ML20083C991

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Applicant Exhibit A-25,consisting of Draft of 900320 Refueling Outage
ML20083C991
Person / Time
Site: Vogtle  
Issue date: 04/21/1995
From:
AFFILIATION NOT ASSIGNED
To:
References
OLA-3-A-025, OLA-3-A-25, NUDOCS 9505230206
Download: ML20083C991 (12)


Text

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USNRC GPC EXHIBIT 25 STRINGfELLOW EX. B

'95 MAY -3 P2 :52 NUCLEAR REGULATORY COMM!SSION ggs w -c te 3 0FFict cr SECRE TARY Do*t n r*N-*' ' - 3 0ccial Exh. No.

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On 3-20-90, Unit 1 was in a refueling outage and Unit 2 was operating at 100%

power. At 0820 C iT, the driver of a fuel truck in the switchyard backed into a support for the phase "C" insulator for the Unit 1 Reserve Auxiliary Transformer (RAT) 1A. The insulator and line fell causing a phase to ground fault. Both Unit 1 RAT 1A and Unit 2 RAT 28 High Side and Low Side breakers tripped, causin i loss of offsite power condition (LOSP). Unit 1 Diesel Generator (DG)gJA and Unit 2 DG28 started, but DGIA tripped, causing a loss of residual heat remival (RHR) to the reactor core since tie Unit 1 Train B RAT and DG were out of se1vice for maintenance. A Site Area Emergency (SAE) was declared and the alte Emergency Plan was implemented. The core heated up to 136 degrees F from 90 degree F b6 fore the DG was emergency started at 0856 CST and RHR was restored.1 At 0915 CST, the SAE was downgraded to an Alert after onsite power was restored.

The direct cause of this series of events was a cognitive personnel error. The truck driver failed to use proper backing procedures and hit a support, causing the phase to ground fault and LOSP. The most probable cause of the DGIA trip was the intermittent actuation of the DG jacket water temperature switches.

Corrective actions include stren thening policies for control of vehicles, extensive testing of the DG, eplacementofsuspectDGtemperatureswitches[

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A.

REQUIREMENT FOR REPORT i

This event is reportable por: a) 10 CFR 50.73 (a)(2)(iv), because an unplanned Engineered Safety Feature (ESF) actuation occurred when the ESF Actuation System Sequencer started, and b) Technical Specification 4.8.1.1.3, because a valid diesel generator failure occurred. Additionally, this report serves as a summary of the Site Area Emergency event.

8.

UNIT STATUS AT TIME OF EVENT Unit I was in Mode 6 (Refueling) at 0% rated thermal power. The reactor had been shut down since 2-23-90 for a 45 day scheduled refueling outage. The reactor core reload had been completed, the initial tensioning of the reactor vessel head studs was complete, and the outage team was awaiting permission from the control room to begin the final tensioning. Reactor Coolant System (RCS)l (RHR) pump in service for decay heat removal..Thelevel Residual Heat Remova temperature of the RCS was being maintained at approximately 90 degrees F.

Due to the refueling outage maintenance activities in progress, some equipment was out of service and several systems were in abnormal configurations. The Train B Diesel Generator (DGlB) was out of service for a required 36 month maintenance inspection. The Train B Reserve Auxiliary Transformer (RAT 18) had been removed from service for an oil change.

The Train B Class IE 4160 Volt switchgear,1BA03, was being powered from the Train A RAT 1A through its alternate supply breater. All non-1E switchgear was being powered from the Unit Auxiliary Transformers (UAT)had beenby backfeeding from the switchyard. All Steam Generator (5/G) nozzle dans removed, but only S/G's 1 and 4 had their primary manways secured.

Maintenance personnel were in the process of restoring the primary manways on S/G's 2 and 3.

RCS level was being maintained at mid-loop for valve repairs and t_he S/G manway restorations. In addition, the pressurizer aanway was removed to provide an RCS vent path.

C.

DESCRIPTION OF EVENT l

On March 20, 1990, at approximately 0817 CST, a truck driver with a security escort entered the protected area in a fuel truck. Although not a member of the plant operating staff, the driver was a Georgia Power Company employee belonging to a service group used to perform various plant services. The driver checked the welding machine that was in the area and found that it did not need fuel. He returned to the fuel truck and was in the process of backing out of the area when he hit a support holding the phase 'C' insulator for RAT 1A. The insulator and line fell causing a phase to ground fault, and the transformer tripped.

