ML20081L310
| ML20081L310 | |
| Person / Time | |
|---|---|
| Site: | Point Beach |
| Issue date: | 11/04/1983 |
| From: | Fay C WISCONSIN ELECTRIC POWER CO. |
| To: | Office of Nuclear Reactor Regulation |
| References | |
| NUDOCS 8311160084 | |
| Download: ML20081L310 (9) | |
Text
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DOCKET NO.
50-266 T
UNIT NAME Point Beach Unit 1 t
DATE November 4, 1983 l
COMPLETED BY C.
W.
Fay g-l TELEPHONE 414/277-2811 AVERAGE DAILY UNIT POWER LEVEL f
October MONTH AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET _
DAY MWe NET DAY MWe NET 1
4 11
-2 21
-2 2
-9 12
-2 22
-2 3
-3 13
-2 23
-2
=I-4
-2 14
__ 24
-1 5
-2 15
-2 25
-2 6 16
-2 26
-2 i
7
-2 17
-2 27
-2 8
-2 18
-2 28
-2 9
-2 19
-2 29
-2
[
1 10
-2 2d
-2 30
-2 l
31
-2 e%
8311160084 831104 PDR ADOCK 05000266
? AD-28A (1-77)
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UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET MO. 50-266
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UNIT NAME Point Beach Unit 1 REPORT MONTH October DATE November 4, 1983 COMPLETED BY C.
W.
Fay TELEPIIONE 414/277-2811 en k
c w tn o u
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St Pe O
vu o
co v m eo co No.
Date g
gg g
jgy Licensee Event y
y Cause and Corrective Action e
am o
oa Report No.
m so To Prevent Recurrence o-a; emc o
- E:
3 o
oQ 3
801001 S
740.7 C
1 N/A ZZ ZZZZZ2 Commenced 26-week refueling and steam generator replacement outage.
F: Forced Reason:
3 4
Method:
Exhibit G-Instruc-S: Scheduled A-Equipment Failure (explain) l-Manual tions for Prepar-B-Maintenance or Test 2-Manual Scram ation of Data Entry C-Refueling 3-Automatic Scram Sheets for LER File D-Regulatory Restriction 4-Other (explain)
E-Operator Training & License Exam F-Administrative 5 Exhibit I-Same AD-28B G-Operational Error (explain)
Source (01-78)
II-Other (explain)
OPERATING DATA REPORT DOCKET NO. 50-266 DA1E November 4, 1983 COMPLETED BY C. W. FAY TELEPHONE 414 277 2811 OPERATIN6 STATUS l
- 1. UNIT NAME: POINT BEACH NUCLEAR PLANT UNIT 1
. NOTES I
- 2. REPORTIN6 PERIOD:
OCTOBER 1983
- 3. LICENSED THERMAL POWER (MUT): 1518.
- 4. NAMEPLATE RATIN6 (GROSS MUE):
523.8 i
l
- 5. DESIGN ELECTRICAL RATING (NET MUE): 497.
- 6. MAXIMUM DEPENDABLE CAPACITY (6ROSS MUE): 519.
I l
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MUE): 495.
- 8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, 6IVE REASONS:
j NOT APPLICABLE
- 9. POWER LEVEL TO UNICH RESTRICTED, IF ANY (NET MUE): Nui APPLICABLE i
- 10. REASONS FOR RESTRICTIONS, (IF ANY): NOT APPLICABLE l
THIS MONTH YR TO DATE CUMULATIVE
- 11. HOURS IN REPORTING PERIOD 745 7,296 113,832
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 3.6 6,506.2 94,078.5
- 13. REACTOR RESERVE *bdTDOWN HOURS 0.0 1.4 625.4
- 14. HOURS 6ENERATOR 6N LINE 3.3 4,499.2 91,607.5
- 15. UNIT RESERVE SHUTBOUN HOURS 0.0 0.0 793.5
- 16. 6ROSS THERMAL ENER6Y 6ENERATED (MUH) 1,496 7,586,323 123,535,3'2
- 17. GROSS ELECTRICAL ENER6Y 6ENERATED (MUN) 500 2,520,190 41,395,'.e0
- 18. NET ELECTRICAL ENER6Y 6ENERATED (MUH) 0 2,383,497 39,365,215
- 19. UNIT SERVICE FACTOR 0.4 89.1 80.5
- 20. UNIT AVAILABILITY FACTOR 0.4 89.1 81.2
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 0.0 66.0 70.7
- 22. UNIT CAPACITY FACTOR (USIN6 DER NET) 0.0 65.7 69.6
- 23. UNIT FORCED OUTA6E RATE 0.0 0.1 2.6
- 24. SHUTDOUNS SCHEDULED DVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
NONE
- 25. IF SHUTD99N AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: MARCH 30, 1984 DATA REPORTED AND FACTORS CALCULATED AS REQUESTED IN NRC LETTER DATED SEPTEMBER 22, 1977
m.
