ML20090D270

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Augmented Insp Team Rept 50-254/92-07 on 920208-13.No Violations or Deviations Noted.Major Areas Inspected: Response to Scram & Equipment Failures on 920206 & 07
ML20090D270
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/26/1992
From: Burgess S, Jablonski F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20090D276 List:
References
50-254-92-07, 50-254-92-7, NUDOCS 9203060124
Download: ML20090D270 (18)


See also: IR 05000254/1992007

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AUGMENTED INSPECTION TEAM REPORT

U.-S. NUCLEAR REGULATORY COMMISSION

QUAD CITIES UNIT 1 REACTOR SCRAM AND ASSOCIATED EQUIPMENT FAILURES

FEBRUARY 27, 1992

INSPECTION REPORT N0, 50-254/92007(DRS)

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-TABLE OF CONTENTS

1.0

Introduction ................................................ 1

1.1

Event Summary ............................................... 1

1.2-

AIT Formation ............................................... 1

1.3

AIT Charter ................................................. 2

2.0

De scri pti on of the Event . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

2.1

Sequence of Events .......................................... 2

2.2

Operator Response ........................................... 4

3.0

Inspection Results .......................................... 5

3.)

The Cause of.the Reactor Scram .............................. 5

3.2

Equipment Failures or Mal functions . . . . . . . . . . . . . . . . . . . . . . . . . . 7

3.2.1

Fail ure o f the HPCI Stop Valve . . . . . . . . . . . . . . . . . . . . . . . . . , . . . . 7

3.2.2

Failure of "C" Electromatic Relief Valve . . . . . . . . . . . . . . . . . . . . 8

3.2.3

Failure of Reactor feed Pumps to Automatically Trip

........10

3.2.4'

Main Steam Line Flow Instrument Anomalies . . . . . . . . . . . . . . . . . .11

3.2.4.1

Off Normal Instruments ..................................... 12

3.2.5

Other Less fignificant Equipment failures .................. 12

4.0

Conclusions ................................................ 13

5.0

Exit Interview ............................................. 14

AIT Charter ...................................... Attachment 1

February 7, 1992 CAL . . . . . . . . . . . . . . . . . . . . . . . . . . . . . Attachment 2

Personnel Contacted . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . Attachment 3

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

P2 port No. 50 254/92007(DRS)

Docket No. 50-254

License No. DPR 29

Licensee: Commonwealth Edison Company

1400 Opus Place

Downers Grove, IL 60515

. Facility Name:

Quad Cities Nuclear Power Plant, Unit 1

Inspection At:

Quad Cities Site, Cordova, IL

Inspection Conducted:

February 8 - 13, 1992

Inspectors: F. L. Brush, Resident Inspector - Clinton Po w Station

F. P. Paulitz, NRR, Instrument & Control Systems Branch

R. M. Pulsifer, NRR, Division of Reactor Projects, PD Ill-2

D. E. Roth, RIII-(observer)

H. A. Walker, Rill, Maintenance and Outages Section

.

Approved By:

DD h*b

2-2'-3I

ohia D. Bur'gess

Date

T am Leader

Approved By:

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. Frank J. aablonski, Chief

Date

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Maintenance and Outages Section

Inspection Summary

Inspection on February 8 - 13. 1992 (Recort No.- 50-254/92007(DRS))

Areas Inspected:

Special Augmented Inspection Team (AIT) inspection conducted

in response to the Quad Cities Unit I scram and equipment failures which

occurred on February 6 and 7, 1992. The review included validation of the

sequence of events, the cause of the reactor scram, the failure of the HPCI

stop valve, the failure of the "C" relief valve, the apparent failure of the

reactor _ feed pumps to automatically trip at the appropriate vessel level and

related operator actions, anomalies associated with the main steam line flow

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instruments, and evaluation of the licensee's corrective actions.

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Results:

No violations or. deviations were identified in any of the areas

inspected. No significant operational safety parameters were approached or

. exceeded. .The AIT concluded the following:

1.

The root cause could not be determined for the main steam high flow trip

signal, which caused the Group I isolation that ultimately led to the

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reactor scram.

The licensee had performed reasonable analyses and

testing to determine root cause. Additional equipment to monitor for

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abnormalities within the main steam high flow trip system was installed

prior to Unit I start-up.

2.

The failure of the HPCI stop valve was attributed to an inadequate

maintenance work package, which was performed in February 1991.

The

work package was considered inadequate because it did not include as-

found or as-left readings of the clearances between the poppet guide and

valve poppet.

After welding was performed on the poppet guide assembly,

incorrect tolerances caused the valve to eventually become stuck in the

open position during HPCI testing conducted on February 6,1992.

3.

The failure of the "C" Electromatic Relief Valve (ERV) was attributed to

brass dust on the shorting contact bar, which was caused by n.atn steam

system vibration.

The licensee determined that the dust originated from

brass components near the shorting contact bar,

in addition, the AIT

concluded that deficient preventive maintenance for the ERVs existed.