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At 0820 CST, both Unit 1 RAT 1A and the Unit 2 RAT 28 High Side and Low Side breakers tripped causing a loss of offsite power condition (LOSp) to the Unit 1 Train A Class IE 4160 volt Bus IAA02, the Unit 2 Train 8 Class IE Bus 28A03 and the 480 volt busses supplied by 1AA02 and 28A03. The Unit 1 TrainBClassIE4160voltbus18A03alsolostpowersinceRAT1Awas feeding both Trains of Class IE 4160 volt busses. The loss of power caused the associated ESF Actuation Systes Sequencers to send a start signal to one Unit I and one Unit 2 Diesel Generators. DGIA and DG2B started and 1

sequenced the loads to their respective busses. Further description of the i

Unit 2 response to this event is provided in LER 50-425/1990-002.

One minute and twenty seconds after DGIA started and sequenced the loads to

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the Class IE bus, the engine tripped. This again caused an undervoltage (UV) condition to class IE bus 1AA02. The UV signal is a maintained signal at the sequencer. However, since DG1A was coasting down from the trip, the shutdown logic did not allow the DG fuel racks or starting air solenoids to open and start the engine. This properly caused the engine sta* ting logic to lock up, a condition that existed until the UV signal was resat. For this reason, DG1A did not automatically re-start after it tripped.

After the trip, operators were dispatched to the engine control panel to investigate the cause of the trip.

According to the operator, several 4,p annunciators were lit. Without fully evaluating the condition, the

>operatorresettheannunciators.

During this time, a Shift Supervisor (SS) determine if any problems were prese)nt on the 1A sequencer.and a Plant Equ The SS pushed the UV reset button, then reset the sequencer by doenergizing and energizing the power supply to the sequencer. This caused the DG air start solenoid to energize for another 5 seconds which caused the engine to start. This happened lg minutes after the DG tripped the first time. The engine started and the sequencer sequenced the available loads as designed. After 1 minute and 10 seconds, the breaker and the engine tripped a second time. It did not automatically re-start due to the starting logic being blocked as described above. By this time, operators, a maintenance foreman and the diesel generator vendor representative were in the DG roce. The initial report was that the jacket water pressure trip was the cause of the. trip.

The maintenance foreman and vendor representativa observed that the jacket water pressure at the gauge was about 12-13 PSIG. The trip setpoint is 6 PSIG and the alarm setpoint is 8 PSIG. Also, the control room observed a lube oil sensor malfunction alars.

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1 At 0820 CST, both Unit 1 RAT 1A and the Unit 2 RAT 28 High Side and Low Side j

breakers tripped causing a loss of offsite power condition (LOSP) to the Unit 1 Train A Class 1E 4160 volt Bus 1AA02, the Unit 2 Tra9n B Class IE Bus 2BA03 and the 480 volt busses supplied by 1AA02 and 2BA03. The Unit 1 TrainBClassIE4160voltbus18A03alsolestpowersinceRAT1Awas feeding both Trains of Class 1E 4160 volt busses. The loss of power caused the associated ESF Actuation System Sequencers to send a start signal to one Unit I and one Unit 2. Diesel Generators. DGIA and DG2B started and sequenced the loads to their respective busses. Further description of the Unit 2 response to this event is provided in LER 50-425/1990-002.

One minute and twenty seconds after DGIA started and secuenced the loads to the Class 1E bus, the engine tripped. This again causec an undervoltage (UV) condition to class IE bus 1AA02. The UV signal is a maintained signal at the sequencer. However, since DGIA was coasting down from the trip, the shutdown logic did not allow the DG fuel racks or starting air solenoids to open and start the engine. This properly caused the engine starting logic to lock up, a condition that existed untti the UV. signal was reset. For this reason, DG1A did not automatically re-start after it tripped.

After th p, operators were dispatched to the engine control panel to invest' e cause of the trip.

According to the operator, several bgc edN jM annuncf re lit. Without fully evaluating the condition, the 1

operato et the annunciators.