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NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE Docket No.
50-266 Unit Name Point Beach Unit 1 Date November 4, 1983 1
Completed By C. W. Fay Telephone 414-277-2811 i
i Unit 1 was in a coastdown status at the beginning of the 1
period in preparation for the eleventh refueling shutdown and steam generator replacement outage.
The generator was taken off t
line at 0320 hours0.0037 days <br />0.0889 hours <br />5.291005e-4 weeks <br />1.2176e-4 months <br /> on October 31, 1983... Hot rod drop testing was completed 0340 hours0.00394 days <br />0.0944 hours <br />5.621693e-4 weeks <br />1.2937e-4 months <br /> that same day.
The reactor vessel core was i
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unloaded, the head rein' stalled,>and primary system put in layup with a nitrogen gas cover.
In-containment construction'during the period included l
shield wall removal in both "A"'and "B" steam generator cubicles, i
containment crane upgrade, scaffolding support for shielding on the j
primary loops, and construction of grillage and bridgework over.the
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reactor vessel cavity all in preparation for the changeout of the two steam generators.
Among the items under construction on the secondary plant are the replacement of the Nos. 4 A&B feedwater heaters, the replacement of "A",
"B",
"C", and "D" moisture-separator-reheater l
tube bundles, NDE inspection of the extraction steam lines, cleaning and inspection of the main feed pump motors, and the cleaning and d
lapping of the main steam safety valves.
j Other safety-related testing and maintenance completed during the period included the 4D emergency diesel annual inspection,
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maintenance to the spare residual heat removal pump, inspection of 2
residual heat removal heat exchanger lHX-llA, inservice testing ~of-i the auxiliary feedwater system steam-driven pumps and valves,-and flow tests for the high and low-head safety injection pumps.
During an initial review of Unit 1 refueling" leakage tests:
of containment isolation valves'on October 17, 1983,-three. valves were discovered to have leakage such that-the limit-in Technical i
. Specification 15.4.4.3.B would have been-exceeded.
The three valves-include the_ containment purge exhaust valve (3212), the containment j
i purge supply valveL(3245), and the charging-line check valve (370).
This event is reportablecin accordance with Technical Specification.
15.6.9.2.A.3, " abnormal degradation discovered in fuel: cladding, j.
reactor coolant-pressure boundary, or-primary l containment", and a.
14-day LicenseesEvent Report will-be prepared forithe'NRC upon-completion.ofzall containment isolation valve testing.- The Residents Inspector was notified of this event.
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-301
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UNIT NAME Point Beach Unit 2 REPORT MONTH October DATE November 4, 1983 COMPLETED BY C.
W.
Fay TELEPHONE 414/277-2811 mu C
M@o v
as "c
St Po En
- o au o
eae am ao No.
Date g
(j g jjg Licensee Event gg gg Cause and Corrective Action m
e am o
or Report No.
m so To Prevent Recurrence Q~
M emC o
E 3
U O
4 831011 F
5.7 A
3 N/A EB INSTRU Voltage spike in the red instrument bus caused by a capacitor failure in inverter 2DY01 sent spurious "B" steam generator feed flow trip sig-nal.
The capacitor was replaced.
1 F: Forced Reason:
Method:
Exhibit G-Instruc-S: Scheduled A-Equipment Failure (explain) l-Manual tions for Prepar-B-Maintenance or Test 2-Manual Scram ation of Data Entry C-Refueling 3-Automatic Scram Sheets for LER File D-Regulatory Restriction 4-Other (explain)
E-Operator Training & License Exam F-Administrative 5 Exhibit I-Same AD-28B G-Operational Error (explain)
Source (03 -78 ) -
H-Other (explain)
1
-=,1 DOCKET NO.
50-301 UNIT NAME Point Beach Unit 2 j
DATE November 4, 1983 COMPLETED BY C. W.
Fay l
l TELEPHONE 414/277-2811 1
AVERAGE DAILY UNIT POWER LEVEL MONTH October AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1
491 11 340 21 489 2
489 12 488 22 491 1
3 488 13 491 23 491 4
'488 14 488 24 491 5
489 15 491 25 490 6
488 16 491 26 491 l
7 489 17 492 27 490 8
489 18 489 28 492 9
489 19 492 29 490 10 489 20 492 30 490 31 490 AD-28A (1-77)
OPERATING DATA REPORT DOCKET NO. 50-301 DATE November 4, 1983 COMPLETED BY C. W. FAY TELEPHONE 414 277 2811 1
OPERATIN6 STATUS
- 1. UNIT NAME: POINT BEACH NUCLEAR PLANT UNIT 2
. NOTES l
l
- 2. REPORTIN6 PERIOD:
OCTOBER 1983
- 3. LICENSES THERNAL POWER (NUT): 1518.
- 4. NAMEPLATE RATING (6ROSS MUE):
523.8
- 5. DESI6N ELECTRICAL RATING (NET MWE): 497.
