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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154L6551998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Catawba Nuclear Station,Units 1 & 2 ML20195E5611998-09-30030 September 1998 Revised Monthly Operating Rept for Sept 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154L6661998-08-31031 August 1998 Rev 1 to MOR for Aug 1998 for Catawba Nuclear Station,Unit 2 ML20153B2921998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Catawba Nuclear Station,Units 1 & 2 ML20153B3071998-07-31031 July 1998 Revised Monthly Operating Repts for Jul 1998 for Catawba Nuclear Station,Units 1 & 2 ML20237B2531998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Catawba Nuclear Station,Units 1 & 2 ML20236Q8071998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Catawba Nuclear Station,Units 1 & 2 ML20237B2551998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Catawba Nuclear Station,Units 1 & 2 ML20236F0321998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Catawba Nuclear Station,Units 1 & 2 ML20236Q8091998-05-31031 May 1998 Revised MOR for May 1998 for Catawba Nuclear Station,Units 1 & 2 ML20247K4451998-04-30030 April 1998 Narrative Summary Pages to Apr 1998 MOR for Catawba Nuclear Station ML20247M0251998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Catawba Nuclear Station,Units 1 & 2 ML20247M0361998-03-31031 March 1998 Revised Monthly Operating Rept for Mar 1998 for Catawba Nuclear Station,Units 1 & 2 ML20217B2271998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216E2371998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Catawba Nuclear Station ML20217B2341998-02-28028 February 1998 Revised Monthly Operating Repts for Feb 1998 for Catawba Nuclear Station,Units 1 & 2 ML20202G8641998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F4301998-01-31031 January 1998 Revised Monthly Operating Repts for Jan 1998 for Catawba Nuclear Station ML20198P3261997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Catawba Nuclear Station,Units 1 & 2 ML20202G8911997-12-31031 December 1997 Revised Monthly Operating Repts for Dec 1997 for Catawba Nuclear Station,Units 1 & 2 ML20198P3431997-11-30030 November 1997 Revised MOR for Nov 1997 for Catawba Nuclear Station,Unit 1 ML20203H5721997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Catawba Nuclear Station,Units 1 & 2 ML20199C7271997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Catawba Nuclear Station ML20203H5801997-10-31031 October 1997 Revised Monthly Operating Repts for Catawba Nuclear Station, Units 1 & 2,for Oct 1997 ML20211P9771997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Catawba Nuclear Station ML20216K1511997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for CNS ML20210L0411997-07-31031 July 1997 Monthly Operating Repts for July 1997 for CNS ML20216K1611997-07-31031 July 1997 Revised MORs for July 1997 for CNS ML20141H2221997-06-30030 June 1997 Monthly Operating Repts for June 1997 for Catawba Nuclear Station,Units 1 & 2 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
Text
. .-
OPERATING DATA REPORT DOCKET NO 50-413 DATE March 15. 1996 OPERATilE STATUS COMPLETED BY R.A. Williams 1 TELEPHONE 704-382-5346 I
- 1. Unit h ee: Catamba 1
- 2. Reporting Period: February 1, 1996-February 29,1996
- 3. Licensed Thereal Power (MWt): 3411
- 4. Nameplate Rating (Stoss MWe): 13054 Notes
- 5. Design Electrical Rating (Not MWe): 1145 (Brass NWel calculated as
- 4. Marious Dependable Capacity (Gross MWe): 1192 1450.000 MVA .90 power j
- 7. Marisan Dependable Capacity (Net MWe): !!29 factor per Page 111, )
- 8. If Changes Occur in Capacity Ratings (Itees Number 3 Through 7) Since Last NUREG-0020.- l Report. Give Reasons:
)
- 9. Power Level To Which Restricted, If Any (Net MWe): !'
- 10. Reason For Restrictions, if any:
This Month Yr.-to-Bate Cumulative
]
- 11. Hours In Reporting Period 696.0 1440.0 93553.0.