During this time, a Shift Supervisor

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(SS)andaflantEqui nt Operator (PE0) went to the sequencer panel to

[ eN' detemigif any prob s were present on the 1A sequencer. The SS pushed the UV reset button, then reset the sequencer by deenergizing and energizing the power supply to the sequencer. This caused the DG air start solenoid to energize for another 5 seconds which caused the engine to start. This happened 19 minutes after the DG tripped the first time. The engine started and the sequencer sequenced the available loads as designed. After 1 minute and 10 seconds, the breaker and the engine tripped a second time. It did not automatically re-start due to the starting logic being blocked as described above. By this time, operators, a maintenance foreman and the diesel generator vendo. representative were in the DG roce. The initial report was that the jacket water pressure trip was the cause of the trip.

The maintenance foreman and vendor representative observed that the jactot water pressure at the gauge was about 12-13 PSIC. The trip setpoint is 6 PSIG and the alars setpoint is 8 PSIG. Also, the control room observed a lube oli sensor malfunction alare.

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Fifteen minutes after the second DGIA trip, DGIA was started from the engine control panel using the emergency start breakglass button. The engine started and loads were manually loaded. Ifhen the DG is started in the emergency mode, all the trips except four are bypassed. However all alarms will be annunciated. During the emergency run. no trip alarms we,re noticed by the personnel either at the control room or at the engine control panel.

The only alarms noted by the control room operator assigned for DG operation were lube oil pressure sensor malfunction and fuel oil level high/ low alam.

At 1040 CST, RAT 18 was energized to supply power to 4160 volt bus IBA03.

DGIA suppiled power to 4160 volt bus 1AA02 until 1157 CST, at which time bus 1AA02 was tied to RAT 18.

9 A Site Area Emergency was declared at 0840 CST, due to a loss of all offsite and onsite AC power for more than 15 minutes. The Emergency g'

J Director signed the notification form used to inform offsite government agencies of the emergency at 0848 CST and notifications began at 0857 CST. f7, Due to the loss of power, which rendered the primary Emergency Notification <g",

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Network (ENN) inoperable, and some mis-communication, the initial

\\r notification was not received by all agencies untti 0g35 CST.

The Emergency Director instructed personnel to complete various tasks for restoring containment and RCS integrity. A11' work was accomplished and maintenance personnel exited containment by 1050 CST.

The SAE was downgraded to an Alert Emergency at 0g15 CST after restoration of core cooling and one train of electrical power. By 1200 CST, plant M conditions had stabilized with both trains of electrical power being supp11ec fromeoffsite source ((RAT 18).

After discussions with the NRC and local government agencies, the emergency was terminated at 1247 CST and all agencies were notified by 1256 CST.

D.

CAUSE OF EVENT et PmlECT c57938 Direct Cause:

1.

The direct cause of the loss of offsite Class IE AC power was the fuel truck hitting a pole supporting a 230kV line for RAT 1A. This was a cognitive personnel error on the part of the truck driver. There were no unusual characteristics of the work location that directly contributed to this personnel error.

2.

The direct cause of the loss of onsite Class 1E AC power was the failure of the operable DG, DGIA, to start and load the LOSP loads on buss i

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Fifteen minutes after the second DGIA trip, DG1A was started from the engine control panel using the emergency start breakglass button. The engine started and loads were manually loaded. When the OG is started in the emergency mode, all the trips except four are bypassed. However, all alarms will be annunciated. During the emergency run, no trip alarms were noticed by the ersonnel either at the control room or at the engine control panel.

The on1 alams noted by the control room operator assigned for DG operation were lu oil pressure sensor malfunction and fuel oil level high/ low alars.

At 1040 CST, RAT 1B was energized to supply power to 4160 volt bus 1BA03.

DGIA supplied power to 4160 volt bus 1AA02 until 1157 CST, at which time bus IAA02 was tied to RAT 15.

A Site Area Emergency was declared at 0840 CST, due to a loss of all

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offsite and onsite AC power for more than 15 minutes. The Emergency Director signed the notification form used to inform offsite government agencies of the emergency at 0848 CST and notifications began at 0857 CST.

Due to the loss of power, which rendered the primary Emergency Notification Network (ENN) inoperable, and some mis-communication, the initial notification was not received by all agencies until 0g35 CST. - Mx;;nt

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The Emergency Director instructed personnel to complete various tasks for restoring containment and RCS integrity. All work was accomplished and maintenance personnel exited containment by 1050 CST.