- 4. NAXINUM DEPENSABLE CAPACITY (6ROSS MWE): 519.
l l
-7. MAXIMUM DEPENSABLE CAPACITY (NET MWE): 495.
- 8. IF CHANGES OCCUR IN CAPACITY RATIN6S (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
NOT APPLICABLE l
- 9. POWER LEYEL TO WHICH RESTRICTED, IF ANY (NET MWE): NOT APPLICABLE
- 10. REASONS FOR RESTRICTIONS, (IF ANY): NOT APPLICABLE THIS MONTH YR TO DATE CUMULATIVE
- 11. HOURS IN REPORTIN6 PERIOB 745 7,296 98,637
- 12. NUNDER OF HOURS REACTOR WAS CRITICAL 741.5 4,906.1 86,964.2 l
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 1.5 198.3 l
l'
- 14. NOURS SENERATOR ON LINE 739.3 4,783.6 85,438.8 l
- 15. UNIT RESERVE SHUT 90WN HOURS 0.0 1.5 182.7
- 14. GROSS THERNAL ENER6Y SENERATED (MWH) 1,115,645 7,169,793 118,685,387
- 17. BROSS ELECTRICAL ENER6Y 6ENERATED (NWH) 378,240 2,413,030 40,214,430 1
- 18. NET ELECTRICAL ENER6Y GENERATED (NWH) 361,310 2,298,630 38,287,597 l
- 19. UNIT SERVICE FACTOR 99.2 65.6 86.6
-20. UNIT AYAILABILITY FACTOR 99.2 65.6 86.8 i
- 21. UNIT CAPACITY FACTOR (USIN6 MBC NET) 98.0 63.6 79.0 l
- 22. UNIT CAPACITY FACTOR (USING DER NET) 97.6 63.4 78.1
)
'23. UNIT FORCEB OUTA6E RATE 0.8 0.8 1.5 J
- 24. SHUTBOUNS SCHEBULEB OVER NEXT 4 MONTHS (TYPE, DATE, AND DURATION OF EACH):
NONE
- 25. IF SHUT 90WN AT EN8 0F REPORT PERIO3, ESTINATED BATE OF STARTUP: NOT SHUTDOWN
. DATA REPORTES AND FACTORS CALCULATED AS RE00ESTED IN NRC LETTER 3*TED SEPTEMBER 22, 1977
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NARRATIVE sui 4 MARY OF OPERATING EXPERIENCE Docket No.
50-301 Unit Name Point Beach Unit 2
-Date November 4, 1983 Completed By C. W. Fay Telephone 414-277-2811 Unit 2 operated at approximately 490 MWe net throughout the period with'one unplanned outage.
On October 10, 1983 at 0617 hours0.00714 days <br />0.171 hours <br />0.00102 weeks <br />2.347685e-4 months <br /> the unit experienced a turbine and reactor trip.
The trip was initiated by a capacitor failure in inverter 2DY01 which sent a voltage spike to the red instrument bus causing a spurious "B" steam generator. feed flow alarm.
Operators deenergized the inverter after shifting to an alternate power supply and commenced EOP-5A and EPIP 1.1.
While attempting to return the generator back on line, the unit experienced a second reactor trip from 9% thermal power caused by a low-low steam generator level.
At 1057 hours0.0122 days <br />0.294 hours <br />0.00175 weeks <br />4.021885e-4 months <br /> the reactor was taken critical, at 1158 hours0.0134 days <br />0.322 hours <br />0.00191 weeks <br />4.40619e-4 months <br /> the generator went back on line, and the unit returned to full power at 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br />, approximately nine hours after.the initial trip.
The primary-to-secondary leakage remains at less than ten gallons per day.
During the performance of the auxiliary feed pump tests, motor-operated valve 2MOV-4006, which provides-alternate supply from the service water system to the pump suction, tripped upon stroking.
The thermal overload valves were reset and the valve-stroke tested satisfactorily.
This event was not considered reportable.
Other safety-related testing completed-during the period included inservice testing of the.auxiliaryffeed system pumps and valves, inservice testing.ofqthe containment accident fan coolers, and the inservice testing of(the.high-head.safetyy injection pumps.
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v Sin Electnc roata couranr 231 W. MICHIGAN, P.O. BOX 2046, MILWAUKEE, WI 53201 November 9, 1983 Director of Regulatory Operations U. S. NUCLEAR REGULATORY COMMISSION Washington, D. C.
20555 Gentlemen:
MONTHLY OPERATING REPORTS POINT BEACll NUCLEAR PLANT Attached are monthly operating reports for Units 1 and 2, Point Beach Nuclear Plant, for the calendar month of October 1983.
Very truly yours, YbU Vice President-Nuclear Power C. W.
Fay Attachments Copies to J.
G. Keppler - NRC, Region III NRC Resident Inspector C. F. Riederer - PSCW 8+7
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