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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEAR3F0399-04, Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease1999-03-10010 March 1999 Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease 3F0498-28, Ro:On 980421,unplanned Release of Effluent Water from Crystal River Nuclear Plant Regeneration Waste Neutralization Tank.Root Cause Analysis Currently Being Conducted.Pipe Isolated for Repairs1998-04-23023 April 1998 Ro:On 980421,unplanned Release of Effluent Water from Crystal River Nuclear Plant Regeneration Waste Neutralization Tank.Root Cause Analysis Currently Being Conducted.Pipe Isolated for Repairs 3F0398-21, Special Rept:On 980302,insp Vendor Notified FPC That Grease Sample for Tendon 51H25 Had Water Content of 14.9% Volume by Weight.Caused Undeterminate.Subject Tendon Was Partially re-greased During Performance of Surveillance1998-03-10010 March 1998 Special Rept:On 980302,insp Vendor Notified FPC That Grease Sample for Tendon 51H25 Had Water Content of 14.9% Volume by Weight.Caused Undeterminate.Subject Tendon Was Partially re-greased During Performance of Surveillance 3F0198-07, Special Rept 97-09:provides Details of Conditions Found Not Meeting Acceptance Criteria During Ongoing Twentieth Year Tendon Surveillance of Containment Post Tensioning Sys. Commitments Encl1998-01-0808 January 1998 Special Rept 97-09:provides Details of Conditions Found Not Meeting Acceptance Criteria During Ongoing Twentieth Year Tendon Surveillance of Containment Post Tensioning Sys. Commitments Encl 3F0198-04, Special Rept 97-08:on 971208,mid Range & High Range Noble Gas Stack Monitors Found to Be Inoperable Greater than Seven Days.Cables to low-medium-high Valve Controllers re-connected Inside Radiation Monitoring Panel1998-01-0303 January 1998 Special Rept 97-08:on 971208,mid Range & High Range Noble Gas Stack Monitors Found to Be Inoperable Greater than Seven Days.Cables to low-medium-high Valve Controllers re-connected Inside Radiation Monitoring Panel 3F1297-06, Special Rept 97-07:re Hoop Tendon 51H26 That Was Found to Have Normalized lift-off Force of More than 10% Below Predicted Value.Out of Tolerance Tendons Were Returned to Proper pre-stress Level.Commitment Attached1997-12-0606 December 1997 Special Rept 97-07:re Hoop Tendon 51H26 That Was Found to Have Normalized lift-off Force of More than 10% Below Predicted Value.Out of Tolerance Tendons Were Returned to Proper pre-stress Level.Commitment Attached 3F1197-14, Special Rept 97-03:on 971021,mid Range & High Range Noble Gas Monitors Found Inoperable Greater than Seven Days.Filter Holder Immediately re-installed1997-11-19019 November 1997 Special Rept 97-03:on 971021,mid Range & High Range Noble Gas Monitors Found Inoperable Greater than Seven Days.Filter Holder Immediately re-installed 3F8097-33, Special Rept 97-02:on 970714,fire Suppression Sys Required by Fire Protection Plan Out of Svc for Greater than Fourteen Days.Two Continuous Fire Watches Put in Place as Compensatory Measures as Required by CR-31997-08-22022 August 1997 Special Rept 97-02:on 970714,fire Suppression Sys Required by Fire Protection Plan Out of Svc for Greater than Fourteen Days.Two Continuous Fire Watches Put in Place as Compensatory Measures as Required by CR-3 3F1096-22, Special Rept:On 960902,unit Shutdown Due to Leak in Turbine Lube Oil Sys.Issue Will Be Resolved Before Startup from Current Outage1996-10-28028 October 1996 Special Rept:On 960902,unit Shutdown Due to Leak in Turbine Lube Oil Sys.Issue Will Be Resolved Before Startup from Current Outage 3F0896-25, Special Rept:On 960712,declared Seismic Monitoring Instrumentation Inoperable for More than 30 Days.Caused by Triaxial Peak Accelographs Failures.Instruments Will Be Omitted from FSAR Section 2.5.4.41996-08-28028 August 1996 Special Rept:On 960712,declared Seismic Monitoring Instrumentation Inoperable for More than 30 Days.Caused by Triaxial Peak Accelographs Failures.Instruments Will Be Omitted from FSAR Section 2.5.4.4 3F0496-30, Special Rept 96-02:on 960313,fire Detection Zones Required by Fire Protection Plan Out of Svc for Greater than Fourteen Days.Hourly Fire Watch Established1996-04-26026 April 1996 Special Rept 96-02:on 960313,fire Detection Zones Required by Fire Protection Plan Out of Svc for Greater