- 12. Number Of Hours Reactor Was Critical 696.0- 1369.1 73662.7
- 13. Reactor Reserve Shutdown Hours --0-- - --0--
- 14. Hours Generator On-Line 696.0 1348.9 72437.6
- 15. Unit Reserve Shutdown Hours --0-- - --0--
- 16. Gross Thereal Energy Generated (MWH) 2088420 4182470 236132729
- 17. Gross Electrical Energy Generated (ItlH) 747794 1497392 83400203
- 18. Net Electrical Eastgy Benerated (MWH) 705303 1411806 79456895
- 19. Unit Service Factor- 100.0 93.7 77.4
- 20. Unit Availability Factor 100.0 93.7 77.4
- 21. Unit Capacity Factor I!! sing i1DC Net) 89.8 86.8 74.0
- 22. Unit Capacity Factor (Using DER Net) 88.5 85.6 73.2
- 23. Unit Forced Outage Rate 0.0 6.3 8.2
- 24. Shutdown Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Refueling - June 13, 1996 - 99 dsys
- 25. If Shut Down At End Of Report Period. Estimated late of Startup:
- 26. linits In Test Status (Prior to Coseercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTR! CITY COMMERCIAL OPERATION 9603200178 960314 ~
PDR ADOCK 05000413 R PDR
1
, OPERAilll6 DATA REPORT l
DOCKET 110 50-413 till!T -Catasha i j BATE March 15. 1996 l
COMPLETED BY R.A.Ililliams 1 TELEPHDIlE 704-302-5346 i
l M0llTH February. 1996 l l
1 E AVERAGE M ILY Poller LEVEL' E AVERAGE MILY P0lER LEVEL q (Mlle*t) (llie-liet) i I 1163 17 4&B 2 1163 il 469 3 1162 - 19 556 I
4 11&1 20 1000 5 1158 21 1168 6' 1152 22 '1158 s
7 1141 23 1157 8 1139 24 1161 ____
9 1154 25. 1163 10 1156 26 1155
!! 1153 27 '1152 12 1150 28 1155 13 1132 29 1162 14 481 i
15- 458 16 459 l
l
4 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-413 UNIT NAME Um;antsa 1 .
DATE us/13/sb REPORT MONTH February 1996 COMPLETED BY x. A. nilliams TELEPHONE Ciue)-asz-dasb (1) (2) (3) (4) (5)
R MET- '
E HOD T A OF LICENSE N Y S SHUT EVENT SYS- CAUSE AND CORRECTIVE O P DURATION O WN REPORT TEM COMPONENT ACTION TO
. DATE E HOURS N RX NO. CODE CODE PREVENT RECURRENCE 6-P 96- 2-14 F --
B --
EA TRANSF MAIN POWER TRANSFORMER MAINTENANCE 7-P 96- 2-19 F --
B --
IA INSTRU NUCLEAR INSTRUMENTATION SYSTEM /
THERMAL POWER MISMATCH (1) (2) (3) (4)
F Forced Reason- Method: Exhibit G - Instructions S Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of, Data B-Maintenance or test 2-Manual Scram Entw Sneets For Licensee C-Refueling 3-Automatic Scram Event Report (LER D-Regulatory Restriction , ,
4-Other (Explain) File (NUREG-0161))
E-Operator Training & License Examination F-Administrative (5)
G-Operator Error Exhibit I - Same Source H-Other (Explain) (Explain)
_ _ _ _ . _ _ . _ _ _ _______________.___________________.________________________________s m_ _ _._____.___m
_.____________m _ _ _ _ . _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _
+
DOCKET: 50-413 UNIT: Catawba 1 e
Date: 03/15/96 NARRATIVE
SUMMARY
j MONTH: February,1996 2'
Catawba Unit 1 began the month of February operating at 100% full power. 'Ihe unit operated at or near 4
100% full power until 02/13/96 at 2045, when the unit began decreasing power and held at 45% power on i 02/14/96 from 0240 to 02/19/96 at 1514 for maintenance on main power transformers (Required per unit 2 loss of offsite power event). During power escalation, the unit held at 67% power from 1830 to 2210 due to
' nuclear instrumentation system / thermal power mismatch. The unit returned to 100% full power on 2/20/96
' at 1150 and operated at or near 100% power the remainder of the month.
4 J
4 i
i 4
Prepared by: R. A. Williams Telephone: (704)- 382 5346
~
MONTHLY REFUFI ING INFORMATION REOUEST
- l. Facility name: Catawba _ Unit 1
- 2. Scheduled next refueling shutdown: June 1996
- 3. Scheduled restart following refueling: Sep**=har 1996 THE PROJECT MANAGER HAS BEEN ADVISED BY SEPARATE COMMUNICATION OF ANY T.S. CHANGE OR LICENSE AMENDMENT. THEREFORE, QUESTIONS 4 THROUGH 6 WILL NO LONGER BE MAINTAINED IN THIS REPORT.
