ML20085C925

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AO 50-265/74-25:on 740916,ultrasonic Tests Indicated Crack at Weld 02BB-F10 on 4 Inch Pipe to Weldolet of Recirculation Sys Loop 2B Discharge Valve Bypass Line.Cause Unestablished.Plans Initiated to Repair Failed Weld
ML20085C925
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 09/26/1974
From: Kalivianakis N
COMMONWEALTH EDISON CO.
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20085C928 List:
References
AO-50-265-74-25, AO-50-265174-25, NJK-74-299, NUDOCS 8307130229
Download: ML20085C925 (4)


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September 26, 1974 Mr. John F . O ' Leary , Director Directorate of Licensing Regulation U. S. Atomic Energy Commission Washington, D. C. 20545 Reference : Quad-Cities Nuclear Power Station Docket No. 50-265, DPR-30 Appendix A, Sections 1.0.A.5 and 6.6.B.l.a DRO Bulletin Number 74-10

Dear Mr. O' Leary:

L Enclosed please find Abnormal Occurrence Report No. A0 50-265/

74-25 for Quad-Cities Nuclear Power Station. This occurrence was previously reported to Region III, Directorate of Regulatory Operations by telephone on September 16, 1974 and to you and Region III, Directorate of Regulatory Operations by telecopy F on September 17, 1974. .

This report is submitted to you in accordance with the requiro-ments of Technical Specification 6.6.B.1.a., and is also submitted in compliance with the action requested in item 4 of the refer-enced DRO bulletin.

Very truly yours, COMMONWEALTH EDISON COMPANY QUAD-CITIES NUCLEAR POWER STATION S

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N. J. Kalivianakis -^/

Station Superintendent NJK/ REQ /1k

'cc: Region III, Directorate of Regulatory Operations 'f6 ~

J. S. Abel p,cus'/-  !

DRO, Assistant Director for Constructicn and Operations J 8307130

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O HEPORT NUMBER: A0 50-265/74-25 .

8 REPORT DATE: Septembe r 26, 1974 OCCURRENCE DATE: Septembe r 16, 1974 FACILITY: Quad-Cities Nuclear Power Station Cordova, Illinois 61242 IDENTIFICATION OF OCCURRENCE:

Crack at weld 02BB-F10; 4 inch pipe to weldolet weld of Reactor Recirculation System Loop 2B discharge valve bypass line.

CONDITIONS PRIOR TO OCCURRENCE:

Unit 2 Reactor in cold shutdown condition.

L DESCRIPTION OF OCCURRENCE:

On September 15, 1974 the station was advised of a problem discovered at Dresden Nuclear Power Station that involved the failure of welds on the Reactor Recire Pump Discharge Vulve By- _

pass line. Since Quad-Cities Unit 2 was shutdown at the time for a maintenance outage, plans were made to inspect the similar piping on that unit. Longitudinal and shear wave ultrasonic j

nondestructive tests were performed on both loops of the Unit 2

Reactor Recirculation System Discharge Valve Bypass lines. A P

total of 22 welas were inspected. On September 16, 1974 the tests indicated a nonvisable anomaly at weld number 02BB-F10 on the 'B' loop discharge bypass line. A subsequent radiograph

( on September 16, 1974 confirmed the anomaly as a 3 inch long subsurface crack at the top of the 4 inch bypass line approxi-mately 1/4 inch away from the pipe to ucidolet weld. Each end of the crack terminated at the weld. The weldolet is located -

on the upstream side of the 2B recirc pump discharge valve (MO-2-0202-58) at the point where the bypass line -(2-0203B-4") joins the recirc pump discharge line (2-0201B-28"). Unit 2 remained shutdown and plans were made to repair the defective .* eld.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The mode of failure and thus the cause of this occurrence had not been established as of the date of this reoort. The failure is being studied by representatives of the Ceco OAD 1

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j department, the General Electric Company., and Argonne National Laboratory to determine the failure mechanism. Further infor-mation will be provided when the studies are concluded and the failure mode is determined. ,

ANALYSIS OF OCCURRENCE:

Since the crack was detected before it had completely pene-trated through the pipe, there was no leakage or damage to other systems associated with this occurrence. The repairs made to the 4 line restored it to its original configuration since the repair i specifications and materials were the same as the original in-stallation. There were no changes to the system as previously designed and analyzed, and the repairs performed restored the level of integrity as required by the Technical Specifications.

Therefore, no unreviewed safety questions are created because y of this occurrence or the repairs made. Additionally, there were no effects on the health and safety of the public associated with this occurrence. , 1 i

l Considering that the system as originally installed did fail, "j j

and that the mode of failure is presently unknown, it.is recog-nized that the possibility of this type of failure reoccurring does exist. However, it is felt that the normal drywell leakage and atmospheric monitoring systems are adequate to give warning i

of this type of failure in the future. Since the failure was j not catastrophic and would probably not be such if it occurred

again, any leakage as a result of a similar failure would be i detected and the appropriate plant actions per the Technical
Specifications would take place. As a final consideration, a ^

gross failure of this line would be within the capabilities of I the ECCS systems. Thus, the safe operation of the reactor was not threatened by this occurrence and is not compromised by the

repairs made.

CCRRECTIVE ACTION:

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Plans were developed to repair the failed weld immediately 4

since the point of failure was in a location that was able to i be isolated with the normal valves associated. with the 'B' loop

! recire pump. The repairs consisted of removing approximately a 9 1/2 inch long piece including the failed portion and replacing 11t with a new piece. The repair procedures and required Quality l Control Records are documented with Safety Related Work Request

! Number 3711-74. Following completion of the repairs, dye pene- ,

trant tests were performed, radiographs were made, and ultrasonic

_ tests were performed. The completed repairs and ~ tests were a

approved by the ASME ' Authorized Inspector representing 'the Hart- '

ford Steam Boiler Company. The repairs were successfully completed and the unit was returned to power operation on September 25, 1974 j G

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  • * ~ Prior to startup of the unit, strain gauges and accelerometers were installed on the repaired bypass line in order to remotely monitor the line vibration characteristics during operation.

The resultant data will be analyzed by the Southwest Rese arch Institute to help evaluate the occurrence and determine the cause.

As an additional precautionary measure, all other 4" and less diameter pipes connected to the recirc discharge piping were visually inspected for any signs of leakage. No signs of failures were noted during this inspection.

FAILURE DATA:

The initial phone conversations with the Region III repre-sentatives had reported that a discontinuity had been found in this weld during the baseline piping inspection of this system.

A closer review of our records has shown that this was not the case and that there were no discontinuities associated with this weld at the time of the baseline inspection. There have been no other similar failures related to the recirc system piping thus, there is no failure data associated with this occurrence.

Also, since there is no failure data, there are no safety in-plications related to cummulative experience associated with aa this occurrence.

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