Although previous ERV failures indicated high resistance readings across

the contact shorting bar, the licensee did not evaluate the possibility

of adding preventive maintenance to periodically obtain resistance

readings and clean the shorting bar. Also, the licensee did not pursue

obtaining experience from other Ceco nuclear plants that have the same

type of relief valves.

Preventive maintenance practices may have

precluded the failure of the "C" relief valve.

4.

The apparent failure of the Reactor Feed Pumps to automatically trip at

the appropriate vessel level was attributed to instrument drift.

Because the trip setpoint for one of the two level indicating switches

had drifted from +48 inches to +53.5 inches, neither of-the RFPs would

have tripped automatically at the expected trip point.

Operator actions

manually tripped the RFPs before reaching the respective trip settings;

however, if manual actions had not been taken the pumps would have

automatically tripped at +53.5 inches.

5.

Anomalies associated with the "B", "C", and "0" main steam line flow

indicators, were attributed to a faulty power supply and square root

converters. These instruments are for indication only and are different

from the transmitters that provide the reactor protection shutdown.

The

control room flow indicators had "Off Normal Instruments" or ONI

stickers on the front, which meant that maintenance was needed to repair

previously identified problems of false flow indications.

These

erroneous flow indications occurred again after the MSIVs were closed

during this event and resulted in personnel being sont into the plant to

look for steam leaks that didn't exist.

The AIT was concerned the

operator's attention was diverted because of indicators that needed

repair.

.The team concluded that the operators performed well in mitigating the

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consequences of the reactor scram and Group 1 isolation.

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1.0

Introduction

1.1

Event Summarv

On February 7, 1992, at 2:01 a.m., the Unit I reactor scrammed from 100

percent power after an erroneeus main steam line high flow signal apparently

caused the main steam isolatici valves (MSIV) to close automatically. During

the event, the high pressure ctolant injection (HPCI) system was out of

service and in day 1 of a 14 da.' Limiting Condition for Operation (LCO).

Immediately following the main steam isolation and reactor scram, the control

room operators manually tripped the "B" reactor feed pump (RFP) prior to the

expectes trip setpoint of +48 inches, the "A" RFP was also tripped by

operators after reactor water level exceeded the RFP trip setpoint of +48

inches, lhe "C" RFP automatically started and was also tripped by operators.

To lower reactor pressure, the operators opened the "B" electromatic relief

valve (ERV).

Once pressure dropped to an acceptable level, the "B" ERV was

closed. The reactor core isolation cooling-(RCIC) system was also manually

initiated to control reactor pressure, The operators attempted to open the

"C" ERV; however, the valve did not respond.

The "B" ERV was again opened to

control pressure.

During the event, the "B", "C", and "D" main steam line flow indicators

indicated a small amount of steam flow with the MSIVs closed. A team of

personnel was sent into the plant to inspect for steam leaks.

When no leaks

were identified, seven of the eight MSIVs were reopened. The "B"

inboard MSIV

was left closed due to a continued concern with the "B" main steam line flow

indication.

At 3:17 a.m., the reactor scram was reset and at 4:00 a.m. the RCIC pump was

taken off line.

1.2

Auamented Inspection Team Formation

Subsequent to the reporting of this event, Region III managers determined that

an Augmented Inspection Team (AIT) was warranted to gather information on the

causes, conditions, and circumstances relevant to several equipment failures

associated with the reactor scram. On Friday, February 7, 1992, an AIT was

formed consisting of the following personnel:

Team Leader:

S. D. Burgess, Team Leader, RIII - Maintenance and

Outages Section

Team Members:

F. L. Brush, RIII - Resident Inspector, Clinton Power

Station

F.- P. Paulitz, NRR - Instrument & Control Systems

Branch

R. M. Pulsifer, NRR - Division of Reactor Projects, PD

III-2

D. E. Roth, RIII - Observer

H. A. Walker, RIII - Maintenance and Outages Section

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The team arrived on site during the morning of February 8, 1992.

In parallel

with formation of the AIT, Rlli issued a Confirmatory Action Letter (CAL) on

February 7, 1992, which confirmed certain actions in support of the team and

established conditions required to be met prior to the restart of the plant

(Attachment 1).

1.3

AIT Charter

A charter was formulated for the AIT and transmitted from T. O. Martin to

S. D. Burgess on February 7, 1992, with copies to appropriate EDO, NRR, AE00,

and Rill personnel (Attachment 2).

The AIT was terminated on Thursday, February 13, 1992.

2.0

Description of the Event

2.1

Seouence of Events

At the AIT's request, a chronology of events related to the scram on February

7,1992, was assembled by the licensee.

The chronology, which included

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operator actions, was verified to be accurate by AIT personnel by review of

operating logs and interviews with licensee. operating personnel.

The

chronology was as follows:

NOTE: All times are in Central Standard Time.

