ML20082V328

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Monthly Operating Repts for Nov 1983
ML20082V328
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 11/30/1983
From: Alden W, Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8312200075
Download: ML20082V328 (10)


Text

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OPERATING DATA REPORT DOCKET NO. 50 - 277

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DATE DECEMBER 15, 1983 COMPLETED BY PHILADELPHI A ELECTRIC COMPANY

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N.B. ALD EN ENGINEER -IN -CH ARGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPH ONE (215) 841-5022 4

OPERATING STATUS

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_--=.

1. UNIT NAME: PEACH BOTTOR UNIT 2 l NOTES: UNIT 2 CONTINUED FORCED l

g g

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2. REPORTING PERIOD: NOTEMBER, 1983 J

IGSCC PIPE INSPECTION AND l

g g

3. LICENSED THERNAL POWER (RWT) :

3293 l

REPAIR OUTAGE.

l

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l g

4. NABEPLATE RATING (GROSS HWE) :

1152 I

l

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g g

5. DESIGN ELECTRICAL RATING (N ET MWE) :

1065 l

l g

g

6. 811I505 DEPENDABLE CAPACITY (GROSS NWE) : 1098 l

l g

7. MAIIBU5 DEPENDABLE CAPACITY (NET NWE) :

1051 l

l

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-- _= =___ ___

8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
9. POWER LEYEL TO WHICH RESTRICTED, IF ANY (NET HWE):
10. REASONS FOR RESTRICTIONS, IF ANY:

8312200075 831130 DR ADOCK 05000277 PDR THIS n0 NTH YR-TO-DATE CUEULATIVE

11. HOURS IN REPORTING PERIOD 720 8,016 82,464

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_-_= =

'2.

NUMBER OF HOURS REACTOR WAS CRITICAL 0

3,918.1 59,007.8

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3. REACTOR RESERTE SBUTDOWN HOURS 0.0 0.0 0.0 4 HOURS GENERATOR ON-LINE 0.0 3,834.8 57,363.7

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5. UNIT RESERVE SHUTDOWN BOURS 0.0 0.0 0.0
6. GROSS THERMAL ENERGY GENERATED (HWH) 0 12,187,155 168,696,127 i7. GRDSS ELECTRICAL ENERGY GENERATED (59H) 0 4,029,130 55,549,640

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8. NET ELECTRICAL ENERGY GENEBATED (59H)

-6,575 3,850,229 53,235,378

9. UNIT SERVICE FACTOR 0.0 47.8 69.6
0. UNIT AVAILABILITY FACTOR 0.0 47.8 69.6

.1. UNIT CAPACITY FACTOR (USING BDC NET) 0.0 45.7 61.4

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2. UNIT CAPACITY FACTOR (USING DER NET) 0.0 45.1 60.6

= =,, _ _ _ ---- --

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'3. UNIT FORCED OUTAGE RATE 100.0 50.8 12.8

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4 SHUTDOWNS SCHEDULED OVER NEIT 6 MONTHS (TY PE, DATE, AND DURATION OF EACH) :

REFUELING / MAINTENANCE OUTAGE BEGINNING 2/21/84 FOR 32 WEEKS.

5. IF SHUTDOWN AT END OF REPORT PERIOD, ESTI5ATED DATE OF STARTUP: 12/03/83
6. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COM5ERCIAL OPERATION

- CEG ATIVE T ALUE REPORTED FOR CONSISTENCY WITH FEDERAL ENERGY REGULATORY C05 MISSION REPORTS.

CPERATIN3 DATA REP 3RT 4

DICKET ND. 50 - 278 DATE DECEMBER 15,1983 COMPLETED BT PHILADELPHIA ELECTRIC COMPANY

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W.M. ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE (215) 841-5022 OPERATING STATUS

1. UNIT NAME: PEACH BOTTOR UNIT 3 l NOTES: UNIT 3 EXPERIENCED 1 l

g g

REPORTING PERIOD: N OV EM BER, 1983 l

SHUTDONN FOR RELIEF VALVE l

g g

'. LICENSED THERMAL POWER (MWT) :

3293 l

REPLACEMENT AND 3 l

g g

NAMEPLATE RATING (GROSS RNE) :

1152 l

SCHEDULED LOAD R:90CTIONS.

l g

g DESIGN ELECTRICAL BATING (NET MWE) :

1065 l

l g

MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 1098 l

l g

g CAIIMUM DEPENDABLE CAPACITY '(NET ENE) :

1035 l

l IP CH ANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

POWhR LEVEL TO NHICH RESTRICTED, IF ANY (NET MWE) :

a.

