ML20127L998

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Notice of Violation from Insp on 850425
ML20127L998
Person / Time
Site: Catawba Duke Energy icon.png
Issue date: 05/30/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20127L940 List:
References
50-413-85-14, NUDOCS 8507010035
Download: ML20127L998 (2)


Text

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... w MAY 3 01985 ENCLOSUilE 1 NOTICE OF VIOLATION Duke Power Company Docket No. 50-413 Catawba License No. NPF-35 The following violations were identified during an inspection conducted on April 25, 1985. The Severity Levels were assigned in accordance with the NRC Enforcement Policy (10 CFR Part 2, Appendix C).

1. Technical Specification (TS) 3.0.4 states that entry into an Operational Mode or other specified condition shall not be made unless the conditions i for the Limiting Conditions for Operation are met without reliance on provisions contained in the action requirements. TS 3.4.1.4.2 requires two residual heat removal (RHR) loops to be operable and at least one loop in operation when in Mode 5 with the reactor coolant loops not filled.

Contrary to the above, two RHR loops were not operable when the plant entered a condition of Mode 5 with reactor coolant loops not filled, in that on April 20, 1985, loop 1A of RHR was declared inoperable and reactor coolant loops were drained on April 22, 1985, while the RHR loop was still in an inoperable status.

This is a Severity Level IV violation (Supplement I) applicable to Unit 1.

2. 10 CFR 50, Appendix B, Criterion XI and Duke Power Company QA Topical Report, " Quality Assurance Program," Duke-1-A (Amendment 7), Section 17.2.11, require that test results be evaluated to assure that test requirements have been satisfied.

Contrary to the above, the licensee did not adequately evaluate the results of Instrument Procedure IP/0/A/3710/08, Vital Battery and Terminal Post Inspection performed on May 9,1984, July 25,1984, and July 30, 1984, in that the data recorded did not meet the specific acceptance criteria; however, neither the review by management nor Quality Control identified that the acceptance criteria was not met.

This is a Severity Level V violation (Supplement I) applicable to Unit 1.

8507010035 850530 PDR ADOCK 05000413 G PDR

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n Duke Power Company Docket No. 50-413 Catawba 2 License No. NPF-35 Pursuant to 10 CFR 2.201, you are required to submit to this office within 30 days of the date of this Notice, a written statement or explanation in reply, including: (1) admission or denial of the alleged violations; (2) the reasons for the violations if admitted; (3) _the corrective steps which have been taken and the results achieved; (4) corrective steps which will be taken to avoid further violations; and (5) the date when full compliance will be achieved.

Security or safeguards information should be submitted as an enclosure to facilitate withholding it from public disclosure as required by 10 CFR 2.790(d) or 10 CFR 73.21.

3 0 NSE Date: .

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