Jnitial Conditions

Unit 1

820 MWe

HPCI out of service (day 1 of 14)

Unit 2

Refueling outage - core unloaded

Reactor water level at flange

Time

Event Descripti_o_n

01:59

Center desk nuclear station operator (NS0) leaves control room.

02:01:06

Reactor scram, Group I isolation (MSIV closure)

02:01:09

Group 11 and 111 trip.

02:01:53

"B" RFP manually tripped by Unit 2 NSO.

NSO resumed duties on

Unit 2 by direction of Shift Control Room Engineer (SCRE).

02:02

Center desk NSO enters control room.

SCRE initiated entry into

abnormal procedure QGA 100.

02:02:53

Reactor water level indicates +48 inches on the "A" and "B" Yarway

instruments.

GEMAC level indicates +56 inches.

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02:03

Shift engineer _(SE) enters control room.

Reactor water level:

GEMAC = +56 inches, Yarways >50 inches.

02:03:46

"A" RFP manually tripped by Unit 1 NSO.

02:03:46

"C" RFP automatically comes on.

RFP standby position was not

deselected.

02:03:48

"C" RFP turned off.

02:05:52

Reactor pressure at 1041 psig.

02:06

Extra NSO opens "B" ERV to lower reactor pressure.

02:07

Extra NSO places residual heat removal (RHR) in torus cooling

mode.

02:08:09

Reactor water cleanup blowdown flow established.

02:10

Communications center senior reactor operator (SRO) notifies the

Assistant Superintandent of Operations (AS0)_of event.

02:12

Shift foreman dispatched to inspect for steam break by SE.

SE

sent equipment attendants (EAs) to RHR to inspect immediately,

nothing found.

SE sent instrument maintenance foreman to check

main steam line flow differential pressure (dP) instruments.

All

were consistent.

02:12:05

"A" RFP turned on.

02:14

Extra NS0 closes "B"

ERV.

02:19

Extra NSO placed RCIC-in service to control reactor pressure.

02:29

Extra NSO attempts to open "C" ERV to control pressure.

Valve did

not open-as indicated by position lights, acoustic monitors, steam

flow, alarms, and pressure indication.

. 02:29:38

Extra NS0 opens "B" ERV to control pressure.

02:30:36

"A" RFP turned off.

02:32

ASO contacts control room for briefing.

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02:33:15

"A" RFP on.

SCRE monitoring level per procedures.

02:33:17

Group II and III isolation.

. 02:35

"B" ERV closed.

02:53

Group I isolation reset. Area inspections show no visible

indications of a steam leak.

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02:58

.Seven MSIV's opened by extra NSO.

"B" inboard MSIV left closed

due-to concern with flow indication.

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03:15

NRC resident notified of event.

03:17

Reactor scram reset.

03:30

AS0 notified nuclear d"ty officer of event.

04:00

RCIC turned off.

Condensate and feedwater system used for reactor

level control.

04:02

Exited abnormal procedure QGA 100,

04:12

Emergency notification completed for engineered safety feature

(ESF) actuations.

04:15

ASO notifies Technical Superintendent of event.

05:42

"A" RFP shutdown by Unit 1 NSO.

06:30

MSIVs closed to determine if MSIV flow obstruction existed.

All

MSIVs determined to be functional and isolatable.

2.2

Operator Response

The team reviewed plant logs, appropriate plant emergency and off-normal

procedures, and interviewed the operating crew to determine what actions were

taken in response to the event and the suitability of those actions.

On February 7, 1992, prior to the event, the operators were performing routine

functions with no major evolutions or plant transients in progress.

The HPCI

system was in day 1 of a 14 day LC0 for corrective maintenance as detailed in

section 3.2.1.

-The initial event information noted by the operators was as

follows:

e Annunciator

" Channel B Main Steam Line High Flow"

e All MSIVs indicated shut

e Reactor scram

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At 2:01:06 a.m. on February 7, 1992, an automatic reactor scram occurred when

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the MSIVs closed on a main steam line high flow signal.

Almost immediately,

the Unit 2 NSO removed the "B" RFP from service after reactor vessel level,

which had reached a minimum of -20 inches below instrument zero, started to

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increase. This was a normal action for the operators since the feedwater

regulating valves had a history of seat leakage when fully closed.

The SCRE

initiated entry into Quad Cities General Abnormal Procedure QGA 100, "RPV

Control," because reactor water level had decreased below +8 inches during the

event.

The following procedures were used as a result of the entry in QGA

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100:

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e Quad Cities Operating Procedure QCOP 3200 9, " Condensate /Feedwater"

e Quad Cities Operating Procedure QCOP 1300-2, "RCIC System Manual

Start-Up" (Injection / Pressure Control)

e Quad Cities General Procedure QGP 2-3, " Reactor Scram"

'After the shift engineer directed recovery operations, the Unit 1 NS0 removed

the "A" RFP from service after reactor water level exceeded the RFP trip

setpoint of +48 inches. The "C" RFP automatically started because the

operator failed to place the

"C" RFP switch in the "0FF" position before

securing the "A" RFP. Additional information on this action is contained in

section 3.2.3 of this report. The extra NS0 opened the "B"

ERV to control

reactor pressure and also placed RHR in torus cooling. At 2:12:05 the "A"

RFP

was placed in service. After pressure had decreased, the "B" ERV was closed

and the RCIC pump was placed into service to control reactor pressure;

however, the RCIC pump was not used to inject water into the reactor vessel.

