ML20083R033

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Ro:On 720801,containment Spray Pump 51 C Failed to Start Following Attempt to Recirculate Water in Suppression Chamber.Caused by Loss of Continuity Across Breaker Position Switch.Switch Cleaned
ML20083R033
Person / Time
Site: Oyster Creek
Issue date: 08/11/1972
From: Finfrock I
JERSEY CENTRAL POWER & LIGHT CO.
To: Anthony Giambusso
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20083R030 List:
References
NUDOCS 8303310237
Download: ML20083R033 (2)


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il Jersey Central Power & Light Company t

M ADISON AVENUE Al PUNCH BOWL RO AD e MoRRISTOWN, N.J. o796o e 539-6111 i

i August 11, 1972

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4 Mr. A. Giambusso Deputy Director for Reactor Projects Directorate of Licensing gN 4 fg g 4

4ADneab United States Atomic Energy Commission 7Wr Washington, D. C. 20545

Dear Mr. Giambusso:

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Subject:

Oyster Creek Station

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Docket 50-219 Containment Spray Pump Failure i

The purpose of this letter is to report to you that Containment l

Spray Pump 51 C could not be started from the Control Room on August 1, 1972 when an attempt was made to recirculate water in the Suppression Chamber for the purpose of obtaining a sample for chemical analysis.

s Troubleshooting of the pump supply breaker closing circuit j

was conducted and although the breaker was visually checked to be f

l properly racked in,a loss of continuity was discovered t_o exis h %

l across the breaker position switch,/which is closed when the breaker-is racked in and ready for service. The breaker was racked out, the switch inspected and cleaned, and the breaker was racked back into normal position. Continuity checks indicated the switch to be closed.<

However, when a starting signal was applied, the breaker failed to I-close. The start-stop switch and the keylock switch were operated and observed without potential several times. Control voltage was applied and the breaker closed at this time, the pump started and an operability check was satisfactorily completed.

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The start-stop switch and the keylock switch were inspected

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and found to be in good condition. Resistance checks were made across l

the breaker position switch contact and measured to be.09, ohms. The -

breaker was racked out, the switch contacts' cleaned and burnished, and af ter racking the breaker back in, contact resistance was measured to

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be.0019 ohms. All wiring was checked and no loose leads found.

l There was no safety significance associated with this event since, as stated in the FDSAR, Volume I,Section VI 7-1 and Amendment 32, only one Containment Spray Loop is necessary to remove the energy postulated from the loss of coolant accident. The second Containment Spray Loop in this case, Loop I, would have been capable of performing this function since the primary pump in that loop was started and found.

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Mr. A. Ciambusso Page II August 11, 1972

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.In. addition, the Control Room Operator could have started the backup' pump in Loop II'during the postulated accident. Operability of that pump.was. checked wh.en it was run to permit taking a water

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In the future, all 460-volt safeguard system breaker control devices will be checked during annual refueling outages. In addition, an immediate inspcetion is being made of all 460-volt safeguard system breakers.

We are enclosing forty copies of this letter.

Very truly yours, G1)

.td.

Ivan R. Finfro I, J Manager, Nuclear Generating Stations IRF/pk s

Enclosures cc: Mr. J. P.'0'Reilly, Director Regulatory Operations I

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