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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20217G7821997-07-22022 July 1997 Special Rept:On 970227,ECCS Sys Was Actuated & Injected Water in Rcs.Declared HPCI Subsystem Operable Following Restoration of Subsystem to Normal Standby Lineup ML20097D4661992-05-27027 May 1992 Special Rept,Reflecting Quad-Cities Nuclear Power Station, Unit 2 Summary Status of Fuel Performance at End of Cycle 11. No Sipping Performed on Reload Fuel Assemblies at End of Cycle 11 ML20066J6331991-01-31031 January 1991 Forwards Summary Status of Fuel Performance for End of Cycle 11 ML20207P1881987-01-0606 January 1987 Special Rept:Summarizes Status of Fuel Performance as of End of Cycle 8.Of 2031 Assemblies used,289 Determined to Have Failed & Discharged as Leaker Assemblies.Aug 1986 Sipping Tests Showed No Indication of Assembly Failure ML20082P6541983-12-0505 December 1983 Telecopy RO 50-83/20-01T:on 831202,review of Ultrasonic Test Data Obtained During Current Refuel Outage Revealed Circumferential Linear Indication in Heat Affected Zone of Weld 02B-S9.Further Info Expected within 14 Days ML20078J8531983-10-12012 October 1983 Telecopy Ro:On 831011,during Performance of Ultrasonic Insp of Cleanup Sys Piping,Crack Indication Discovered in Heat Affected Zone of Weld 12S-S27 of Line 2-1202-6A.Further Info to Be Provided within 14 Days ML20084S1401977-05-13013 May 1977 Ro:On 770512,unit Experienced Sudden Turbine Control Valve Opening Resulting in Feedwater Flow Increase & Reactor Scram from APRM flux.Short-term Reactivity Increase Corresponding to Reactor Period of Less than 5s Experienced ML20084S1531977-05-0909 May 1977 Ro:On 770507,station Experienced Momentary Short Period of Less than 5s During Shutdown Margin Demonstration.Similar Experience Occurred on 770504.Addl Info Will Be Submitted in RO 50-254/77-23 ML20084S1901977-02-17017 February 1977 Telecopy Ro:On 770217,info Received by Station Indicated That MAPLHGR Limit Curves Given by Tech Specs Shall Be Additionally Lowered.Reduction Resulted from Review of ECCS Analysis.Maplhgr Curves Lowered Effective 770217 ML20084S2041977-01-18018 January 1977 Telecopy Ro:On 770118,info Received by Station Indicated That MAPLHGR Limit Curves Shall Be Lowered.Reduction Resulted from Review of ECCS Analysis.Curves Lowered ML20084S3501977-01-0404 January 1977 RO-50-254/76-37:on 761205,limit for Having No More than 2 Ci Activity in Radwaste Tank Farm in 24h Exceeded. Caused by Deterioration of Effectiveness of Radwaste Sys to Perform as Designed.Radwaste Sys Being Updated ML20084S3551976-12-30030 December 1976 RO 50-254/76-36:on 761202,cooling Water Suction Header Common to Both RHR Containment Cooling Loop 1A & Diesel Generator 1 Cooling Water Pump Airlocked.Caused by Procedure Inadequacy.Maint Procedures Will Be Revised ML20084S2861976-12-28028 December 1976 RO 50-254/76-38:on 761215,GE Notified Util That NRC Discovered Errors in Code Inputs to ECCS App K Analysis, Caused by GE Incorrectly Applying Data for ECCS App K Analysis.Maplhgr Curves Reduced by 4% ML20084S3391976-12-16016 December 1976 Ro:On 761215,preliminary Info Received by Station Indicated That MAPLHGR Curves Should Be Lowered by 4%.Change Resulted from Review of ECCS Analysis.Curves Lowered ML20084S3611976-12-16016 December 1976 RO 50-254/76-35:on 761203,discovered Discrepancy Between Tech Spec & Nedo 20360 Rod Worth Minimizer Operable Rated Power.Orders Written in Daily Order Book Requiring Rod Worth Minimizer Operability Below 20% ML20084S3701976-12-0303 December 1976 Ro:On 761203,info Received Indicated That Rod Worth Minimizer (RWM) Operability Requirements Should Be Changed from 10% to Below 20% Rated Power.Caused by Review of Rod Drop Accident Analysis ML20084S3791976-11-22022 