As pressure again began to increase, the "C" ERV failed to respond when an

operator attempted to open it. A detailed discussion of this failure is

contained in section 3.2.2.

Immediately, the operator opened the "B"

ERV.

The "A" RFP was then secured for three minutes to control reactor water level.

Again, after pressure had decreased, the Unit 1 NSO closed the "B"

ERV.

Early in the event the SCRE requested that IM personnel check the MSIV high

flow sensors. After checks were made, the IMs reported that there were no

apparent problems. The operator also noticed anomalies with the "B", "C",

and

"D" main steam line flow indications.

Because these instruments indicated a

small amount of flow when the MSIVs were closed, a team of personnel was sent

into the plant to inspect for signs of a steam leak. No leaks were identified

and seven of the MSIVs were reopened.

The "B" inboard MSIV was left closed

due to a continued concern with the "B" main steam line flow indication.

Further discussion of these anomalies is contained in section 3.2.4.

At 3:17 a.m., the reactor scram was reset and at 4:00 a.m. the RCIC pump was

taken off line and procedure QGA 100 was exited.

The shift engineer also

reviewed Quad Cities Abnormal Procedure QGA 200, " Primary Containment

-Control," during the event and determined that plant conditions did not

require entry into that procedure.

Based on review of this event and operator interviews, the team determined

that the operators performed well in responding to the plant transient.

Their

actions were prudent and conservative, placing the plant in a stable condition

in a very short time.

3.0

Jm nection Results

3.1

The Cause of the Reactor Scram

The cause of the Group I isolation signal, which resulted in the closure of

the MSIVs, and ultimately in the reactor scram, could not be determined. When

the reactor scrammed, only the "B" Channel High Steam Flow annunciator was

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the reactor scrammed, only the "B" Channel High Steam flow annunciator was

received in the control room. No alarms were received for the "A" Channel

High Steam Flow, the A and B Group I isolation annunciators, High Steam Flow

or Group I Isolation computer point alarms nor any other Group I isolation

alarms.

The Group I isolation signal comes from Barton Model 27B differential pressure

indicating switches (DPIS), four of which are connected to each flow element

with a flow element on each of the four main steam lines.

Thcse 16 DPISs are

located in the RHR room in the southeast corner of the reactor building

basement.

Eight of the switches are on panel 2201-10 sections A and B and

eight are on section C.

In order to achieve a full Group I isolation, one of

the eight DPISs in each channel must actuate, which will cause the MSIVs to

close and scram the reactor.

The licensee speculated that the Group I isolation was caused by a spurious

actuation of the DPISs, possibly by personnel bumping the racks or instruments

since this had occurred-in the past.

The sei.uriiJ card readers and radiation

protection control records indicated only three per:onnel could have been in

the area of the racks when the plant scrammed; however, ir+arviews with these

personnel indicated that they were not in the immediate area of the

instruments when the event took place.

The licensee-performed a functional check and calibration of the trip

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circuitry.

One DPIS was replaced and all indications and inputs to

annunciators and computer points worked correctly.

To determine whether bumping of these instruments or racks could have caused

the reactor scram, the licensee conducted a special test that pressurized the

DPISs to a pressure differential close to the trip setpoint.

The torus bulk

head door and rack enclosure door were slammed. The impulse sensing lines,

racks, and instruments were bumped for trip susceptibility.

No alarms were

received for high steam flow or Group I isolation as the result of the special

test.

The licensee also checked several of the flow check valves in the sensing

lines _and determined that_there was no blockage.

Walkdowns of the sensing

lines and the electrical wiring from the instrument racks to the circuit fuses

and trip relays (102 A through D) in the control room panels were performed

- but no abnormalities were identified.

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The AIT team inspected the instrument racks to determine the degree of

protection of the instruments on the racks from accidental bumping.

The

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probability of bumping these instruments or a rack when passing from the torus

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area to the stairwell in that southeast RHR corner room is remote. The rack-

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containing instruments A through H is located next to a wall with space

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between the instruments and the stairway.

Thera is a wire mesh barrier over

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the top of the rack and on the side of the stairway between the instruments

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with a door for access to the racks.

The other rack is 90 degrees around the

corner, also against the wall, and it has a wire mesh barrier above it.

Personnel must pass in front of rack s1ction A and B before getting to section

C.

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During the exit, the licensee committed to monitor the eight main steam flow

sensing lines with pressure transducers whose output will be recorded to

determine if there are any_ process fluid disturbances.

