to th3 unit's design basis within Chapter 15 of the Final Safety Analysis Report (FSAR).
These conditions arose as a result of review and assessment inadequacies that occurred over several years. The programmatic deficiencies which led to this event include:
Loss of control of tracking appropriate design basis calculations.
Change in the methodology of analysis of the boron dilution event.
insufficient evaluation of the impact of plant changes on the boron dilution event.
e Errors in the FSAR description of the boron dilution event.
Lack of tracking of cumulative plant changes on the boron dilution path.
e The erroneous reporting of the completion of the analysis undertaken to determine the maximum system flows was ths result of an failure of supervision and management to verify the accuracy of the information contained within the license event report prior to submittal.
111. Analysis of Event Boron dilution is a Chapter 15 analyzed Design Basis Event. The boron dilution analysis is performed for Northeast Nuclear Energy Co. by Westinghouse Electric Corp. The accident scenario considered is the inadvertent opening of the primary water makeup control valve and failure of the blend system, either by controller or mechanical failure.
The addition of unborated water to the RCS would result in a positive reactivity insertion and a reduction of available shutdown margin. For at power operation and start-up conditions, the dilution accident reduces the shutdown margin.
For shutdown modes, the dilution accident reduces the total negative reactivity inherent in the borated RCS inventory and thereby reduces the shutdown margin which would normally be available.
The most probable limiting dilution event analyzed is the mis-operation of the CVCS system. The specific scenario id;ntified is the inadvertent operation of the primary makeup control valve (FCV-111 A) and failure of the blend system
(:ither by controller or mechanical failure). This failure permits the primary makeup water system to injc';t directly to the charging pump suction (at the Volume Control Tank outlet) without being blended with boric acid at the maximum rate permitted by the piping system. The limiti'1g dilution flow rate for this scenario has been determined to be 150 gpm for all modes of plant operation except Mode 1-automatic. The limiting dilution flow rate for Mode 1-automatic has been determined to be 120 gpm. For conservatism, all analyses for the bo,on dilution event assumed the limiting c1se flow rate of 150 gpm dilution flow. An analysis is not performed for an uncontrolled boron dilution accident
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION
~ FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 4 of 7 96 026 02 TEXT filmore space is required, use additional copies of NRC Form 366A) (11) during refueling. In this mode (mode 6), the event is prevented by administrative procedures which isolate all potentially unborated water paths to the CVCS. This precludes the addition of unborated water to the reactor vessel via CVCS.
While performing the system review it was discovered that a potentially more conservative flow path (i.e. one producing greater flow rate), the alternate dilute flow path, was not analyzed in the boron dilution analysis. This scenario also assumes identical failure modes as previously analyzed but while operating the CVCS system in an alt: mate dilute mode. While in the altemate dilute mode, the flow is provided to the top of the Volume Control Tank (VCT) via the VCT spray nozzle while simultaneously being provided to the suction side of the charging pumps, th:reby bypassing the VCT. These two flow paths are in parallel such that all fluid eventually winds up in the suction side of the charging pumps. Because the flow path in operation has changed, the previously calculated flow for two PGS pumps calculation would no longer be valid. Thus, operation of two PGS pumps could potentially place the plant in a condition outside of the Design Basis condition for the unit (i.e. two PGS pump flow rate may be in excess of 150 gpm). Although the potential exists for exceeding this dilution flow rate assumption, review of the CVCS flow control system indicates that total make-up flow deviation circuit (non-safety grade) most likely would have performed its function and terminated any dilution event within 30 seconds of initiation.
Subsequent investigation has revealed that the current Westinghouse standard practice for boron dilution safety analysis is to consider only " inadvertent dilutions". Tous neither the normal dilution nor attemate dilution pathways are included in the analysis. The justification for excluding " deliberate dilutions" from the analysis is that during intentional boron dilution operations, the plant operators are keenly aware of, and continuously monitor, the dilution process in progress for any sign of deviation or malfunction, such that the possibility of an undetected malfunction is considered remote.
Conversely, during automatic makeup mode of operation, high concentration boric acid solution is normally blended with unborated makeup water to provide a solution matching the prevailing RCS boron concentration. This blended solution is delivered into the charging pump suction at the VCT outlet. In this mode, the CVCS malfunction is defined as the failure of the blender system to provide concentrated boric acid, while the primary water flow control valve simultaneously goes to the fully open position. As a consequence, the RCS is inadvertently and unintentionally diluted. This comes at a time when the operator expects the RCS boron concentration to remain the same or to increase. Thus this operating mode forms the basis for calculating the limiting boron dilution analysis flow rates.