REASONS FOR RESTRICTIONS, IF ANY:

THIS MONTH YR-TO-DATE CUMULATIVE

. HOURS IN REPORTING PERIOD 720 8,016 78,360

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NU3BER OF HOURS REACTOR WAS CRITICAL 648.6 2,147.6 56,077.3

__s.

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REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 HOURS GENERATOR ON-LINE 611.0 2,001.4 54,602.2 UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 GROSS THERMAL ENERGY GENERATED O1WH) 1,900,985 5,578,387 158,794,015 GROSS ELECTRICAL ENERGY GENERATED (MWH) 640,210 1,821,520 52,063,050 NET ELECTRICAL ENERGY GENEllATED (MWH) 617,058 1,691,617 49,934,409 UNIT SERVICE FACTOR 84.9 25.0 69.7

  • . UNIT AV AILABILITY FACTOR 84.9 25.0 69.7 UNIT CAPACITY FACTOR (USING MDC NET) 82.8 20.4 61.6 a

UNIT CAPACITY FACTOR (USING DER NET) 80.5 19.8 59.8

,._ a

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UNIT FORCED OUTAGE RATE 6.9 5.3 7.3 SHUTDOWNS SCHEDULED OVER NEIT 6 MONTHS (TYPE, D ATE, AND DURATION OF EACH) :

IF SHUTDCEN AT END OF REP 0h? FERIOD, ESTIMATED DATE OF STARTUP: 10/19/85 UNITS IN TEST STATUS (PRIOR TO COMMERCI AL OPER ATION) :

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION N Re. R T T V R V n t.tt R REPonTRn Pon enN9tSTR4FY WITH PRDERAL ENERGY NEGULATORY COMMISSION DI: PORTS.

1

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 - 277 UNIT PEACH BOTTOM UNIT 2 DATE DECEMBER 15, 1983 COMPANY PHILADELPHIA ELECTRIC COMPANY W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE (215) 841-5022 i

MONTH NOVEMBER 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY PCWER LEVEL (MWE-N ET)

(MWE-NET) 1 0

17 0

2 0

18 0

3 0

19 0

4 0

20 0

5 0

21 0

6-0 22 0

7 0

23 0

8 0

24 0

9 0

25 0

10 0

26 0

11 0

27 0

12 0

28 0

13 0

29 0

14 0

30 0

15 0

l 16 0

AYERAGE DAILY UNIT POWER LEVEL DOOKET NO. 50 - 278 UNIT PEACH BOTTOM UNIT 3 DATE DECEMBER 15,1983 COMPANY PHILADELPHIA ELECTRIC COMPANY r

W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISION-NUCLEAR

'E TELEPHONE (215) 841-5022 MONTH NOVEMBER 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-NET)

(M WE-N ET) 1 950 17 938 2

887 18 0

3 1064 19 0

4 1061 20 0

5 1056 21 0

6 1056 22 250 7

1055 23 924 8

1054 24 873 9

1053 25 987 10 1054 26 1065 11 1052 27 1073 12 836 28 1072 13 1028 29 1074 14 1073 30 1074 h

15 1071 lo 1076

l UNIT SHUTDOWN $ AND PONER REDUCTIONS DOCKET NO. 50 - 277 UNIT NAME PAACH BOTTOM U3It 2 DATE DECEMBER 15, 1963 REPORT MONTH NOVEMBER, 1983 COEPLETED BY PHILADELPHIA ELECTRIC COMPANY

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W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION GENERATION DIVISIuN-NUCLEAk TELEPHONE (215) 841-5022

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ENTRY SHEETS FOR LICENSEE 3 - AUTOMATIC SCRAM.

EVENT REPORT (LER)

C - REFDELING D - REGOLATORI RESTRICTION 4 - OTHER (EIPLAIN)

FILE (N U R EG-0161)

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a UNIT St:UTDONNS AND PONER REDUCTIONS DOCF.ET NO. 50 - 27d a

UNIT NAME PEACH BOTTOM UNIT 3

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4 DATE DECEMBEk 15,1963

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REPORT MONTH NOVEMBER, 1983 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY s

W.M.ALDEN ENGINEER-IN-CHARGE d

LICENSING SECTION GENERATION DIVISION-MUCLEAk TELEPHONE (215) d41-5022

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ENTRY SHEETS FOR LICLMSEE i

C - REFUELING 3 - AUTOMATIC SCRAM.

EVENT REPORT (LEtt J

D - REGULATORY RESTRICTION 4 - OTHER (EIPLAIN)

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G - OPERATION AL ERROR (EYPLAIN)

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EIHIBIT I - SAME SOURCE a

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Dockst No. 50-277 Attachment to Monthly Operating Report for November, 1983 REFUELING INFORMATION 1.

Name of facility:

Peach Bottom Unit 2 2.

Scheduled date for next refueling shutdown:

February 20, 1984 3.

Scheduled date for restart following refueling:

October 1, 1984 4.

Will refueling or resumption of operation thereaf ter require a technical apecification change or other license amendment?