The SAE was downgraded to an Alert Energency at 0915 CST after restoration of core cooling and one train of electrical power. By 1200 CST, plant conditions had stabilized with both trains of electrical power being supplied from offsite sources (RAT 1B).

After discussions with the NRC and local government agencies, the emergency was terminated at 1247 CST and all agencies were notified by 1256 CST.

D.

CAUSE OF EVENT Direct Cause:

1.

The direct cause of the loss of offsite Class IE AC power was the fuel truck hitting a pole supporting a 230kV line for RAT 1A. This was a cognitive personnel error on the part of the truck driver. There were no unusual characteristics of the work location that directly contributed to this personnel error.

2.

The direct cause of the loss of onsite Class 1E AC power was the failure of the operable DG, DGIA, to start and load the LOSP loads on buss 1AA02.

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Root Cause:

1.

The truck driver met all current site training and qualification requirements, including holding a Class 2 Georgia driver's license, s' '{ However, site safety rules, which require a flagman for backing vehicles when viewing is impaired, were violated.

A 2.

The root cause for the failure of DG1A has not been conclusively determined. There is no record of the trips that were annunciated after the first trip because the annunciators were reset before the condition was fully evaluated. Therefore, the cause of the first trip can only be postulated, but it was most likely the same as that which caused the second trip. The second trip occurred at the end of the timed sequence of the group 2 block logic. This logic allows the DG to achieve operating conditions before the trips become active. The block logic timed out and the trip occurred at about 70 seconds. The annunciators observed at the second trip included jacket water high temperature along with other active trips. In conducting an investigation, the tri> conditions that were observed on the second DG trip on 3-20-90 could >e duplicated by venting 2 out of 3 jacket water temperature sensors, simulating a trip >ed condition. The simulation dupitcated both the annunciators and t to 70 sec. trip time. The most likely cause of the DG trips was intermittent actuation of the jacket water temperture switches.

Following the 3-20-90 event, all three jacket water temperature switches, which all have a design setpoint of 2000F, were bench tested.

Switch TS-19110 was found to have a setpoint of 197 degrees F, which i

was approximately 6 degrees below its previous setting. Switch TS-19111 was found to have a setpoint of 199 degrees F, which was approximately the same as the original setting. Switch TS-19112 was found to have a setpoint of 186 degrees F, which was approximately 17 degrees F below the previous setting and was re-adjusted. Switch TS-19112 also had a small leak which was judged to be acceptable to support diagnostic engine tests and was reinstalled. The switches were recalibrated with the manufacturer's assistance to ensure a consistent calibration technique.

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During the subsequent test run of the DG on 3-30-90, one of the switches (TS-19111) tripped and would not reset. This appeared to be an intermittent failure because it subsequently mechanically reset.

This switch and the leaking switch (TS-19112) were replaced with new switches. All subsequent testing was conducted with no additional problems.

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A test of the jacket water system temperature transient during engine starts was conducted. The purpose of this test was to determine the actual Jacket water temperature at the switch locations with the engine in a normal standby lineup, and then followed by a series of starts without air rolling the engine to repli,cate the starts of 3-20-90. The test showed that jacket water temperature at the switch location decreased from a standby temperature of 163 degrees F to approximately 156 degrees F and remained steady.

i Numerous sensor calibrations (including jacket water temperatures),

special pneumatic leak testing, and multiple engine starts and runs were >erformed under various conditions. Since 3-20-90, DG1A and DG1B j

goM have >een started several times (more than twenty times each) and no failures or problems have occurred durini any of these starts. In addition, an undervoltage start test wit Dut air roll was conducted on 4-6-go and DGIA started and loaded properly.

Based on the above facts, it is concluded that the jacket water high temperature switches were the most probable cause of both trips on 3-20-90.

E.

ANALYSIS OF EVENT The loss of offsite power to Class 1E bus 18A03 and the failure of DGIA to start and operate successfully, coupled with DG1B and RAT 18 being out of service for maintenance, resulted in Unit 1 being without AC power to both Class 1E busies. With both Class 1E busses deenergized, the RHR Systes could not perfors its required safety function. Based on a noted rate of rise in the RCS temperature of 46 degrees F in 36 minutues, the RCS water would not have been expected to begin boiling until approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 36 minutes after the beginning of tho event.

