ML20115F944
| ML20115F944 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 12/31/1984 |
| From: | Goodenow R UNION ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20115F935 | List: |
| References | |
| NUDOCS 8504220072 | |
| Download: ML20115F944 (4) | |
Text
_.
MONTHLY OPERATING REPORT DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE March 11, 1985 COMPLsTsu BY R. R. Goodenow TELEPHONE (M 4T 676-R460 PART A OPERATIONS
SUMMARY
DECEMBER 1984 During the month of December, the Power Ascension Testine Procram was completed and the unit was turned over to Load Dispatching on Decemb'er 19 at 9:30 CST.
PART 3 PORV AND SAFETY VALVE
SUMMARY
The PORV's opened on December 17 due to a pressure transient initiated by 50%
load rejection from 100% power test.
The 50% load rejection from 100% nower test was performed on December 19 with no cha11ence to the PORV's.
The safety valves were not challenged durine the month.
8504220072 850313 ~
PDR ADOCK 05000483 CA-#804 R
PDR 05/09/84 QDP-ZZ-04204 Page 1 of 4
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Part C AVERAGE DAILY UNIT POWER LEVEL 50-483 DOCKET NO.
UNIT Callaway DATE March 11, 1985 R. R. Goodenow COMPLETED BY TELEPHONE _(314T 676-8460 MONTH DECEMBER 19R4 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 977.6 17 479,8 1
127.1 975.5 ja 2
1019.4 979.0 3
3, 1087.9 1115.3 1053'.5 1105.5 21 5
1065.6 1110.5 22 4
1115.3 1094.5 7
33 1050.7 s
1117.0 24 1113 I 1118.4 25 9
1052.0 1105.0 to 26 0.0 1093.1 11 27 337.5 1093.1
~
12 g
i 1099.4 1072.3 3
13 1116.3 1111.2 34 y
832.6 1111.5 33 15 16 1102.7 I
0$70Ts4 Page 2 of 4 QDP-ZZ-04204
t f
4 t
Part D s
OPERATING DATA REPORT 50-483 DOCKET NO.
h UNIT Callaway March 11, 1985 i
DATE R. R. Goodenow COMPLETED 8Y TELEPHONE (314) 676-8460 i
1 OPERATING STATUS
- 1. REPORTING PERIOD: December 1984 GROSB MOUR$ lN REPORTING PERIOD:
302.5
- 2. CURRENTLY AUTHORIZED POWER LEVEL (MWt): 3411 MAX. DEPEND. CAPACITY (MWo Mett: Not vet knowa DESIGN ELECTRICAL RATING (MWo.Nett:
1171*
- At stretch reactor power level which o
is not currently authorized under the operating license.
- 3. POWER LEVEL TO WHICH RESTRICTED flF ANY) (MWe Nett
- 4. REASONS FOR RESTRICTION tlF ANYl:
3 THIS MONTH YR TO DATE CUMULATIVE j
302.5 302.5 302.5-
- 5. NUMSER OF MOURS REACTOR WAS CRITICAL 0
0 0
- 6. REACTOR RESERVE SHUTDOWN MOURS 302.5 302.5 302.5
- 7. MOURS GENERATOR ON LINE 0
0 0
- s. UNIT RESERVE SHUTDOWN HOURS 1,001,525 1,001,525 1,001,525
- 9. GROSS THERMAL ENERGY GENERATED (MWHI 339,180 339,180 339,180
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWM).
323,023 323,023 323,023
- 11. NET ELECTRICAL ENERGY GENERATED (MWHI j
100%
1007 1007
- 12. REACTOR SERVICE FACTOR 1007 100%
1007
- 13. REACTOR AVAILAstLITY F ACTOR 100%
100%
1007
- 14. UNIT SERVICE FACTOR 1007 1007 1007
- 15. UNIT AVAILABILITY PACTOR
- 18. UNIT CAPACITY FACTOR (Ueme MDC)
, NA NA NA 91 27*
- 91. ?7*
91.??*
- 17. UNIT CAPACITY F ACTOR (Uems Design MWel.
07 07 07
- 18. UNIT FORCED OUTAGE RATE
- 19. SHUTDOWNS SCHEDULED OVER NEXT 4 MONTHS (TYPE. DATE. AND DURATION OF EACHl: None l
l I
- 20. IF SMUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OP STARTUP:
NA
- 21. UNITS IN TEST STATUS (PRIOR TO COMMERCI AL OPERATION):
FORECAST ACHIEVED 10/2/84 INITI AL CRITICALITY 10/24/84 INITIAL ELECTRICITY l
12/19/84**
COMMERCIAL OPERATION
- Unit placed in service. Commercial operation pending Missouri Public CA 4
Service Commission hearing.
Page 3 of 4
-ZZ 04204 t
Part'E DOCKET NO.
50-483 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT N AME Callaway (JATE March 11, 1985 R. R. Goodenow COMPLETED BY TELEPilONE (314) 676-8460 REPORT MONTil DECEMHER 1984 ME THOD OF SHUTTING DOWN TYPE F: FORCED DUR ATION THE HEACTOR OR NO.
DATE S: SCHEDULED (HOURS)
HEASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS 1
841231 Scheduled 11 1
Reduced to 50% power to' clean up secondary chemistry.
SUMMARY
CA-#804
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