The four DPIS' input

contacts to each of the four sub-channel trip logic relays will also be

monitored and recorded to pinpoint which set is actuating.

This monitoring is

intended to help identify the source of the signal that caused the MSIV

isolation on February 7,1992.

The monitoring equipment was in place prior to

start up from this event.

The licensee also proposed a long term modification to the main steam line

high flow detection system.

The digital Barton DPIS instruments will be

replaced with an analog system. Unlike the present DPISs, the functional

check of this new equipment would be made from an area not subject to

radiation.

This modification is projected to be more reliable as well as

reduce exposure to personnel.

3.2

Equipment Failures or Malfunctions

3.2.1

Failure of HPCI StoD Valve

During quarterly HPCI pump tests the HPCI steam stop valve successfully

operated a number of times from April 1991, until February 6, 1992, when the

valve failed to close during post modification testing of the remote HPCI

turbine trip pushbutton.

Unsuccessful attempts were made to close the valve;

however, the valve was eventually closed by applying an external force.

The HPCI turbine steam stop valve is a poppet type, hydraulically positioned

shut-off valve designed to close quickly on the following trip signals: HPCI

-turbine overspeed, high reactor water level, low HPCI booster pump suction

pressure, high HPCI turbine exhaust pressure, remote HPCI turbine trip

pushbutton, and local manual trip lever.

Following the failure and to allow for further troubleshooting, maintenance

personnel attempted to disconnect the actuator from the poppet stem.

The

valve bonnet was then removed to facilitate inspection of the poppet. The

outside of the poppet and the inside of the poppet guide, which was welded to

the bonnet, were severely galled.

This interference prevented the valve from-

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stroking.

The AIT determined that the root cause of the valve failure was an inadequate

maintenance work package that was completed in February 1991. The work

package was inadequate, because it did not include as-found or as-left

readings of the clearances between the poppet guide and valve poppet after

welding was performed on the poppet guide assembly.

The welding caused the

guide to become oval shaped and to lose perpendicular 1ty with the bonnet,

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which allowed the poppet to come into contact with the guide after the valve

was reassembled and resulted in fretting of both metal surfaces when the valve

was operated. The valve stuck open during the HPCI test that was conducted on

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February 6, 1992.

The licensee repaired the Unit 1 poppet assembly in accordance with vendor

recommendations using the poppet guide and valve bonnet from the Unit 2 HPCI

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valve.

During inspection of the Unit 2 stop valve, indications of contact

between poppet and poppet guide were noted.

Measurements indicated that.the

poppet guide was perpendicular to the bonnet but the guide was slightly out of

round.

In 1988, cracks were also repaired on the poppet guide to bonnet weld

similar to the weld repair on the Unit 1 valve.

The work package had instruc-

ted maintenance personnel to take as-found measurements on the poppet guide's

position in_ relation to the bonnet.

However, there were no instructions to

measure the concentricity of the guide.

The licensee planned to replace or

repair the Unit 1 poppet guide and install it in the Unit 2 HPCI stop valva.

3.2.2

Failure of "C" Electromatic Relief Valve

During cool down from the Unit I reactor scram on February 7, 1992, pressure

control was accomplished by manually initiating the RCIC system and opening

the ERVs, as needed, to avoid reaching the automatic pressure relief set

points.

As pressure rose initially, ERV "B" was opened and, after pressure

dropped to an acceptable level, the valve was closed. After a short period,

as pressure began to rise again, the control switch for ERV "C" was placed in

,

the open position; however, the valve did not respond.

The "B" valve was then

opened a second time to control the pressure.

The ERV is a six inch solenoid actuated pressure relief valve, which may be

operated, when desired, by closing a switch that allows 125 volts DC to

actuate the operating solenoid. Automatic pressure relief is accomplished by

using a pressure sensing element to control the solenoid.

A cut out switch

(contact shorting bar) is built into the solenoid assembly to increase coil

resistance in order to reduce the solenoid current when the solenoid is

actuated and in the holding position.

The Unit 1 plant has fivc pressure

relief valves that are used to prevent over pressurization of the main steam

system.

The "A" relief valve is a dual purpose valve manufactured by Target

Rock and the other four valves, "B", "C",

"D" and "E", are ERVs manufactured

by Dresser Industries.

During troubleshooting,- two unsuccessful attempts were made to actuate the

valve from the control room. -After-the cover for the solenoid was removed,

.the valve opened on the first attempt.

On subsequent attempts the valve

appeared to open and close normally. The cover and-internal components were

carefully examined along with the plunger and other moving parts of the

solenoid; the results were inconclusive.

Electrical connections were tight

and electrical measurements indicated that the valve solenoid coil was normal.

The resistance reading across the cut out switch terminals was 182 ohms, which

was very high compared to the- normal resistance-of less than 1 ohm.

The

licensee concluded that the high resistance across the cut out switch contacts

caused the failure of the solenoid valve on ERV "C" to operate on demand.

An inspection of the "C" cut out switch, indicated a tarnish build up on the

contact points.