- 4. Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
If yes, what will these be?
l l
If no, has reload design and core configuration been reviewed by Safety Review Committee regarding unreviewed safety questions?
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information.
- 6. Important licensing considerations (new or difTerent design or supplier, unreviewed design or performance analysis methods, significant changes in design or new operating procedures).
- 7. Number of Fuel assemblies (a) in the core: 191 (b) in the spera fuelpool: SQ
- 8. Present licensed fuel pool capacity; lill )
Size of requested or planned increase: =
- 9. Projected date oflast refueling which can be accommodated by present license capacity:
September 2002 l
DUKE POWER COMPANY DATE: March 15.1996 Name of
Contact:
R. A. William
-1 l
l i
. . 4, .
l i
OPERATING BATA REPORT DOCKET NO 50-414 BATEllarch 15. 1996 GPERATilsliTAIM Coll'LETED BY R.A. Williams TELEPHONE 704-302-5346
-1. Unit Name: Catauba 2
-2. Reporting Period: February 1, 1996-February 29,1996
- 3. Licensed Thereal Poser (IEft): 3411
- 4. Naseplate Rating (Bress Igle): 13055 Notes eNaseplate Rating.
- 5. Design Electrical Rating (llet IRie): 1145 (Stess INiel calculated as
. 6. Maxieue Dependable Capacity (6ress ille): 1192- 1450.000 MVA .90 poser
. 7. Marious Dependable Capacity (Net INie): 1129 .
facter per Page ill,
- 8. If Changes occur in Capacity Ratings (itses llueber 3 Through 7) Since Last NURE6-M20.
! : Report. Give Reasons:
. 9. Power Level.To lihich Restricted, if Any (llet Ille):
'10. Reason For Restrictions, if any u.
i This llenth Yr.-to-Date Casulative f
! 11. Hours In Reperting Perled' 696.0 1440.0 83569.0'
.- 12. Ilmeber Of Hours Reacter lias Critical ' 453.3 .1197.3 65363.5~
- - !!3.ReacterReserveShutdownHours --0-- ; 14. lieurs Generator On-Line- 415.1 .'1159.1 64296.7
-15. Unit Reserve Shutdown Hours - . ~- -
l - 16. Sress Thereal Energy Benerated (IIIH) 1387556 3916194' 207332732 i' 17. 8tess Electrical Energy Generated (IllH) 492873 1 4 2297 . 73'M664
-'18. list Electrical Energy Generated (IllH) 462214 1327684 69239941-
- 19. Unit Service Facter 59.6 80.5 76.9
- 20. Unit Availability Facter 59.6 00.5 76.9 i 21. Unit Capacity Facter (Using 110C liet) 58.8 -II.7 73.2
'22. Unit capacity Facter (Using DER Wet) 58.0 80.5 72.4
- 23. Unit Forced Outage Rate W.4 19.5 9.1 j --24. Shutdeen Scheduled Over liest 6 llenths (Type, Date, and Duration of Each): j 4
None
- 25. If Shut Down At End Of Report Period. Estimated late of Startup:
- 26. Units In Test Status (Prior to Ceasercial Operation): Ferocast- Achieved j- INITIALCRITICALITY !
4 Ill!TIAL ELECTRICITY j C0filERCIAL OPERAT1011 I
i t ,
J
=-%i ri-r -, ;r- , , -
.-4 w-- - . - -
- g. p
. - - . . . ~ . . . . . . - . . . ..-.~. ....- - . - - -- ..- . .. . . _ . . . . - . ~ - . . . .-.
i
. OPERAi!N M TA REPORT l i i 1 l -
. DOCKET IN) 50-414
! ILili Catada 2 .
MTE Marth 15. I996 !
CS FLETED BY R.A.ll1111a== !
TELEPlWE 7M-3R2-53M i l' !
j !
L !
llBitTH Februarv. 1996 .
l e,
l
~
! My, . AYERASE MILY P0llER LEVEL- 31 AYERAIE MILY poler LEVEL l'
(llie-itet) (Illie-list) -
L ~1 11&& 17 0 .
'2 1163 II 3&5 '
i .- 3 1165 19 1129
+
4 .- 1L&& 20 1146
.5 1166 21 1153
~
6- 608 22 1151
.. . t 7 0 23- 1151
.i
- l. ;
r
'S 0 M- 1158 l 9 0 25 1163 i
.i
- 10 0 26 1160 '
t 1
11 0 27 1159 1 I
. 12 0 28 1160 -) ,
. 13 0 29 1167
\ .
