ML20134B932

From kanterella
Jump to navigation Jump to search
Discusses Insp Rept 50-461/96-10 on 961119.Violations Noted & Being Considered for Escalated Enforcement Action
ML20134B932
Person / Time
Site: Clinton Constellation icon.png
Issue date: 01/24/1997
From: Caldwell J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Jackie Cook
ILLINOIS POWER CO.
References
NUDOCS 9701310160
Download: ML20134B932 (9)


See also: IR 05000461/1996010

Text

_ _ _ . _ _ _ _ _ _ _ . - _ _ _ . _

. _ . . _

_

, _ _ _ _ _ _

.

. .

l

f,

,

January 24, 1997

.

.

EA 96-412

Mr. John G. Cook

!

Senior Vice President

Illinois Power Company

500 South 27th Street

.

Decatur, IL 62525

)

,

SUBJECT: NRC INSPECTION REPORT NO. 50-461/96010

Dear Mr. Cook:

On November 19, 1996, NRC completed i'.s review of activities associated with

the September 6, 1996, shutdown of Clinton Power Station. Specifically,

during the evening of September 5,-operators were attempting to place the unit

in single loop operation to allow continued unit operation by isolating a

reactor coolant leak in the "B" reactor recirculation pump shaft seal package.

The details of our review of activities associated with this event and

additional findings from the independently chartered Operational Safety Team

Inspection (OSTI) were provided.in Inspection Report No. 50-461/96010 and

50-461/96011.

Based on the results of this review, fifteen apparent violations, some with

,4

multiple examples, were identified and are being considered for escalated

i

enforcement action in accordance with the " General Statement of Policy and

,

Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600.

j

Accordingly, no Notice of Violation is presently being issue.d for these

)

inspection findings. The number and characterization of the apparent

violations being considered for escalated enforcement are enclosed with this

letter.

In addition, please be advised that the number and characterization

of the apparent violations may change as a result of further NRC review.

A predecisional enforcement conference to discuss these apparent violations

has been scheduled for February 4,1997, at 10:00 a.m. in the NRC Region III

Office in Lisle, Illinois. The conference will be transcribed. The decision

to hold a predecisional enforcement conference does not mean that the NRC has

determined that a violation has occurred or that enforcement action will be

taken. This conference is being held to obtain information to enable the NRC

to make an enforcement decision, such as a common understanding of the facts,

root causes, missed opportunities to identify the apparent violations sooner,

!

corrective actions, significance of the issues and the need for lasting and

effective corrective action. Along with discussions addressing the enclosed

violations, be prepared to discuss management actions and expectations

Ik

regarding safety focus versus production and performance while in emergency

,

operating procedures as it relates to the emergency actien levels. This

discussion should focus on actions and expectations before and after the

.

September 5 event.

\\Np

9701310160 970124

S

PDR

ADOCK 05000461

s n

G

PDR

r

V

_. -

_

- - . _

.

.

4

J. G. Cook

-2-

In addition, this is an opportunity for you to point out any errors in our

'

inspection report and for you to provide any information concerning your

perspective on (1) the severity of the violations, (2) the application of the

'

factors that the NRC considers when it determines the amount of a civil

penalty that may be assessed in accordance with Section VI.B.2 of the

4

Enforcement Policy, and (3) any other application of the Enforcement Policy to

.

this case, including the exercise of discretion in accordance with Section

VII.

You will be advised by separate correspondence of the results of our

deliberations on this matter. No response regarding these apparent violations

is required at this time.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of

this letter and its enclosure will be placed in the NRC Public Document Room.

,

1

Sincerely,

i

,

James L. Caldwell, Director

,

Division of Reactor Projects

Enclosure: As Stated

Docket No.

50-461

cc:

Mr. Wilfred Connell, Vice President

P. Yocum, Plant Manager

,

Clinton Power Station

!

R. Phares, Manager-Nuclear Assessment

P. J. Telthorst, Director - Licensing

i

Nathan Schloss, Economist

Office of the Attorney General

K. K. Berry, Licensing Services Manager

General Electric Company

.

Chairman, DeWitt County Board

State Liaison Officer

Chairman, Illinois Commerce Commission

-

4

i

l

,

l

(see continued attached distribution)

,

1

a

.