November 1976 Updated RO 50-254/76-33:on 761029,repairs to RCIC Pump Consisted of Rebuilding Pump Casing & Installing New Rotary Element.Pump Reassembled & Repairs Completed by 761111.Welds on Piping Acceptable ML20084S3771976-11-12012 November 1976 RO 50-254.76-34-on 761104,electromatic Relief Valves 1-203-3C & 1-203-3E Failed to Open When Actuated from Control Room.Caused by Excessive Steam Leakage Into Area Below Valve Disc.Investigation in Progress W/Manufacturer ML20084S3941976-11-10010 November 1976 RO 50-254/76-33:on 761029,while Performing RCIC Sys Pump Operability Surveillance,Discovered That Pump Could Not Achieve Flow & Pressure Required.Caused by Two of Five Stages Being Severely Damaged.Pump Being Rebuilt ML20084S5421976-10-30030 October 1976 Updated RO 50-254/76-26:on 760803,rod Worth Minimizer Not Operable for Withdrawal of First Twelve Control Rods to Fully Withdrawn Position While in Startup Mode.Caused by Burned Out Wire Runs on Relay Board.Software Modified ML20084S4031976-10-13013 October 1976 RO 50-254/76-32:on 761001,main Chimney Monitoring Sys & Reactor Bldg Vent Sample Sys Not Functioning Properly.On 760919,flexible Sample Hose Wrapped W/Tape to Stop Possible Leak.Caused by Failure of Flexible Suction Hose ML20084S5641976-10-0404 October 1976 Supplemental RO 50-254/76-25:electrical Nitrogen Vaporizers Installed on Nitrogen Makeup Sys.Installation Should Prevent Future Recurrences ML20084S4761976-10-0404 October 1976 RO 50-254/76-31:on 760920,station Informed by GE of Error in Reload 2 Licensing Submittal in Determining Max Change in Critical Power Ratio Due to Abnormal Operating Transient. Caused by Incorrect Analysis in Preparing Submittal ML20084S4831976-09-21021 September 1976 RO Re Notification by GE of Oversight in Reload 2 Licensing Submittal Leading to Possible Nonconservative Operation During Cycle 3.Work Request to Lower Rod Block Monitor Line to 10% at Full Flow Initiated ML20084S5031976-09-0909 September 1976 RO 50-254/76-29:on 760809,surveillance of Primary Containment Oxygen Concentration Revealed Increase in Concentration from 4.2 to 4.8%.Caused by Instrument Drift. Oxygen Analyzer Recalibr ML20084S5151976-09-0707 September 1976 RO 50-254/76-28:on 760809,position Indication Lost on Reactor Water Cleanup Sys Isolation Valve Mo 1-1201-2.Caused by Relay 595-125 Shorting Out & Burning Up Control Transformer.Relay & Transformer Replaced ML20084S5781976-08-26026 August 1976 RO 50-254/76-24:on 760727,reactor Bldg to Suppression Chamber Vacuum Breaker Pressure Switch PS-1-1622B Tripped at 0.536 Psid.Caused by Instrument Setpoint Drift.Switch Recalibr ML20084S5241976-08-19019 August 1976 RO 50-254/76-27:on 760806,ECCS Analysis Performed by GE for BWR-3 Type Plant Resulted in Calculated Peak Clad Temp Greater than 2,200 F for Reduced Core Flows.Caused by Severity of Conservatisms Associated W/Using App K ML20084S5511976-08-16016 August 1976 RO 50-254/76-26:on 760803,rod Worth Minimizer Multiple Output Distributor Error Detected.Caused by Burned Out Wire Runs on Relay Board.Board Repaired & Hardware & Software Mods & Procedural Changes Being Considered ML20084P7411976-06-23023 June 1976 Telecopy Ro:Initial Swipe Survey of Nuclear Fuel Svcs NFS-4 Cask Indicated Three of 38 Tests Exceeded Limits ML20084P7551976-06-17017 June 1976 Telecopy Ro:On 760617,HPCI Sys Motor Speed Changer Failed to Come Off Low Speed Stop During Monthly Surveillance.Caused by Motor Speed Changer Linkage Being Bound.Linkage Freed ML20084S4131976-03-30030 March 1976 Telecopy Ro:On 760330,suppression Chamber Water Level Instrumentation Found Miscalibrated.Suppression Chamber Water Level Immediately Returned to Normal.Addl Info Will Be Submitted in RO 50-265/76-04 within 14 Days ML20084Q1751976-03-26026 March 1976 Telecopy Ro:On 