Yes

(

If answer is yes, what, in general, will these be?

Technical Specifications to accommodate reload fuel.

Modifications to reactor core operating limits.

Technical specification changes associated with snubber i

j reduction program.

5.

Scheduled date(s) for submitting proposed licensing action and supporting information:

July 2, 1984 for reload fuel; prior to December 21, 1984 for snubber reduction program.

6.

Important licensing considerations associated with refueling, e.g.,

new or different fuel design or supplier, unreviewed design or performance, analysis methods, significant changes in fuel design, new operating procedures:

None expected.

7.

The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:

I (a)

Core - 764 Fuel Assemblies (b)

Fuel Pool - 1170 Fuel Assemblies, 58 Fuel Rods 8.

The present licensed spent fuel pool storage capacity and the F

size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.

9.

The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.

September, 1990 (Mar ch, 1986, with reserve full core discharge)

Dockst No. 50-278 Attechment to Monthly Operating Report for November,1983 REFUELING INFORIRTION 1.

Name of facility:

Peach Bottom Unit 3 2.

Scheduled date for next refueling shutdown:

March 30, 1985.

3.

Scheduled date for restart following refueling:

September 21, 1985.

4.

Will refueling or resumption of operation thereaf ter require a technical specification change or other license amendment?

Yes.

If answer is yes, what, in general, will these be?

Technical Specifications to accommodate reload fuel.

Modifications to reactor core operating limits.

Technical specification changes associated with snubber reduction program.

5.

Scheduled date(s) for submitting proposed licensing action and supporting information:

June 21, 1985 for reload fuel; No later than. January 2, 1985 for snubber reduction program.

6.

Important licensing considerations associated with refueling, e.g.,

new or diff erent fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, now operating procedures:

None expected.

7.

The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:

(a)

Core - 764 Fuel Assemblies (b)

Fuel Pool - 1212 Fuel Assemblies, 6 Fuel Rods 8.

The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.

9.

The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.

September, 1991 (Mar ch, 1987, with reserve for fuel core discharge)

~

Dockot Non. 50-227 50-278 Attachment to Monthly Operating Report for November, 1983 PEACH BOTTOM ATOMIC POWER STATION NARRATIVE

SUMMARY

OF OPERATING EXPERIENCES November, 1983 Unit 2 Unit 2 remained shutdown for the entire month of November for inspection of primary system piping welds and the application of weld repairs on the. reactor recirculation system and shutdown cooling system.

On November 2, the E-1 diesel generator was out-of-service for repair of an oil leak.

On November 15, an unusual event was declared when a ventilation stack radioactive release of 3% of Tech Specs occurred.

The release occurred as a result of fuel pin puncturing work by General Electric in the fuel pool.

A previous occurrence on Unit 3 had resulted in a change to the procedures which resulted in some reduction in the release.

All such work has been halted until a significantly better method can be found.

On November 25, Unit 2 Reactor Hydrostatic Testing was performed.

The unit ended the report period with final preparations for startup.

NRC authorization for plant restart was issued on November 30th.

Unit 3 The unit began the month at full power.

Reactor power was reduced to 770 MWe on November 1 for a control rod adjustment.

The unit was returned to full power on November 3.

On November 10, the 3C main steam line radiation monitor failed causing a half scram and a half Group I isolation; the radiation monitor was returned to service that same morning.

[

Reactor power was reduced to 650 MWe on November 11 for a control rod adjustment.

The unit was returned to full power on November 13.

RCIC was taken out-of-service on November 14

~

to repair the turbine trip / throttle valve and returned to service three days later.

On November 17, the unit was shut

'down for replacement of 71E main steam line relief valve due to acoustic leak indication.

The valve was replaced and startup began on November 20.

Reactor power was reduced to 600 MWe on November 24 for a control rod adjustment.

The unit achieved full power on November 26.

PHILADELPHIA ELECTRIC COMPANY 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 (215)841-4000 December 15, 1983 Docket Nos. 50-277 50-278 Director l

Office of Inspection & Enforcement US Nuclear Regulatory Commission I

Washington, DC 20555 Attention:

Document Control Desk l

l

SUBJECT:

Peach Bottom Atomic Power Station Monthly Operating Report Gentlemen:

Attached are twelve copies of the monthly operating report for Peach Bottom Units 2 and 3 for the month of November, 1983 forwarded pursuant to Technical Specification 6.9.1.C under the guidance of Regulatory Guide 10.1, Revision 4.

Very truly yours, M

. Cooney

[gperintendent Yuclear Generation Division Attachment cc:

Dr. T. E. Murley, NRC Mr. A.

R. Blough, NRC Site Inspector Mr. Stan P. Mangi, Dept. of Envir. Resources Mr.

P. A. Ross, NRC INPO Records Center s>91 ip