.

J. G. Cook

-2-

the amount of a civil penalty that may be assessed in accordance with

Section VI.B.2 of the Enforcement Policy, and (3) any other application of the

Enforcement Policy to this case, including the exercise of discretion in

accordance with Section VII.

You will be advised by separate correspondence of the results of our

deliberations on this matter. No response regarding these apparent violations

is required at this time.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of

this letter and its enclosure will be placed in the NRC Public Document Room.

Sincerely,

James L. Caldwell, Director

Division of Reactor Projects

Enclosure: As Stated

Docket No.

50-461

cc:

Mr. Wilfred Connell, Vice President

P. Yocum, Plant Manager

Clinton Power Station

R. Phares, Manager-Nuclear Assessment

P. J. Telthorst, Director - Licensing

Nathan Schloss, Economist

Office of the Attorney General

K. K. Berry, Licensing Services Manager

General Electric Company

Chairman, DeWitt County Board

State Liaison Officer

Chairman, Illinois Commerce Commission

J. Lieberman, OE

A. B. Beach

J. Goldberg, OGC

W. L. Axelson

R. Zimmerman, NRR

H. B. Clayton

Docket File

DRP

OC/LFDCB

PUBLIC IE-01

SRI Clinton, Dresden,

RIII PRR

LaSalle, Quad Cities

Project Manager, NRR

Document:

P:\\b

g =. .

, .e s..r8\\cl i nton . en f.. .

. c . c.,, .4

..

,f

i -r - c.,, ,,s

. . f i

. --. . . w i .

--

. RI,I I ,

.

M/A

0FFICE

-

M[ik

Mb

@~dl

NAME

DATE

01/Q3/97

vt& e -ma/%

(/k6 7

'

'

0FFICIAL RECORD COPY

.

. _

_ _

. _ . _ _ _ _ _ _

. _ _ _

_ _ . _ .

_ _ _ _ _ _ _ _ _ _

__

_

_

_.

.

.

-

Attachment 1: Annarent Viohtians

i

i

!

1.

C?inton Power Station Technical Specification Section 5.4.1 requires that written

procedures shall be implemented covering the following activities: the applicable

s

i

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

'

February 1978.

4

Regulatory Guide 1.33, Revision 2, Appendix A, " Typical Procedures for Pressurized

Water Reactors and Boiling Water Reactors," (RG 1.33) states, in part, that the

q

3

following are typical safety-related activities which should be covered by written

j

procedures: procedure adherence; shift and relief turnover; log entries; authorities and

responsibilities for safe operation and shutdown; procedures for control of

"

surveillance tests; and, emergency core cooling system tests.

,

CPS 1005.14, Rev. 4, " Formatting of Procedures and Documents," states that a

j

procedural step or section marked with an * are to be performed in sequence.

!

l

CPS 3302.01, Rev.18, " Reactor Recirculation," a procedure required by RG 1.33,

i

section 8.2.4 was required to be performed in sequence as indicated by the * next to

j

the steps.

Contrary to the above, on September 5,1996, the licensee failed to perform all the

!

steps in Procedure CPS 3302.01, " Reactor Recirculation," Section 8.2.4, in sequence.

Specifically steps 8.2.4.5 and 8.2.4.6 were performed prior to the requirements of

l

step 8.2.4.3 being met.

!

!

2.

Clinton Power Station Technical Specification section 5.4.1 requires that written

j

procedures shall be implemented covering the following activities: the applicable

!

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

i

February 1978.

j

l

Regulatory Guide 1.33, Revision 2, Appendix A, " Typical Procedures for Pressurized

,

Water Reactors and Boiling Water Reactors," (RG 1.33) states, in part, that the

j

j

following are typical safety-related activities which should be covered by written

j

!

procedures: procedure adherence; shift and relief turnover; log entries; authorities and

)

responsibilities for safe operation and shutdown; procedures for control of

l-

surveillance tests; and, emergency core cooling system tests.

l

Technical Specification 5.2.2e, " Unit Staff," requires that administrative procedures

'

shall be developed and implemented to limit the working hours of unit staff who

'

perform safety related functions. Controls shall be included in the procedures such

that individuals shall be reviewed monthly by the plant manager, or his designee, to

]

ensure that excessive hours have not been assigned.

f

10 CFR 50.54(m)(2)(iii), states, when a nuclear power unit is in an operational mode

j

other than cold shutdown or refueling, as defined by the unit's technical

specifications, such licensee shall have a person holding a senior operator license of

!

the nuclear power unit in the control room at all times. In addition to this senior

operator, for each fueled nuclear power unit, a licensed operator or senior operator

i

shall be present at the controls at all times.