760326,chemical Waste Sample Tank Discharged to River at Rate in Excess of Limits ML20084S4151976-01-0909 January 1976 Telecopy Ro:On 760108,while in Cold Shutdown,Crack Indications Found on a & B Loops in valve-to-pipe Junctions on Sides of Bypass Valve That Cannot Be Isolated & in Heated Zones ML20084S5091976-01-0505 January 1976 RO 50-254/76-1:on 760105,w/unit in Cold Shutdown for Refueling,Pinhole Leak Found in Fillet Weld of 3/4 Inch Drain Line.Caused by Degradation of Reactor Coolant Primary Boundary.Work Request Being Issued ML20084S5311975-12-31031 December 1975 RO 50-265/75-47:on 751231,w/unit Operating at 805 Mwe, Reactor Core Isolation Cooling (RCIC) Trip Throttle Valve Could Not Be Reset Following Successful Monthly Surveillance Functional Testing.Hpci Tested & Found Operable ML20084U2081975-02-25025 February 1975 Ro:On 750212,following Verification of Reactor core,mixed- Oxide Fuel Assembly Identification Number Stamped in Wrong Orientation Discovered.Caused by Mfg Error.Fuel Insp Procedure Changed to Verify Number Orientation as Correct ML20084U2121975-02-20020 February 1975 Ro:On 750212,during Core Spray Operational Hydrostatic Test, Water Observed Overflowing Reactor Bldg Floor Drain Sump 1B.Caused by Premature Actuation of Core Spray Discharge Header Relief Valves.Test Procedure Amended ML20085C9241974-11-15015 November 1974 Ro:On 741011,control Rod Drive N-11 Jammed Fully Inserted Past Position 00 & Would Not Withdraw After Increasing Drive Pressure.Caused by Broken Seals on Stop Piston.Drive N-11 Replaced ML20085C9181974-11-15015 November 1974 Ro:On 741017,during Removal of Faulty Intermediate Range Monitor 18 Detector,Detector Became Stuck in Shuttle Tube. Caused by Coupling Between Shuttle & Drive Tubes Overtightened.New Shuttle Tube Ordered ML20084K5181974-06-26026 June 1974 Telecopy RO Re Setpoint Drift of Standby Liquid Control a Relief Valve.Valve Reset & Tested ML20084K6451974-06-22022 June 1974 AO 50-265/74-12:on 740612,high Differential Pressure Noted Across Combined High Efficiency & Carbon Filters.Caused by Exhausted High Efficiency Prefilter.Original Carbon Filters, New Rough Prefilters & New Efficiency Prefilters Installed ML20084K5461974-06-19019 June 1974 Telecopy Ro:On 740619,water Leak Discovered at Pressure Test Connection & Feedwater Line.Caused by Cracked Weld at Weldolet Line.Repairs in Process ML20084K5541974-06-19019 June 1974 Telecopy Ro:On 740619,water Leak Discovered at Pressure Test Connection & Feedwater Line.Caused by Cracked Weld at Weldolet Line.Repairs in Process ML20084K5891974-06-14014 June 1974 Telecopy Ro:On 740613,level Switch LIS-2-263-72D Failed. Switch Lightly Pressed & Functioned Normally.New Switch Ordered ML20084K5941974-06-14014 June 1974 Telecopy Ro:On 740613,level Switch LIS-2-263-72D Failed. Switch Functioned Normally When Lightly Pressed.New Switch to Be Installed ML20084K6291974-06-13013 June 1974 Telecopy Ro:Level Switch Failed to Actuate Control Room Annunciator.Cause Under Investigation ML20084L0441974-06-10010 June 1974 Telecopy Ro:On 740609,high Water Conductivity Discovered in Reactor.Shutdown & Water Cleanup Initiated ML20084K8401974-06-10010 June 1974 Telecopy Ro:On 740610,feedwater Valve Failed.Caused by Wall Thickness Being Less than Design Min.Cleanup, Decontamination & Water Processing Initiated ML20084K8361974-06-10010 June 1974 Telecopy Ro:On 740610,feedwater Low Flow Valve Failed.Caused by Not Maintaining Min Wall Thickness.Radiation Released Not Above Normal Level.Decontamination,Cleanup & Water Processing Initiated 1997-07-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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N i () ~3 s, -
CoMm'onw2:lth Edison Ouad-Cities Nuclear Power Station b IE FILE COPY Post Office Box 216 , ,. .