A calculation completed on October 21,1996 showed that for the borate / blend pathway (the boron dilution path of l
r: cord for the boron dilution analysis) the flow delivered to the suction side of the charging pumps with one PGS pump running is 132.1 gpm and with two PGS pumps running is 142 gpm. This is below the analyzed boron dilution limit of 150 gpm. Thus, while it was believed at the time of reporting of this event that the plant may have operated in an unanalyzed condition (the two PGS pumps case was not covered in the availab!e calculations or the boron dilution (nalysis), the most recent calculation shows that it was not the case. The calculation shows that even with the two PGS pumps operating, the makeup flow rate at delivered to the charging pumps is below the 150 gpm analyzed boron j
dilutio.1 limiting flow rate.
IV. Corrective Action
The corrective action for the resolution of this issue includes a detailed calculation, using the appropriate limiting flow path and accounting for any modifications that have occurred within that path, for both the one PGS pump case and the two PGS pump case. The calculation was performed and determined that boron dilution flow rate with one PGS pump is 132.1 gpm and with two PGS pumps running the flow rate is 142 gpm. Both cases show that the resulting
' NRC FORM 366A U.S. NUCLEAR REGULATORY CoMMISsloN 16 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL Revision Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 5 of 7 96 026 02 TEXT (11more space is required, use additional copies of NRC Form 366A) (11) flow rate is below the 150 gpm boron dilution limit. Thus the results of the calculation show that the plant did not operate outside its design basis.
In addition, Westinghouse and unit personnel evaluated the technical basis for use of the attemate dilute mode pathway as the limiting case for the boron dilution analysis. The results of the evaluation show that the boron dilution analysis of record did not consider the alternate dilute path or the normal dilute path because both paths are used only during deliberate plant dilution operations and deliberate dilutions are excluded from the boron dilution analysis. This is standard practice for boron dilution analysis of the FSAR Chapter 15 event. During deliberate dilutions the operators manually control dilution and have means of monitoring it so that any deviations from the expected values are identified and corrective steps are taken by the operators:
The FSAR will be updated to clarify the design basis dilution flow paths and the major assumptions of the boron dilution event. The justification for excluding deliberate dilutions will be added to the FSAR.
The calculations (for the boron dilution event) will be updated or deleted as applicable and entered into Calculation tracking database.
The programmatic conditions which allowed this event to occur were investigated and have been identified along with appropriate corrective actions. These are listed as follows:
Superseded calculations were not identified as no longer applicable e
Corrective action
Superseded calculations are currently identified on new calculation cover sheets and are further tracked as related calculations on a Calculation Tracking Program database via page two of the new calculation.
Inconsistent assumptions were used in the calculations which tried to address boron dilution flow rates.
Corrective action
The FSAR will be updated to reflect the proper assumptions, limiting fP.nypaths and number of pumps which are allowed to operate for the analyzed boro e dilution event.
In addition the calculation of record has been revised to reflect the la est applicable flow rates for the boron dilution event incorporating applicable plant c.'anges to the i
boron dilution flowpath and restating the appropriate boron dilution analysis assumptions.
The implementation of a modification of the boron dilution flowpath (via change out of a check valve to a different size and type) was not evaluated in terms of its impact on the boron dilution analysis. Specifically the 50.59 safety evaluation did not evaluate this change's impact on the boron dilution event.
Corrective action
The latest Design Control Manual Rev. 03 and related Nuclear Group Procedures for safety evaluations provide additional guidance for considering the impact of modifications on FSAR Chapter 15 Design Basis Events during the design change process. The use of an integrated Safety Evaluation was implemented after this modification was done. The use of an Integrated Safety Evaluation is an additional barrier present today which is designed to prevent this type of error from occurring.
" NRC FORM 36fA U.s. NUCLEAR REGULATORY Commission I4 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISloN Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 6 of 7 96 026 02 TEXT lif more space is required, use additional copies of NRC Form 366A) t17) i A change in the methodology for the analysis of the boron dilution event occurred. Prior to 1988 the boron e
dilution event was done in a Probabilistic Risk Assessment (PRA) type of assessment which included all j
possible boration paths evaluated as a statistical probability of that path being utilized a certain amount of time. The assumptions used in the most recent boron dilution analyses were generalin nature. Thus it was not clear as to which boron dilution flow path to use as the limiting case and what specific assumptions to i
apply.
