IR 05000708/2008027

From kanterella
(Redirected from ML20132G229)
Jump to navigation Jump to search
Notice of Violation from Insp on 850708-0827
ML20132G229
Person / Time
Site: Seabrook, 05000708 NextEra Energy icon.png
Issue date: 09/18/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20132G227 List:
References
50-443-85-20, NUDOCS 8510010503
Download: ML20132G229 (2)


Text

__

__ -

.___ _

__

_ - _ - _ _

_ _ _ _

_

,

f

\\

l i

APPENDIX A

"

i NOTICE OF VIOLATION i

Public Service Company of New Hampshire Docket No.

50-443

Seabrook Unit 1 License No. CPPR-135 I

As a result of the inspection conducted on July 8 - August 27,1985 and in accordance with the NRC Enforcement Policy (10 CFR 2, Appendix C) published -in the Federal Register on March 8,1984 (49 FR 8583) the following violations were identified:

.

i i

A.

10CFR50, Appendix B, Criterion III and the Seabrook Station FSAR, Section

'

17.1.'1.3 require that the suitability of-materials and processes essential to the safety-related functions of components be reviewed and that deviations.

>

'from the appropriate quality) standards be controlled. Procedure, ASP-3 (Revision 2 New Hampshire Yankee

'

conformance report (NCR)' dispositions are used as design changes, to include

providing design details appropriate _to the identified nonconforming conditions.

i UE&C NCRs 74/1903B and 74/29148 specify repair dispositions to the limit switch j

supports on three safety-related, safety injection (SI) valves.

{

Contrary to the above, as of July. 19,1985, repair work was completed to the three subject, safety-related valve limit switch supports (1-SI-V89, V90, &

I i

V93) using design details,as specified by NCRs 74/19038 and 74/2914B, which

.

were inappropriate to the identified nonconforming conditions and which were unclear as-to specifying the controls and standards necessary to assure the ability ~of the affected components to perfonn their safety-related functions.

This lack of design change clarity resulted in the installation of material

.

and welds in conflict with engineering intent and in the failure to apply the

'

required quality assurance controls, including inspection, to safety-related j

work activities.

l This is a Severity Level IV Violation (Supplement II)'.

,

!

.

i B.

10CFR50, Appendix B, Criterion XVI and the Seabrook Station FSAR, Section

,

l 17.1.1.16 require that conditions adverse to quality be corrected.

In the

'

!

case of significant conditions adverse to quality, particularly those governed

!

by 10CFR50.55(e) requirements, the corrective measures prescribe that the actions

taken be documented and reported, as appropriate.

Seabrook Project Policy No.27 (Revision 3) specifies that in the reporting of 10CFR50.55(e) information,.

'

i corrective action is verified to have been completed by the Construction QA-organization prior to the issuance of a Final Report to'the NRC. For a re-

portable 10CFR50.55(e) deficiency on the diesel generator exhaust silencer

!

pedestal cracking, corrective action was specified to ~be the redesign and i

replacemer.t of' the original concrete pedestals with steel pedestals. The l

Final Report to the NRC, dated June 10,1985, stated that.the redesign and

l rework had been completed.

'

l Contrary to the above, as of July 8,1985, corrective action to the subject l

deficiency on the diesel generator exhaust silencer pedestal cracking had not been completed prior to the issuance of the Final Report to the NRC. Construc-

tion QA verification, in accordance with Project Policy No.27, was inadequately

)

8510010503 850918

'

PDR - ADOCM 05000443 G

PDR

-

g l

,-,_ _ _ _ _. - _ _

_ _ _ _

.

_

.c

-

.

-

.

- - - _. -

-

--

-.. _

...

.

_.

_..

~_

.

_- -

y

.

applied by relying only on documentation, in lieu of hardware, verification.

The QA program for corrective measures was also inadequate, for this case, in

.

not requiring that all safety-related work activities be examined and documented

!

in accordance with quality control acceptance criteria. These inadequacies

!

led to incomplete and unverified bolting work on the steel replacement pedestals at a time when QA docunentation and the June 10,1985 Final Report

.

indicated the corrective action rework had been completed.

,

This is a Severity Level IV Violation (Supplement II).

Pursuant to the provisions of 10 CFR 2.201, Public Service Company of New Hampshire

,

is hereby required to submit to this office within 30 days of the date of the

'

letter transmitting this Notice, a written statement or explanation in reply,

!

including for each violation:

(1) the corrective steps which have been taken and the results achieved; (2) the corrective steps which will be taken to avoid further j

violations; and (3) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

!

'

.

l

!

!

i l

I l

\\

t k

,.

!

!

!

!

!

. - -

. - -.... - - -

._.

__

. - - -. -... -

. -

. - -. -...

..

__-

- _ -...