An analysis of the material indicated that the tarnish most

likely was caused by the loose dust found in tha enclosure which vaporized

during contact arcing.

The origin of the dust appeared to be wear from moving

brass parts located inside the actuator.

After cleaning, the moving parts of

the four Unit 1 ERVs were lubricated with a graphite based lubricant to reduce

friction and wear.

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The' AIT agreed with the-licensee that the failure of the "C" ERV was

attributed to brass dust on the contact shorting bar; however,- the team also

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concluded that deficient preventive maintenance (PM) for the ERVs existed.

Maintenance history indicated that Unit 1 ERVs had failed to open 12 times

since 1975.: Four of these failures, including the most recent, were

attributed-to problems with the_ cut out switch; however, _it was difficult to

determine if the failure mechanism was the same as-the February 7, 1992

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failure. One of the failures _ indicated a high electrical resistance across

the cut out switch contacts but none of the previous failures indicated

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tarnish or other buil_d up on the switch contact surfaces.

Although electrical

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PM-tasks were in place as. required by the EQ requirements and vendor

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recommendations, the licensee did not evaluate the possibility of adding PM to

. periodically obtain resistance readings and clean the cet out switch. Also,

Ethe same type of relief valves are used at the licensee's Dresden Station, but

the-licensee had not evaluated Dresden's experience with the valves for

applicability to Quad Cities. Dresden's PM program included obtaining

resistance readings.and lubricating certain brass components in the valve

actuator. -Dresden had not noticed any dust in their valve actuators, nor

failures of the ERVs due to high resistance across the cut out switch.

The ."C" ERV cut out' switch was replaced and the solenoid was cleaned,

reassambled'and tested. _ The valve stroked properly after work was completed.

-The licensee checked resistance readings on the remaining Unit 1 ERVs and all

were_below eight ohms.

The ERVs were-then cleaned and tested.

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resistance _ measurements across the-cut out switches for all four ERVs was less

.than one ohm. All four ERVs stroked properly after the cleaning and tests.

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The team reviewed maintenance history dating back to 1986 for the "A" Target

Rock relief valve.

No significant failure trends or excessive repetitive

failures were noted.

Licensee _ personnel stated that there were no_ existing-mechanical PM tasks in

place for the ERVs;-however, some types of mechanical PM were being performed.

For example, the' ERV pilot valve internals were changed each time a unit

outage occurred in order to prevent inadvertent opening of the ERVs due to

excessive leakage through the pilot valves. A-review of maintenance history

verified the pilot valve replacement.

The environmental qualifications (EQ) for the ERVs' qualified life of 40 years

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-was based-on drywell_ temperatures of 150 degrees.

Information supplied by the

licensee indicated that temperatures as high as 176 degrees had been recorded

in 1991 in the vicinity of_ the ERVs._ Licensee personnel stated that they

. thought that the temperature issue had been previously noted and evaluated,

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however, the previous evaluation could not be located.

Engineering did a

brief analysis of the temperature concern and determined that the equipment

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would.still be qualified for 40 years .at temperatures as high as 187 degrees.

- A copy of this. preliminary analysis was provided to' the NRC inspector.

The

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licensee committed to providing the NRC the final analysis, complete with

appropriate' calculations, within ten days of the exit.

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3.2.3

Failure of the Reactor Feed Pumos to Automatically Trio _at the

Aonropriate Vessel level

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The Unit 1 NSO tripped the "A" RFP after the "A" Yarway reactor water level

indication exceeded +50 inches since the feed pumps were expected to trip at

+48 inches. Once the "A" RFP was tripped, the "C" reactor feed pump

automatically started because it was in the STANDBY position. The Unit 1 NSO

then immediately secured the "C" RFP.

The Unit 1 NSO stated that he

remembered seeing the Unit 2 NSO place the "C" standby feed pump selector

switch in the OFF position but did not check the switch before securing the

"A"

RFP.

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The RFPs are motor driven centrifugal pumps that supply water to the reactor

vessel. The "A" and "B" RFPs were in service with the "C" RFP in STANDBY when

the Unit I reactor tripped.

Forty-three seconds after the scram, the Unit 2

NS0 re.noved the "B" RFP from service per procedure Q0P 3200-5, " Reactor Feed

Pump Shutdown. " .The procedure required the "C" standby reactor feed pump

selector: switch be placed in the 0FF position when removing a feed pump from

service to-prevent an inadvertent start of the standby pump.

The switch was

then placed back in STANDBY after the "B" pump was stopped since the "A" feed

pump was still in service.

The "B" Yarway reactor water level instrumentation

indicated +48 inches, which was the setpoint for the main turbine and RFP

automatic trip.

As level continued to increase, the setpoint (+48 inches) for the "A" RFP trip

was passed, but the "A" pump did not trip.

This did not result in a safety

concern because the operator tripped the pump at >50 inches.

It was

subsequently determined that the setpoint for the "A" RFP had drifted and the

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"A" RFP would have tripped at +53.5 inches.