Restoration of RHR and closure of the containment equipment hatch were completed well within the estimated I hour and 36 minutes for the projected l

onset of boiling in the RCS. A review of information obtained from the Process and Effluent Radiation Monitoring Systes (PERMS)is event, noand grab s analysis indicated all normal values. As a result of th increase in radioactive releases to either the containment or the

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Additional systems were either available or could have been made available to ensure the continued safe operation of the plant:

1 1.

The maintenance on RAT 18 was completed and the RAT iras returned to service approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> into the event.

2.

Offsite power was available to non-1E equipment through the generator step-up transformers which were being used to "back-feed' the Unit Auxiliary Transformers (UAT)lt was cleared, Class IE busses IAA02 and and supply the non-1E busses. Provided that the phase to ground fau 1BA03 could have been powered by feeding through non-1E bus 1NA01.

3.

The Refueling Water Storage Tank could have been used to manually establish gravity feed to the RCS to maintain a supply of cooling water to the reactor.

Consequently, neither plant safety nor the health and safety of the public was adversely affected by this event. A more detailed assessment of this event and an assessmen the event had it occurred under more severe circumstances will be rformed and included in a supplemental LER.

F.

CORRECTIVE ACTIONS 1.

A management policy on control and operation of vehicles has been established.

2.

Tem>orary barricades have been erected with signs which direct auttorization for control of switchyard traffic to the SS.

3.

The loss of Offsite Power (LOSP) diesel start and trtp logic has been modified on Unit 1 so that an automatic ' emergency" start will occur upon LOSP. Therefore, non-essential diesel engine trips are blocked upon LOSp. The Unit 2 OG's will be modified by 4-30-90.

4.

The DGIA test frequency was increased to three times per week until 4-20-90 when the test frequency will be changed to once every 7 days in accordance with Technical Specification Table 4.8-1.

This frequency E

will be continued untti 7 consecutive valid tests are completed with no 1

more than one valid failure in the last 20 valid tests. Including the t

two valid failures of this event, there have been a total of four valid u

failures in 69 valid tests of DGIA as of 1157 CST on 3-20-90.

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A back-up ENN systes powered from the AT&T system, eich previously existed and was operational for South Carolina agencies, has been added to Georgia local and state agencies. Shift personnel have been instructed concerning energency coemunications systems and their power suppites.

7.

Further corrective actions will be addressed in a supplemental LER.

G.

AD0!TIONAL INFORMATION 1.

Failed Components:

Jacket Water High Temperature Switches manufactured by California Controls Company.

Model #A-3500-W3 2.

Previous Similar Events:

None 3.

Energy Industry Identification System Code:

Reactor Coolant System - A8 Residual Heat Removal System - B Diesel Generator Lube 011 Systee - LA Olesel Generator Starting Air System - LC Olesel Generator Cooling Water Systee - L8 Olesel Generator Power Supply System - EK Safety Injection System - BQ 13.8 kV Power System - EA 1460 volt non-1E power system - EA 1460 volt Class IE power system - E8 Chemical and Volume Control Systee - CB Containment Building - NH 480 volt Class IE Power Systee - EC Engineered Safety Features Actuation System - JE Radiation Monitoring Systes - IL 4

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ff. Further corrective actions will be addressed in a supplemental LER.

G.

ADDITIONAL INFORMATION 1.

Failed Components:

Jacket Water High Temperature Switches manufactured by California Controls Company.

Model #A-3500-W3 2.

Previous Steilar Events:

None 3.

Energy Industry Identification System Code:

Reactor Coolant System - A8 Residual Heat Removal Systes - 8 01esel Generator Lube 011 System - LA Diesel Generator Starting Air Systes - LC Diesel Generator Cooling Water System - LB Diesel Generator Power Supply System - EK Safety Injection System - 8Q 13.8 kV Power Systee - EA 1460 volt non-lE power systes - EA 1460 volt Class IE power systee - EB Chemical and Volume Control System - CB Containment Building - NH 480 volt Class IE Power System - ED Engineered Safety Features Actuation Systee - JE Radiation. Monitoring System - IL 92PRWECT 05m5 l

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