,

, - ,

. _ -

-

.- .. - . - - . - . - - - - - - - - - . . - .

-

. - - - - . - - .

.

.

i

s.

Procedure CPS 3317.01, Rev.16, " Fuel Pool Cooling Cleanup,", a procedure

required by RG 1.33, step 8.1.2.16 required that the inlet and outlet valves on

'

the idle spent fuel pool cooling heat exchanger be closed .

4

Contrary to the above, between September 18 and 25,1996, operators failed

to close the inlet and outlet valves of the idle 'A' train FC heat exchanger.

b.

Procedure CPS 3402.01, Rev.14, " Control Room HVAC," a procedure

required by RG 1.33, Step 8.1.1.1.1, requimd the final position of the

moisture separator drain valve OVC043B to be open and the loop seal fill

valve OVCOMB to be closed upon completion of filling the make-up (M/U)

air filter moisture separator loop seal.

Contrary to the above, on September 18,1996, the licensee failed to open the

moisture separator drain valve and close loop seal fill valve resulting in

draining of the control room ventilation loop seal.

c.

Procedure CPS 4001.01, Rev. 7, " Reactor Coolant System Leakage," a

procedure required by RG 1.33, Step 4.4 required radiation protection to be

notified, by the control rcom, if unidentified leakage exceeded 5 gpm such

that area samples and/or AR/PR trending information could be p' avided to

.

assist in detecting the location / source of the leak.

Contrary to the above, on September 5,1996, the control room failed to notify

radiation protxtion of the need to assist in the identification of unidentified

leakage in excess of 5 gpm.

d.

Procedure CPS 3005.01, " Unit Power Changes," a procedure required by RG 1.33, Step 6.1.b required the control room notify the chemistry department

after a thermal power change of greater the 15% so they could take a gas

sample.

Contrary to the, on September 6,1996, the control room failed to notify the

chemistry department after a thermal power change of greater than 15%.

e.

Procedure CPS 1401.01. Rev. 24, " Conduct of Operations," is a procedure

required by RG 1.33.

1)

Section 8.4.3.13 required the Line Assistant Shift Supervisor (LASS) to

inform the relief operator of, as a minimum, current plant status,

i

operations in progress and work to be performed in the immediate

future.

i

Contrary to the above, on September 17,1996, the LASS failed to

inform the relief operator of activities in the plant which were going to

affect fuel building differential pressure.

2)

Section 8.3.3.1 requires the shift supervisor remain in a monitoring

role during off normal operation unless he determines that the LASS is

not able to deal with the situation.

- - - .

.

. . .

. - -

_ - -

_ .. _ _

__ - _ . _ - - . . - . _ _ _

_ _ _

_ _

.

.

!

Contrary to the above, on September 6,1996, the shift supervisor

failed to remain in a monitoring role and directed activities to place the

unit in single loop operation.

3)

Section 8.4.4.10 required that significant plant operating data, such as

abnormal plant conditions and plant transients, be entered in the shift

supervisor and main control room journals.

l

Contrary to the above, on September 6,1996, no entry was made in

the shift supervisor's journal when suppression pool level exceeded the

technical specification limit requiring entry into a limiting condition for

l

operation action statement.

!

l

4)

Section 8.1.6.2.1 requires the Shift Technical Assistant (STA) to assist

l

the shift supervisor in evaluating conditions for possible entry into an

emergency classification condition; notifications to outside agencies are

not to interfere with his/her primary duties.

l

Contrary to the above, on September 5,1996, the STA failed to assist

the shift supervisor in evaluating conditions, i.e., containment

unidentified leakage, for possible entry into an emergency

classification condition.

f.

