ML20084U756

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AO 50-265/75-1:on 741230,HPCI Steam Exhaust Check Valve Leak Rate Exceeded Tech Spec Limit.Caused by Leakage Between Valve Body Seat Ring & Disc.Valve Seats Remachined
ML20084U756
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/26/1975
From:
COMMONWEALTH EDISON CO.
To:
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084U751 List:
References
AO-50-265-75-1, NUDOCS 8306290223
Download: ML20084U756 (2)


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+ Q O REPORT NUMBER: A0-50-265/75-1 REPORT DATE: 2-26-75 OCCURRENCE DATE: 12-30-74 FACILITY: Quad-Cities Nuclear Power Station Cordova, Illinois 61242 IDENTIFICATION OF OCCURRENCE:

Excessive Icakage through the high pressure coolant injection system (liPCI) steam exhaust check valve, 2-2301-45.

CONDITIONS PRIOR TO OCCURRENCE:

The Unit two reactor was in the cold shutdown condition for the current refueling

, outage. The HPCI system was out-of-service with flPCI turbine exhaust manual valve, 2-2301-74, closed.

DESCRIPTION OF OCCURRENCE:

j While performing local Icak rate tests on primary isolation valves it was determined '

that the llPCI steam exhaust check valve had a leak rate of 62.2 SCFH which is in excess of the 18.36 SCFH limit allowed by Technical Specification 4.7.A.2.1 (2)(b).

The leak rate test was performed by pressurizing the pipe volume between the valves 2-2301-45 & 74 to 48 psig through a 3/4-inch pressure test point.

A work request was issued and repairs were initiated.

1 DESICNATION OF ApPARCNT CAUSE OF OCCI'RRENCE:

Equipment Failure - the apparent cause of the excessive leakage through the check valve was leakage between the valve body seat ring and the disc.

ANALYSIS OF OCCURRENCE:

When operating under accident conditions the HPCI exhaust passes through check valve 2-2301-45 and manual valve 2-2301-74 and into the suppression chamber, i n the event of a high suppression chamber pressure, manual valve 2-2301-74 could be closed to prevent back flow through the check valve to the HPCI turbine. -

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The backward leakage through check valve 2-2301-45 does not render the itPCI system inoperable, therefore, safe plant operatior, was not jeopardized. Since the HPCI room is not normally manned and is enclosed by secondary containment, no abnormal radiation exposures would be experienced by plant personnel and the public health l and safety would not be affected. -

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8306290223 750103 PDR ADOCK 05000265 PDR O .

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D-4-2-75-1 February 26, 1975 1

O O CORRECTIVE ACTION:

The Maintenance Department disassembled the check valve and remachined the valve seats. On January 30, 1975, following the repair and replacement of the check valve, a local leak rate test was conducted and resulted in a measured leakage rate of 0.4 SCFH. This value is within the Technical Specification limit.

FAILURE DATA:

t Check valve 2-2301-45 was not tested for leakage at any tine between pre-operational testing and the current refueling outage. Therefore no previous Icakage data exist

for this valve.

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