than Fourteen Days.Hourly Fire Watch Established 3F0396-21, Special Rept 96-01:on 960218,RM-A1 Taken Out of Svc Due to Failure of Detector to Respond to Check Source.Replacement Detector from Stores & Bench Calibrate.Expects to Return RM-A1 to Svc Prior to Restart from Refueling Outage1996-03-26026 March 1996 Special Rept 96-01:on 960218,RM-A1 Taken Out of Svc Due to Failure of Detector to Respond to Check Source.Replacement Detector from Stores & Bench Calibrate.Expects to Return RM-A1 to Svc Prior to Restart from Refueling Outage 3F0895-16, Ro:On 950713,1 H non-emergency Rept Made Re Condition Suspected to Be Outside Design Basis of Plant.Based on Conclusions of Design Basis Evaluation,Rescinds 1 H non-emergency Rept (NRC Event 29062)1995-08-11011 August 1995 Ro:On 950713,1 H non-emergency Rept Made Re Condition Suspected to Be Outside Design Basis of Plant.Based on Conclusions of Design Basis Evaluation,Rescinds 1 H non-emergency Rept (NRC Event 29062) 3F0895-15, Special Rept 95-01:on 950630,ODCM Required Waste Gas Analyzer (WGDA-1) Declared Inoperable & Unavailable for Greater than Seven Days Due to Deficiency in Microprocessor. Microprocessor Replaced & WGDA-1 Returned to Operation1995-08-11011 August 1995 Special Rept 95-01:on 950630,ODCM Required Waste Gas Analyzer (WGDA-1) Declared Inoperable & Unavailable for Greater than Seven Days Due to Deficiency in Microprocessor. Microprocessor Replaced & WGDA-1 Returned to Operation 3F1094-07, Special Rept:On 940919,determined That Two Transmitters Which Comprise Rv Level Indication Sys Portion of Rc Inventory Tracking Sys Not Functioning Normally Due to Line Blockage in Common Tubing.Sys Restoration outage-dependent1994-10-10010 October 1994 Special Rept:On 940919,determined That Two Transmitters Which Comprise Rv Level Indication Sys Portion of Rc Inventory Tracking Sys Not Functioning Normally Due to Line Blockage in Common Tubing.Sys Restoration outage-dependent 3F1293-07, Special Rept 93-03:on 931124,ODCM Required Radiation Monitor Taken Out of Svc Due to Failure to Pass Check Source Functional Test & Unavailable for Greater than 7 Days. Subj Monitor Restored to Normal Operation on 9312061993-12-23023 December 1993 Special Rept 93-03:on 931124,ODCM Required Radiation Monitor Taken Out of Svc Due to Failure to Pass Check Source Functional Test & Unavailable for Greater than 7 Days. Subj Monitor Restored to Normal Operation on 931206 3F1093-17, Special Rept 93-02:on 931011,primary Meteorlogical Sys Taken Out of Svc for Performance of TS Surveillance 4.3.3.4 & TS 3.3.3.4 Entered Since Backup Sys Out of Svc.Surveillance Performed & Sys Returned to Operation on 9310191993-10-27027 October 1993 Special Rept 93-02:on 931011,primary Meteorlogical Sys Taken Out of Svc for Performance of TS Surveillance 4.3.3.4 & TS 3.3.3.4 Entered Since Backup Sys Out of Svc.Surveillance Performed & Sys Returned to Operation on 931019 3F0992-18, Special Rept 92-003:on 920815,auxiliary Bldg high-range Noble Gas Monitor Failed Calibr & Declared Inoperable for More than 7 Days.Automatic Isotopic Monitoring Sys Available for Use.Amplifier Components & detector-sensor Replaced1992-09-24024 September 1992 Special Rept 92-003:on 920815,auxiliary Bldg high-range Noble Gas Monitor Failed Calibr & Declared Inoperable for More than 7 Days.Automatic Isotopic Monitoring Sys Available for Use.Amplifier Components & detector-sensor Replaced 3F0692-10, Special Rept 92-02:on 920514,waste Gas Decay Tank Hydrogen & Oxygen Monitoring Channels Removed from Svc & Not Returned to Operable Status within 14 Days.Caused by Need to Facilitate Maint.Ts Amend Will Be in Place by Sept 19921992-06-12012 June 1992 Special Rept 92-02:on 920514,waste Gas Decay Tank Hydrogen & Oxygen Monitoring Channels Removed from Svc & Not Returned to Operable Status within 14 Days.Caused by Need to Facilitate Maint.Ts Amend Will Be in Place by Sept 1992 3F0592-17, Special Rept 92-01,on 920506,reactor Bldg Purge Exhaust Duct Monitor Was Taken Out of Svc.Caused by Inability to Calibrate RM-A1 Noble Gas Activity.Monitor mid-range Channel Was Recalibrated1992-05-26026 May 1992 Special Rept 92-01,on 920506,reactor Bldg Purge Exhaust Duct Monitor Was Taken Out of Svc.Caused by Inability to Calibrate RM-A1 Noble Gas Activity.Monitor mid-range Channel Was Recalibrated 3F0591-02, Special