Procedure CPS 1001.01, Rev. 6, " Control of Working Hours," Step 8.7,

,

'

which implements the overtime control and review requirements of Technical Specification Section 5.2.2e, requires a group supervisor's review / approval of

i

bi-monthly Time Control Reports as a means of satisfying this control and

review requirements.

Contrary to the above, during the period between April 1006 through August

1996, monthly reviews of overtime usage by the Operations Department

personnel have not been performed.

g.

Procedure CPS 1001.05, Rev. 8, " Authorities and Responsibilities of Reactor

Operators for Safe Operation and Shutdown," which implements the

requirements of 10 CFR 50.54(m)(2)(iii), defines the "A" reactor operator

(RO) as the individual designated to fulfill the requirements to have a licensed

RO or senior reactor operator (SRO) present at the controls of a fueled nuclear

power unit at all times.

Contrary to the above, on September 18,1996, with the reactor fueled, the

"A" RO left the at the controls area for approximately 3 minutes without

obtaining an appropriate relief.

. _ . _ . _ _

. _ _ .

_

__ __..-___.._ ______ _ __._ _

__.___m

-

.

'

.

4

,

3.

10 CFR 50 Appendix B, Criterion V requires activitiss affecting quality shall be

l

prescribed by documented instructions or procedures of a type appropriate to the

l

circumstances.

I

j

Contrary to the above:

i

i

a.

As of September 1996 procedures CPS 9080.01, Rev. 40, " Diesel Generator

j

1A (IB) Operability - Manual and Quick Start Operability" and CPS 9080.02,

'

Rev 37, " Diesel Generator IC Operability - Manual and Quick Start

Operability," activities affecting quality, were not appropriate to the

j

circumstances. Specifically, Step 5.11 in both procedures prescribed

i

preconditioning of the emergency diesel generators, by priming the fuel oil

i

system prior to diesel generator starting, thereby negating the test's validity in

)

i

demonstrating the emergency diesel generators' ability to perform satisfactorily

)

l

inservice.

j

b.

As of September 1996 procedures CPS 9080.01, Rev. 40, " Diesel generator

i

1A (IB) Operability - Manual and Quick Start Operability" and CPS 9080.02,

!

Rev. 37, " Diesel Generator IC Operability - Manual and Quick Start

j

Operability," activities affecting quality, were not appropriate to the

l

circumstances. Specifically, Step 5.5.4 in both procedures prescribed

j

preconditioning of the emergency diesel generators, by "barring over" the

!

diesel prior to starting, thereby negating the test's validity in demonstrating the

)

emergency diesel generators' ability to perform satisfactorily in service.

i

c.

As of October 1996, procedure CPS 9080.02, Rev. 37, " Diesel Generator 1C

Operability - Manual and Quick Start Operability," an activity affecting quality

1

was inappropriate to the circumstances in that it failed to require the high

1

)

pressure core spray (HPCS) emergency diesel generator to be declared

j

inoperable during testing.

i

j

d.

On September 18,1996, procedare CPS 9861.02D019, Rev. 26, "LLRT for

j

'

j

1M045" (LLRT for portions of the main steam system), an activity affecting

i

quality, was not appropriate to the circumstances in that it failed to provide

necessary steps to bypass and restore a group I containment isolation signal.

,

.

1

4.

10 CFR 50.59(a)(1)(iii), " Changes, Tests and Experiments," states, in part, the

holder of a license authorizing operation of a utilization facility may conduct tests or

4

'

experiments not described in the safety analysis report, without prior Commission

j

approval, unless the proposed change, test or experiment involves a change in the

technical specifications incorporated in the license or an unreviewed safety question.

i

.

1

!

10 CFR 50.59(b)(1) requires, in part, that the licensee maintain records of tests

i

carried out pursuant to paragraph (a) of this section. These records must include a

written safety evaluation which provides the bases for the determination that the test

4

]

does not involve an unreviewed safety question.

i

i

4

i

!

.-.

- .

__

_ _ _ _ _ _ _

O

Contrary to the above:

On August 1,1996, the licensee performed a test, not described in the safety

a.

analysis report, to verify that there was no negative impact on emergency core

cooling systems (ECCS) when cycling condensate (CY) to the containment was

isolated. 'Ihe test was performed without performing a written safety

evaluation to determine that the test did not involve an unreviewed safety

question.

b.

