ML20115F964

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Revised Monthly Operating Rept for Jan 1985
ML20115F964
Person / Time
Site: Callaway Ameren icon.png
Issue date: 01/31/1985
From: Goodenow R
UNION ELECTRIC CO.
To:
Shared Package
ML20115F935 List:
References
NUDOCS 8504220077
Download: ML20115F964 (4)


Text

..

MONTHLY OPERATING REPORT DOCKET NO.

50-483 UNIT NAME CALLAWAY UNIT 1 DATE March 11, 1985 COMPLETsu BX R.

R."GOODENOW TELEPHONE (114T 676-8460 PART A OPERATIONS

SUMMARY

JANUARY 1985 Reduced load levels due to high dissolved oxygen in the condensate and the feedwater from January 1 to January 16.

Also had reduced load on January 7 due to heater drain pump seal problem.

Full power operation was maintained for the remainder of the month, except as noted in Part E.

PART B PORV AND SAFETY VALVE

SUMMARY

None I

B504220077 850313 CA-#804 A

O 3

05/09/84 QDP-ZZ-04204 Page 1 of 4 1

Part C AVERAGE DAILY UNIT POWER LEVEL 50-483 DOCKET NO.

UNIT Callaway DATE M reh 11, 1985 COMPLETED BY R. R. GCODENOW TELEPHONE (314) 676-8460 MONTH JANUARY 1985 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Neu 491 17 1102 l

I f

175 1102 2

ja 445 1098 3

9 758 1095 4

20 710 21 1079 5

1085

's 705 22 278 1056 7

23 372 987 8

24 457 1088 i.

g 3

?

453 1104 10 26 453 1107 11 27 1115 455 g

12 454 1114 13 29 459 1114 14 30 538 272 15 1011 16

.i i

0[

4 Page 2 of 4 QDP-ZZ-04204

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r Part D OPERATING DATA REPORT 50-483 DOCKET NO.

UNIT Callaway DATE March 11, 1985 R. R. Goodenow COMPLETED BY TELEPHONE (3141 676-8460 OPHATING STATUS

1. REPORTING PER Oo: January 1985 gross MOuRS IN REPORTING PERIOD:

744 3411 Max. DEPENo. CAPACITY IMWo.Neih Not vet known

2. CURRENTLY AUTHORIZED POWER LEVEL (MWt):

DESIGN ELECTRICAL RATING (MWs Net):

1171*

  • At stretch reactor power level which
3. PNER2EVEL"Tc5v0eNIERNNdtikA"N 1(

operating license.

No 1:

4. REASONS FOR RESTRICTION (IF ANY):

THIS MONTH YR TO DATE CUMULATIVE 724.5 724.5 1027.0'

5. NUMSER OF HOURS REACTOR WAS CRITICAL O

O O

6. REACTOR RESERVE SMUTDOWN MOURS 705.0 705.0 1007.s i

7

7. MOURS GENERATOR ON LINE i

O O

n

a. UNIT RESERVE SMUTDOWN MOURS i

p

9. GROS $ THERMAL EN'.RGY GENERATED (MWM)

.1 R75 R?d 1 R79 A?&

? RM 1A4 607 411 607 411 OA7 not

10. GROSS ELECTRICAL ENERGY GENERATED (MWM)..

569,311 569,311 892,334

11. NET ELECTRICAL ENERGY GENERATED IMWM) 97.4%

97.4%

98.1%

12, REACTOR SERVICE F ACTOR 97.4%

97.4%

98.1%

is. REACTOR AVAiLASILITY FACTOR 94.8%

94.8%

96.37

14. UNIT SERVICE F ACTOR 94.8%

,94.8%

96.37

15. UNIT AVAILASILITY PACTOR I

NA

__NA NA

16. UNIT CAPACITY FACTOR (Using MDCI 65.37*

6 5. 3*z*

79.RT*

17. UNIT CAPACITY F ACTOR tussng oceipi MWel 5.2%

5.2%

3.7%

18. UNIT FORCED OUTAGE RATE
19. SMUTDOWNS SCHEDULED OVER NEXT S MONTHS (TYPE. DATE. AND DURATION OF EACMI: None
20. IF SMUT DOWN AT END OF REPORT PERIOO. ESTIMATEO DATE OP STARTUP:

NA

21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

PORECAST ACHIEVED lO/2/84 INITIAL CRITICALITY INITIAL ELECTRICITY 10/24/R4 12/19/84**

COMMERCIAL OPERATION

    • Unit placed in service.

Commercial operation pending Missouri Public CA-#804 Service Commission hearing.

05/09/84 Page 3 of 4 QDP-ZZ-04204 l

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DOCKET NO.

50-483 Part E UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Callaway I) ATE March 11. 1985 R. R. GOODFNOW COMPLETED BY TELErtlONE (314) 676-8460 REPORT MONTil JANUARY 1985 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR OR NO.

DATE S: SCHEDULED IHOURS)

REASON REDUCING FOWER CORRECTIVE ACTIONSNSNTS 1

850102 Forced 10.8 A

3 Reactor Trip from 100%" Power due to feedwater isolation valve failing closed.

LER 85-001-00 2

850107 Forced 10.8 A

3 Turbine Trip from 50% Power due to indication of turbine high vibration.

LER 85-002-00 3

850131 Forced 17.4 A

3 Turbine Trip f rom 100% Power due to main generator loss of field.

LER 85-005-00 l

SUMMARY

1 1

CA-#804

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