Cordova, Ilknois 61242 < , -^ k',/ M Telephone 309/654-2241 NJ K-76-420 A 6 g + 'e Rittat0 November 12, 1976 m2 DEC 71976 d a -
"d " Ess w semes 5
J. Keppler, Regional Director /
Office of Inspection and Enforcement 11 TO\
Region ill U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137
Reference:
Quad-Cities Nuclear Power Station Docket No. 50-254, DPR-29, Unit 1 Appendix A, Sections 3 5.D.3 and 6.6.B.I.e.
Enclosed please find Reportable Occurrence Report No. Ro 50-254/76-34 for Quad-Cities Nuc, lear Power Station. This occurrence was previ.ously reported to Region ill, Of fice of Inspection and Enforcement by' telephone on November l',
1976 and by telecopy on-November 2, 1976.
This report is submitted to you in accordance with the requirements of Technical Specification 6.6.B.I.
Very truly yours, COMMONWEALTH EDIS0N COMPANY QUAD-CITIES NUCLEAR POWER STATION
' /
W N.J. Kallvianakis Station Superintendent
~
NJK/LFG/lk cc: G.A. Abrel1 lb c 2 8306160709 761112 PDR ADOCK 05000 S
NOV 101976
__ ____2
(3
'")
- i. LICENSEE EVENT R RT CONTROL 8 LOCK:l l l l l l l (PLEASE PRINT ALL REQUIRED INFORMATION) 1 6 AME LCENSE NUMBER E TYPE O1 ll lL lQl Al Dl 1l l0l0l-l0l0l0l0l0l_l0l0l l 4l 1 l1l 1l 1l l0l1l l 7 89 14 15 25 26 30 31 32 CATEGCRY TYP E OCCKET NUMBER EVENT DATE REPORT DATE U59 l1 l1 l1 l2 l 7 l 6[
O CONTl l l l Ll l0 l 5 l 0 l-l 0 l 2 l 5l 4l l1 l110 l 1 l 7 l 6l 7 8 57 58 60 61 68 69 74 75 80 EVENT DESCRIPTION gg l During the startup for Unit Two, Cycle Three, the electromatic relief valves were l 7 89 80 SE l tested for operability. Two of the relief valves failed to open. Due to these l 7 89 80 g[ l problems on Unit Two, it was decided to test the Unit One electromatic relief valves. [
7 89 80 3E l At 2:45 pm on November 1, 1976, the Unit One relief valves were tested. The 1-203-3Cl 7 89 80 HG I and 1-203-3E relief valves failed to open when actuated from the control room. it wasl 7 89 pauf 80 E ODE COMPONENT CODE V101ATION 35 l Sl Fl W 7 89 10 11 l V l Al Ll Vl ElXl 12 17 W43 l Dl2 l4 l3 l 44 47
{48 CAUSE DESCRIPTION gg l (Proximate Cause-Equipment Failure) These valves are designed to operate by venting l 7 89 80
@ l the area below the valve disc by opening a pilot valve, and causing a differential J 7 89 80 DE I pressure across th4 valve disc. This results in the valve being forced- (see attached)
S % POWER CTHER STATUS DS VERY DISCOVERY DESCRIPTON 1
7 8 W
9 l0l7l7l l 10 12 13 NA 44 l W45 l Test based on Unit 2 valve failures l 46 80 R LEAS D OF AMOUNT OF ACTIVITY LOCATON OF RELEASE 30 7 8 W
9 dl 10 11 NA 44 l l 45 NA 80 l
PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTON
(( l 0l 0 l 0 l 7 89 11
]12 l
13 NA 80 l
PERSONNEL INJURIES NUMBER DESCRIPTON 3E l 0l 0 l 0 l l NA l 7 89 11 12 80 OFFSITE CONSEQUENCES
@l 7 89 NA 80 l
LOSS OR OAMAGE TO FAClUTY TYPE DESCRIPTON .
32 U 7 89 l
10 NA 80 l
PUBLICITY DE l NA l 7 89 80 ADDITIONAL FACTORS gg l (Event Description contd) determined that the pilot valves were functioning as l 7 89 80 i DE l evidenced by a temperature rise down stream of the pilot valve. However, (cont) l 7 89 80 NAME: James Schrock PHONE:
GPO 801
(3 V (v)
CAUSE DESCRIPTION contd open by reactor steam pressure. There is an orifice through the disc retainer that allows the area below the valve disc to re pressurize and close the valve when the pilot valve is closed. The apparent cause of the valve failures was that there was excessive steam leakage into the area below the valve disc, in addition to the normal steam flow to this area through the orfice. As a result of this additional steam flow, the pilot valve could not adequately vent the area below the valve disc to allow the valve to open.