On August 1,1996, the licensee performed a test on the water leg pump (

WLP) check valve, IE12F085A, not described in the safety analysis report, to

verify its functionality. The test was performed without performing a written

safety evaluation to determine that the test did not involve an unreviewed

safety question.

c.

Between August 2 and September 18,1996, the licensee performed a weekly

test, not described in the safety analysis report, to verify the operability of

check valve IE12F085A. The test was performed without performing a

written safety evaluation to determine that the test did not involve an

unreviewed safety question.

d.

On May 3,1995, with the reactor at power, the licensee performed a test, not

described in the safety analysis report, of the control rod drive (CRD) pumps

to determine whether a drop in CRD pressure was due to leaking valves or

CRD pump degradation. The test was performed without performing a written

safety evaluation to determine that the test did not involve an unreviewed

safety question.

5.

10 CFR 50.59(a)(1)(I), " Changes, Tests and Experiments," states, in part, the holder

of a license authorizing operation of a utilization facility may make changes in the

facility as described in the safety analysis report without prior Commission approval,

unless the proposed change involves a change in the technical specifications

incorporated in the license or an unreviewed safety question.

10 CFR 50.59(b)(1) requires, in part, that the licensee maintain records of changes in

the facility made pursuant to this section to the extent that these changes constitute

changes in the facility as described in the safety analysis report. These records must

include a written safety evaluation which provides the bases for the determination that

the change does not involve an unreviewed safety question.

Contrary to the above:

a.

Since 1989, the licensee has operated the fuel pool cooling and cleanup (FC)

system, as prescribed in CPS 3317.01, with a valve line up different from that

shown on USAR Figure 9.1-4. For example, the inlet and outlet valves on the

idle FC heat exchanger were left in the open position vice the closed position

as prescribed in CPS 3317.01. The change was made without performing a

written safety evaluation to determine that the change did not involve an

unreviewed safety question.

i

--

-

.-

-.

-

.- -

-

.-- -

-- - - .

-

-

. - - -.

-

l

O

e

e

b.

On September 17,1996, annunciator response books were observed on top of

the P-680 main control room panel. USAR section 3.1.2.2.1.0.1 states that

{

the control room had been designed to meet seismic Category I requirements.

The change was made without performing a written safety evaluation to

j

determine that the change did not involve an unreviewed safety question.

!

6.

10 CFR 50.59 (a)(1)(I), " Changes, Tests and Experiments," states, in part, the holder

i

of a license authorizing operations of a utilization facility may make changes in the

facility as described in the safety analysis report without prior Commission approval,

unless the proposed change involves a change in the technical specifications

!

incorporated in the license or an unreviewed safety question.

1

i

10 CFR 50.59(b)(1) requires, in part, that the licensee maintain records of changes in

the facility made pursuant to this section to the extent that these constitute changes in

the facility as described in the safety analysis report. These records must include a

,

i

written safety evaluation which provides the bases for the determination that the

change does not involve an unreviewed safety question.

10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Actions," states, in part,

measures shall be established to assure conditions adverse to quality, such as failures,

j

malfunctions, deficiencies, deviations, defective materials and equipment, and

'

nonconformances are promptly identified and corrected.

Contrary to the above:

l

a.

As of October 1996, the licensee had neither taken prompt corrective action

nor performed a written safety evaluation to determine if an unreviewed safety

j

question existed for the degraded cathodic protection system. Specifically, in

'

August 1995 the licensee had previously identified that the, cathodic protection

system was not adequate to protect buried piping as stated in the USAR section

9.4.5.2.

b.

As of October 1996, the licensee had neither taken prompt corrective action

nor performed a written safety evaluation to determine if an unreviewed safety

question exists for the auto-restart of the control room chillers after loss of

power. Specifically, in 1993 the licensee had previously identified that a

discrepancy existed between the as-built condition of the control room chillers

and the system as described in the USAR. The licensee had identified that the

, chillers may auto-start in 2 minutes after an event while the USAR

documented that they would start 20 minutes after an event.

,