The main turbine vendor

recommended that the trip level be set at +60 inches to prevent turbine damage

due to carryover of water associated with high reactor vessel water level in a

transient.

There is no credit taken for safety in the FSAR nor any setpoint

or surveillance in the Technical Specification for these Yarway level

indication transmitter switches. However, the drifting indicates that more

frequent calibrations should be performed to- ensure that the RFPs trip at the

expected -l evel . To assure the accuracy of the RFP trip setpoint, the licensee

committed to calibrating these instruments on a quarterly basis instead of-the

current refueling cycle basis.

-The licensee performed an as-found calibration check of the "A" and "B" Yarway

level indication transmitter switches (LITS 59 A&B) that should have initiated

the +48 inch trip signal.

Both LITS signals are ' required to trip the RFPs.

The "A" LITS trip setpoint was +53.5 inches. The "B" LITS setpoint was +48

inches. The operators stated that the reactor water level observed on the

Yarway indicators never exceeded +52 inches.

If the operator had not stopped

the "A" RFP at >50 inches, the.RFPs would have automatically tripped when the

reactor vessel water level reached +53.5 inches, which is 5.5 inches above the-

design trip point. -The "A" LITS was recalibrated to +48 inches and a

functional test was satisfactorily performed on the trip circuit.

The Yarway LITS instruments have had a history of drifting as evidenced by the

calibration and maintenance records for these instruments from October 9,

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1989, through February _8, 1992. Calibration history of the "A"

Yarway LITS

showed that the instrument had drifted both low and high three out of four of

the last calibrations (including the post-scram calibration).

The "B" Yarway

LITS had drifted low twice before being replaced in November 1989.

3.2.4

Anomalies Associated with the Main Steam Line Flow instruments

During this event, when the MSIVs were closed, the operator reported some

indication of main steam line flow on the control room board indicators 1-640-

23A, B, C, D.

(These instruments are for indication only and are different

from the transmitters that provide the reactor protaction shutdown.)

Flow of

0.5 million pounds per hour (MPH) was observed on the "A" flow indicator (FI)

and the "B" FI indication was observed to be bouncing up and down.

These

erratic flow changes were also seen on the total steam flow recorder after the

trip. .The recorder displayed spikes ranging from 0.0 MPH to 2.5 MPH.

The "B",

"C" and "D" main steam line ficcr indkators in the control room had

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"Off Normal Instrument" or 0NI stickers on the-front of the indicator meaning

that maintenance was needed to repair previous problems noted with flow

indications. Although there was no indication of high temperature or high

-radiation in the main steam line area, these control room indications provided

questionable data to the operator during this event.

These erroneous flow

readings resulted in personnel being sent into the plant to investigate

potential steam leaks that didn't exist.

The AIT reviewed the open maintenance work requests corresponding to the ONI

stickers for these flow instruments.

The "B" flow indicator had two open work

requests and the "C" and "D" each had one. These work requests were in

various stages of completion and dealt with measured flow when no flow existed

on "B", "C" and "D"_, and erratic flow indication on the "B" indicator. One of

the work requests required work to be done on the Foxboro square root

converters that supplied input to the four main steam high flow indicators and

total steam flow for the recorder used during this event.

These same problems

were observed by operators during the event on February 7, 1992.

Unit 2 also

had- an ONI on the "C" main steam-flow indicator- with-similar problems 'as found

on the Unit 1 indicators. See section 3.2.4.1 for further discussion of the

licensee's ONI program.

The licensee performed troubleshooting on the instruments and determined that

the Foxboro square root converters needed to be replaced on all instruments,

and the- flow transmitter and power supply needed to be replaced on the "B"

-instrument. -These square root converters provided a signal for indication

only and not for the MSIV Group 1 isolation circuitry.

Because these square

root converters were no longer available from the manufacturer, converters

from Unit 2 (in a refueling outage) were used.

The licensee stated that an

alternate converter or a new design would be examined for the Unit 2

instruments.

-The team reviewed the maintenance and calibration history for the flow

indicato~rs and determined that outstanding work requests existed for these

problems and were the reason for the ONI tags.

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Off Normal Instruments

The A'I determined that the licensee needed to ensure timely corrective action

Lof ON1: to ensure that instruments needing repair do not divert the operator's

attention or impac.* the operator's response to plant transients.

The instruments and equipment in the control room that are operating off-

normal are tracked on the ONI list and governed by procedure QAP 300 34, "Off-

Normal Instruments and Equipment," Revision 4.

The licensee currently logs ON!s manually and on a computer list.

When all of

the data is on the computer the official log for ONis will be a Total Job

Management (TJM) report to be kept in the control room. QAP 300-34 required

that operations categorize these items into Category I or 11 depending upon

importance and route for assignment of work request and resolution.

QAP 300-34 stated that on a monthly basis the SCRE shall notify an Operating

Engineer on ONI items that have been active longer than two weeks in order to

ensure timely repairs on instruments that can be repaired. A copy of an audit

report-dated December 21, 1991, indicated that there were 110 ONis meeting

-this criteria.