14 0 1
- 15 : 0 16 0 I
i i
I-
. _ . . , _ - . . - J ., _ . . _ . . . . _ , _ __'
.__m. . _.m.. .._ .- ._ . -_ _ _. . _ _ _ _ .-
UNIT SHUTDOWNS AND POWER REDUCTIONS ' DOCKET NO. 50-414 /
UNIT NAME uu; Antea 2 .
DATE ud/1d/sb REPORT MONTH February 1996 COMPLETED BY x. A. williams TELEPHONE t ius ; -s ese-ose 6 (1) (2) '(3) (4)' (5)
R MET-E HOD -
T A OF LICENSE N Y S SHUT EVENT SYS- CAUSE AND CORRECTIVE O P DURATION O DOWN REPORT TEM COMPONENT ACTION TO
. DATE E HOURS N R/X NO. CODE CODE PREVENT RECURRENCE 1 96 6 F 280.95 A 3 EA XXXXXX REACTOR TRIP DUE TO LOSS OF OFFSITE POWER 1-P 96- 2-18 S --
B --
HA VALVEX MAIN TURBINE CONTROL VALVE MOVEMENT TESTING 2-P 96- 2-18 F --
B --
IA INSTRU NUCLEAR INSTRUMENTATION CALIBRATION t
(1) (2) (3) (4)
F Forced Reason- Method: Exhibit G - Instructions S Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of, Data B-Maintenance or test 2-Manual Scram Ent y Sneets For Licensee C-Refueling 3-Automatic Scram (LER D-Regulatory Restriction 4-Other (Explain) Event File Report (NUREG-0161))
E-Operator Training & License Examination F-Administrative (5) l G-Operator Error Exhibit I - Same Source l H-Other (Explain) (Explain) ,.
4
_ _ . ._._ _ _ _ - _ _ _ _ _ _ _.________m__.____.-.______.__-______-.-__._..___m.._._m__m.-_-_.___..-m_ _ . _ _ _ _ _ . . _ _ _ _ _ . _ _ _
-I, 4
I DOCKET: 50-414 UNIT: Catawba 2 Date: 03/15/96 1 NARRATIVE
SUMMARY
MONTH: February,1996 Catawba Unit 2 began the month of February operating at 100% full power. De unit operated at or near 100% full power until 02/06/96 at 1230, when the unit tripped due to loss of offsite power. The unit was placed on-line 02/18/96 at 0528. During power escalation, the unit held at 64% power from 1700 to 1808 - .
I due to main turbine control valve movement testing. He unit held at 69% power from 1843 to 2253 due to nuclear instrumentation calibration. De unit returned to 100% full power on 02/23/96 at 1630 and operated at or near 100% power the remainder of the month.
)
i l
l i
-I Prepared by: R. A. Williams Telephone: (704)- 382-5346
MONTHLY REFUFI tNG INFORMATION REQUEST
- 1. Facility name: Catawba. Unit 2
- 2. Scheduled next refueling shutdown: March 1997
- 3. Scheduled restart following refueling: May 1997
! THE PROJECT MANAGER HAS BEEN ADVISED BY SEPARATE COMMUNICATION OF i
ANY T.S. CHANGE OR LICENSE AMENDMENT. THEREFORE, QUESTIONS 4 THROUGH 6 WILL NO LONGER BE MAINTAINED IN THIS REPORT.
i ,
I l l 4. Will refueling or resumption of operation thereafter require a technical specification change or !
otherlicense amendment? j Ifyes, what will these be?
If no, has reload design and core configuration been reviewed by Safety Review Committee regarding unreviewed safety questions?
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information. I l
- 6. Important licensing considerations (new or different design or supplier, unreviewed design or j l performance analysis methods, significant changes in design or new operating procedures).
i
- 7. Number of Fuelassemblies (a) in the core: 121 (b) in the spent fuelpool: 524 l
- 8. Present licensed fuel pool capacity: lill j Size of requested or planned mcrease: =
i
- 9. Projected date oflast refueling which can be accommodated by present license capacity:
September 2011 ;
l DUKE POWER COMPANY DATE: March 15.1996 Name of
Contact:
R. A. Williame Phone: (704)- 382-5346 i
i'