Corrective action
In 1989, Westinghouse issued Safety Analysis Standard 4 which identified the methodology and regulatory acceptance criteria associated with the licensing basis Boron dilution accident for a plant specific FSAR or other licensing documentation. In 1990 the Boron Dilution using the methodology defined in Standard 4 was performed.
The FSAR Chapter 15 Boron Dilution Event description was changed to reflect the I
standard methodology and assumptions. Standardizing the methodology and assumptions will permit the application of consistent methodology and assumptions in any future re-analysis of the boron dilution event which might occur as the result of plant modifications or other changes.
In response to the erroneous reporting of the completion of the analysis undertaken to determine the maximum system flows the individuals involved were counseled by their supervision. Additionally, validation of factual 3
statements contained within docket submittals has been instituted within the management review process.
V.
Additional Information
Similar Events LER 96-009-00: InoDerable Shutdown Marain Monitors from Low Count Rate. Due to inadeauate Desian Control This event was attributed to an inadequate design control program. During the initial design of the SMM system, the analytical setpoint was determined to be less than or equal to a value of 2. As installed in 1991, the SMMs were conservatively set at 1.5 to account for time delays associated with low count rate operation per the vendor technical manual. A setpoint calculation specifying the minimum t,hutdown margin monitor count rate necessary for operability was not performed when the system was originally installed. This calculation was required to ensure that the hardware used to mitigate a boron dilution event met the requirements of the analysis. The lack of the minimum count rate calculation allowed the possibility for the plant to be in Mode 5 with a SMM count rate that was too low for operability of the system. The assumed accident analysis shutdown margin derived from RCS boron concentration was too low and may not have allowed the required 15 minute response time for the operator to mitigate the event with the SMM alarm setpoint set at 1.5 times the present steady state count rate.
Design Control was identified within the corrective actions as an area in which improvements had occurred in recent years. The implementation of the Design Control Manual, and the training and improvements made in the use and control of vendor services since that time were credited towards preventing future recurrences of this event.
NRC FORM 386A (4 95)
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-._..m e
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 7 of 7 96 026 02 TEXT (11more space is equired, use additionalcopies of NRC Form 366A) til) l Manufacturer Data i
None l
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| 05000336/LER-1996-001, :on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program |
- on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-001-02, :on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power |
- on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-002, :on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash |
- on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000423/LER-1996-002-02, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) | | 05000423/LER-1996-002, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1996-003, :on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements |
- on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2)(viii) | | 05000336/LER-1996-003-01, :on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys |
- on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000245/LER-1996-003-02, Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-003-01, :on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised |
- on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-004-01, :on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment |
- on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1996-004, :on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented |
- on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000423/LER-1996-004-02, :on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements |
- on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-005-01, :on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability |
- on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-005-02, :on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated |
- on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(s)(2) | | 05000423/LER-1996-005-03, :on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised |
- on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-006-01, :on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established |
- on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-006-02, :on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner |
- on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000423/LER-1996-007, :on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed |
- on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-007, :on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised |
- on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised
| | | 05000423/LER-1996-007-01, :on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable |
- on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-007-02, Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000336/LER-1996-008, :on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced |
- on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced
| | | 05000423/LER-1996-008-01, :on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism |
- on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1996-009, :on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint |
- on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1996-009-01, :on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed |
- on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-009-01, :on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change |
- on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-009-02, Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-010, :on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised |
- on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised
| | | 05000423/LER-1996-010-02, :on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted |
- on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000336/LER-1996-011-01, :on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised |
- on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised
| | | 05000423/LER-1996-011-02, :on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/ |
- on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-012, :on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/ |
- on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-012-01, :on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected |
- on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1996-012-02, :on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits |
- on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000423/LER-1996-013, :on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified |
- on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000336/LER-1996-013-01, :on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply |
- on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-013-02, :on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement |
- on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000336/LER-1996-014-01, :on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3 |
- on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1996-014-02, :on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown |
- on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-015-05, Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000423/LER-1996-015-04, Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1996-015-01, :on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures |
- on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-015-02, Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-016-02, :on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches |
- on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches
| | | 05000336/LER-1996-016-01, :on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested |
- on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-017, :on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified |
- on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-017-02, :on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised |
- on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000336/LER-1996-018-01, Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1996-018, :on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced |
- on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-019-02, :on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept |
- on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) |
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