There are two possible leakage paths that could have resulted in the valve failures. The steam could have leaked between the valve disc guide and the piston rings on the valve disc or there could be leakage past the threads on the disc retainer.
ADDITIONAL FACTORS EVENT DESCRIPTION contd as described below, there was no noticeable steam flow from the reactor through the valve discharge piping.
The presence of steam flow was checked by first lowering the setpoint on the turbine Load Set, in order to open a main steam bypass valve. Each relief valve =was actuated from the control room for a one-second time interval.
Relief valve opening and subsequent steam flow are then verified by means of observing closure of the bypass valve during the time the relief valve is.
open.
This response of the bypass system was satisfactorily verified for relief valves 1-203-3A, 1-203-38, and 1-203-3D.
In accordance with Technical Specification 3.5.D.3, an orderly shutdown was commenced immediately and load was decreased at the rate of 50 MWe per hour.
The unit was in the Cold Shutdown Condition by 8:00am on November 2, 1976.
Work Requests 4094-76 and 4095-76 were issued to determine the source of the problem and perform repairs.
The failure of two electromatic relief valves renders the Auto-blowdown function of the Emergency Core Cooling System inoperable. However, the High Pressure Coolant injection (HPCI) Sub-system was demonstrated to be fully operable, thereby providing a means available for introducing emergency core cooling water into the reactor vessel at operating pressure. Ancther function of the electromatic relief valves is to protect the vessel from over pressurization. This function was provided for by virtue of the three operable relief valves providing a path for blowdown to the suppression chamber. The Target Rock Safety-Relief Valve 1-203-3A was demonstrated to be operable, and would have lifted at a reactor pressure of 1125 psig.
Valves 1-203-3B and 1-203-3D would have opened at reactor pressures of 1130 psig and 1135 psig, respectively. Therefore, there was overpressure protection at all three pressure setpoints specified in Technical Speci-fication 4.6.E. Also, the Electro-hydraulic Control (EHC) system was operable,
enabling the bypass valves to dump steam to the condenser in the event of a turbine trip, thereby controlling reactor pressure. Furthermore, all i nine Main Steam Safety Valves were operable, and were fully capable of preventing the reactor vessel pressure from reaching the Safety Limit of 1325 psig at the vessel steam space. Therefore, the possible consequences of this occurrence were minimized by the redundant design of the safety systems and the fact that all other safety systems were operable. At no time was the public health and safety in Jeopardy, nor was the ability to safely shutdown the reactor compromised. (R0 50-254/76-34)
Corrective Action to Prevent Recurrence When Unit One was shut down and de-inerted, a drywell entry was made. The two elecromatic relief valves that failed were removed, brought to the shop, disassembled, and inspected. The disc retainer lock arm and lock screw was missing from'the 1-203-3E relief valve. It was decided to replace the 1-203-3E valve, serial number 7069, with a spare relief valve, serial number 7062, and finish inspecting the 7069 valve at a later date. The spare relief valve had been overhauled and had new piston rings, valve disc, and pilot valve disc installed. The 1-203-3C relief valve, serial number 7063, was overhauled and the piston rings and valve disc guide were replaced. Both valves were then given a leak test and operability test in the shop and then were replaced on the main steam lines. Startup was then commenced on Unit One on November 6, 1976. The reactor was brought to operating pressure and the 1-203-3C and 1-203-3E relief valves were tested using Temporary Procedure No. 743 This procedure constitutes a revis. ion to the existing procedure for manual operation of the electromatic relief valves, .and calls for verification of a bypass valve closure response as well as temperature, to verify steam flow from a relief valve. This revision will be a permanent procedure, and shall be implemented accordingly. After the electromatic reliefs were replaced on the Unit One steam lines the 7069 relief inspection was completed and the threads on the disc retainer were found to be worn.
Investigations into this problem are being continued between the valve manufacturer and Commonwealth Edison Company to resolve the causes of these valve failures.
Failure Data Unit One Main Steam Relief Valves had not experienced this type of failure in the past. Modification M-4-1-73-45 was installed on the relief valves in May, 1973 This modification installed a valve disc retainer locking device, to prevent the locking plate from falling off. This change had been performed ba::ed on an electromatic relief valve failure at Oyster Creek Station in December, 1972.
The 1-203-3C and 1-203-3E electromatic relief valves are manufactured by Dresser Corporation, serial numbers BK-7063 and BK-7069
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