At the time of the reactor scram, there were 84 ONI items. Of

the 84 open ONIs, none were Regulatory Guide 1.97 instrumentation, three were

safety-related, and_five could be used as Emergency Operating Procedure (E0P)

equipment. The team determined that,'in all cases, adequate and redundant

means were available to provide the necessary input.

The AIT reviewed all of the control room ONIs and concluded that no safety

significant problems existed. However, several 0NIs have been outstanding for

a long time.

One-safety related ONI corresponded to a work request written in

April 1988. Another safety-related ONI, initiated in October 1991, for a

closed indication light for Recirculation Pump A suction valve, was repaired

in February 1992, by tightening a loose wire for the bulb.

Overall, the AIT considered the ONI process to be weak. The resident

inspectors have been following this issue for several months and the licensee-

was slowly working off the backlog of open items; however, greater emphasis is

needed to ensure that ONIs are addressed and resolved in a timely manner.

The

licensee stated at the exit meeting that work had been completed on an

additional 25 to 30 ONIs on Unit 1 since February 7,1992.

3.2.5

Qt.her Less S'anificant Eouipment Failurgt

The team interviewed operators and reviewed the active out-of-service list and

_the ONI list and determined that there was no indication of other significant

equipment problems with safety related or balance of plant equipment that

could have interfered with the ability of the operators to safely operate the

pl ant. A review of the sequence of events computer data showed that the "B"

' ERV was-cycling open and closed; however, other data in the control room

adequately showed that the "B" ERV did not cycle but operated correctly.

This

problem was traced to a loosely mounted acoustic monitor that resulted in

false ERV position input for the sequence of events data recorder. All other

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. acoustic monitors were found securely attached.

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4.0

Conclusions

After completing the AIT Charter, the team was able to make the following

conclusions:

1.

The root cause could not t e determined for the main steam high flow trip

signal, which caused the Group I isolation that ultimately led to the

reactor scram.

The licensee had performed reasonable analyses and

testing to determine r'ot cause.

Additional monitoring equipment to

monitor for-abnormalit..s within the main steam high flow trip system

was installed prior to Unit I start-up.

2.

The failure of the HPCI stop valve was attributed to an inadequate

maintenance work package, which was performed in february 1991. The

work package was considered inadequate because it did not include as-

found or as-left readings of the clearances between the poppet guide and

valve poppet. After welding was performed on the poppet guide assembly,

incorrect tolerances caused the valve to eventually become stuck in the

open position during HPCI testing conducted on February 6, 1992.

3.

The failure of the "C" Electromatic Relief Valve (ERV) was attributed to

brass dust on the shorting contact bar, which was caused by main steam

-system vibration.

The licensee determined that the dust originated from

brass components near the contact shorting bar.

In addition, the AIT

concluded that deficient preventive maintenance for the ERVs existed.

Although previous ERV failures indicated high resistance readings across

the contact-shorting bar, the licensee did not evaluate the possibility

of adding preventive maintenance to periodically obtain resistance

readings and clean the shorting bar.

Also, the licensee did not pursue

obtaining experience from other CECO nuclear plants that have the same

type of relief valves.

Preventive maintenance practices may have

precluded the failure of the

"C" relief valve.

4.

The apparent failure-of the Reactor feed Pumps to automatically trip at

the appropriate vessel level was attributed to instrument drift.

Because the trip setpoint for one of tne two level indicating switches

had drifted from +48 inches to +53.5 inches, neither of the RFPs would

have tripped automatically at the expected trip point. Operator actions

manually tripped the RFPs before reaching the respective trip settings;

'however, if manual actions had not been taken the pumps would have

automatically tripped at +53.5 inches.

5.

Anomalies associated with the "B", "C", and "0" main steam line flow

indicators, were attributed to a faulty power supply and square root

converters.

The control room flow indicators had "Off Normal

Instruments"_ or ONI stickers on-the front, which meant that maintenance

was needed to repair previously identified problems of false flow

indications. These erroneous flow indications occurred again after the

MSIVs:were closed during this event and resulted in personnel being sent

into the plant to look for steam leaks that didn't exist. The AIT was

concerned the operator's attention was diverted besause of indicators

that needed repair.

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6.

Operators performed well in mitigating the consequences of the reactor

scram and Group I isolation.

7.

The licensee's recovery from this event was thorough.

Corrective

actions to address each of the equipment failures or anomalics were

considered adequate and corrective actions to prevent recurrence were

reasonable and complete.

5.0

Exit Interview

The team met with licensee representatives (denoted in attachment 3) in a

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public exit meeting on February 13, 1992, and summarized the purpose, AIT

charter items, and findings of the inspection.

The team discussed the likely

informational content of the inspection report with regard to documents or

processes reviewed by the team during the inspection.

The licensee did not

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identify any such documents or processes as proprietary.

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