ML20093J038

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Part 21 & Deficiency Rept Re Unconsidered Effects of Superheated Steam Generated by Steam Generator for Main Steam Line Break Analysis,Resulting in Increased Doghouse Temps Outside Containment.Next Rept Expected by 840831
ML20093J038
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 07/09/1984
From: Tucker H
DUKE POWER CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
REF-PT21-84-368-000 PT21-84-368, PT21-84-368-000, NUDOCS 8407250526
Download: ML20093J038 (3)


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Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30303 Re: Catawba Nuclear Station Units 1 and 2 Docket Nos. 50-413 and 50-414

Dear Mr. O'Reilly:

Pursuant to 10 CFR 50.55e, please find attached a Significant Deficiency Report No. SD 413-414/84,16.

Very truly yours, Hal B. Tucker LTP/rbs Attachment cc: Director Office of Inspection and Enforcement Mr. Robert Guild, Esq.

.U. S. Nuclear Regulatory Commission Attorney-at-Law Washington, D. C.

20b50 P. O. Box 12097 Charleston, South Carolina 29412 NRC Resident Inspector Catawba Nuclear Station Mr. Jesse L. Riley Carolina Environmental Study Group Palmetto Alliance 854 Henley Place 21351 Devine Street Charlotte, North Carolina 28207 Columbia, South Carolina 29205 INP0 Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 m!FICI AL CO

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DUKE POWER COMPANY CATAWBA NUCLEAR STATION Report Number: 413-414/84-16 Report Date:

July 9,1984 Facility:

Catawba Nuclear Station Units 1 and 2 IDENTIFICATION OF DEFICIENCY:

Unconsidered effects of superheated steam generated by steam generator for Main Steam Line Break analysis could result in increased doghouse temperatures outside containment. This could possibly preclude safety related components from performing their intended safety function. The potential deficiency was identified May 11, 1984.

Initial Report: On June 8,1984, Mr. Kerry Landis, NRC Region II, Atlanta, Georgia, was notified by telephone of the subject deficiency by L. M. Coggins and R. R. Weidler of Duke Power Company, Charlotte, N. C. 28242.

Component and/or Supplier:

Duke Power Company is responsible for the doghouse environmental analysis. The MSLB analysis is accomplished utilizing input information supplied by Westinghouse, Water Reactor Division.

Description of Deficiency:

Revised information has been received from Westinghouse giving mass / energy release rates for a Main Steam Line Break (MSLB) inside containment. The original Westinghouse information indicated a saturated steam condition from the steam generators; however, revised infonnation identifies steam generator tube uncovery and the formation of superheated steam.

Duke Power had previously assumed the same saturated steam condition for a MSLB in the doghouses located outside containment. Equipment important to safety for mitigating an MSLB in the doghouses has been identified (see list in corrective action below). Environmental qualification paramegers for the doghouses are currently based on original analysis results of 330 F.

Utilizing the new data from Westinghouse, revised Duke Power environmental analysis v ith superheated steam gonditions indicates gn increase in doghouse temperature from the present 330 F parameter to a 440 F revised maximum doghouse temperature.

ANALYSIS OF SAFETY IMPLICATIONS: Subjecting safety relgted components to temperatures higher than the qualification basis of 330 F could possibly preclude components from performing their intended safety functions following a postulated MSLB in either doghouse.

Corrective Action:

In order to resolve the subject problem, analyses are being performed by Duke Power Company and Westinghouse. Safety related equipment potentially impacted by MSLB temperatures higher than the equip-ment qualification envelopes is as follows:

  • Doghouse Level Instrumentation
  • Feedwater Supply to Upper Nozzle Isolation Valves
  • Tempering Isolation Valves
  • Steam Generator Blowdown Isolation Bypass Valves Westinghouse is performing a main steam line break analysis for a spectrum of break sizes and power levels (matrix) to determine when required safety system actuations occur relative to the initiation of superheat in the affected doghouse. Results will be used in determining if required safety functions can be performed prior to the time doghouse equipment qualifi-cation parameters are exceeded. Where potential failures of safety related equipment can be shown to occur, additional systens analyses will be performed to determine acceptability of consequences. If any unacceptable consequences are shown following completion of the analysis, then Duke Power will develop and implement the necessary corrective measures.

The Westinghouse analysis work to determine the matrix of protection system actuation and superheat initiation times will be completed by July 31, 1984.

The target date for Duke Power to evaluate the Westinghouse analysis and determine final actions required to resolve this issue, if any, is August 31, 1984. A supplementary report detailing the results of these activities will be forthcoming on or before this date.

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