Rept 91-001:on 910320,waste Gas Analyzer Removed from Svc to Allow Isolation of Waste Gas Compressor from Maint.Moisture Discovered in Sample Tubing.Work Request to Correct Moisture Intrusion in Analyzer Sample Lines Written1991-05-0101 May 1991 Special Rept 91-001:on 910320,waste Gas Analyzer Removed from Svc to Allow Isolation of Waste Gas Compressor from Maint.Moisture Discovered in Sample Tubing.Work Request to Correct Moisture Intrusion in Analyzer Sample Lines Written 3F1190-13, Special Rept 90-04:on 901015,portion of Mounting Platform for Triaxial Peak Accelograph on Piping on Top of Steam Generator Melted1990-11-21021 November 1990 Special Rept 90-04:on 901015,portion of Mounting Platform for Triaxial Peak Accelograph on Piping on Top of Steam Generator Melted 3F0989-08, Special Rept 89-001:on 890826,dose Equivalent Iodine Dei of RCS Samples Exceeded Tech Specs Limit.Sampling & Analysis of RCS Continued at 4 H Intervals Until Dei Decrease Below Tech Spec Limit.Dei Analysis Results Presented1989-09-21021 September 1989 Special Rept 89-001:on 890826,dose Equivalent Iodine Dei of RCS Samples Exceeded Tech Specs Limit.Sampling & Analysis of RCS Continued at 4 H Intervals Until Dei Decrease Below Tech Spec Limit.Dei Analysis Results Presented 3F0389-01, Ro:On 890118,reactor Coolant Pump 1A Failed.Cause Not Discussed.Sequence of Events Encl1989-03-0101 March 1989 Ro:On 890118,reactor Coolant Pump 1A Failed.Cause Not Discussed.Sequence of Events Encl 3F1188-01, Special Rept 88-001:on 881009,RCS Sample Obtained & Analyzed for Iodine Activity Indicated Dose Equivalent Iodine (Dei) Exceeding Tech Spec Limit.Chemists Continued Sampling & Analysis of RCS at Intervals Until Dei Decreased1988-11-0101 November 1988 Special Rept 88-001:on 881009,RCS Sample Obtained & Analyzed for Iodine Activity Indicated Dose Equivalent Iodine (Dei) Exceeding Tech Spec Limit.Chemists Continued Sampling & Analysis of RCS at Intervals Until Dei Decreased 3F0688-19, Ro:On 880527,emergency Feedwater Piping Near Flow Control Valve Found to Be Warmer than Normal.Cause Not Stated.Water Added to Reseat & to Cool Emergency Feedwater Line & Valve Closed to Prevent Inadvertent Manual Addition of Water1988-06-28028 June 1988 Ro:On 880527,emergency Feedwater Piping Near Flow Control Valve Found to Be Warmer than Normal.Cause Not Stated.Water Added to Reseat & to Cool Emergency Feedwater Line & Valve Closed to Prevent Inadvertent Manual Addition of Water 3F0388-02, Special Rept 87-05-01:two Steam Generator Tubes Found Defective,Having Indications Greater than 40% Through Wall & One Tube Identified as Degraded W/Indication of 38% Through Wall.Tubes Removed from Svc by Plugging.Addl Info Encl1988-03-21021 March 1988 Special Rept 87-05-01:two Steam Generator Tubes Found Defective,Having Indications Greater than 40% Through Wall & One Tube Identified as Degraded W/Indication of 38% Through Wall.Tubes Removed from Svc by Plugging.Addl Info Encl 3F0188-19, Special Rept 87-05:during Refuel IV Outage,Steam Generator Eddy Current Testing Revealed Defective tubes.Pre-outage Planning Developed 6% Random Sampling Insp Plan That Would Be Completed on a Steam Generator1988-01-20020 January 1988 Special Rept 87-05:during Refuel IV Outage,Steam Generator Eddy Current Testing Revealed Defective tubes.Pre-outage Planning Developed 6% Random Sampling Insp Plan That Would Be Completed on a Steam Generator 3F1187-09, Special Rept 87-04:Tech Spec 3.3.3.10 Violated.Caused by Removal of Waste Gas Decay Tank Hydrogen & Oxygen Monitors from Svc & Not Returned to Operable Status within 14 Days. Monitors Will Remain Out of Svc Until Sys in Use1987-11-18018 November 1987 Special Rept 87-04:Tech Spec 3.3.3.10 Violated.Caused by Removal of Waste Gas Decay Tank Hydrogen & Oxygen Monitors from Svc & Not Returned to Operable Status within 14 Days. Monitors Will Remain Out of Svc Until Sys in Use ML20236L4161987-11-0505 November 1987 Special Rept 87-03:on 870927,during Channel Check of Triaxial Peak,Monitor SI-005-MEI Found Inoperable.Cause Undetermined.Replacement Monitor to Be Installed After Refueling & Engineering Design Evaluation to Be Made 3F0887-01, Special Rept 87-02:on 870702,reactor Trip Occurred from 88% Rated Thermal Power.Primary Coolant Sample Obtained & Analyzed for Iodine Activity,Per Tech Spec 4.4.8.Reactor Power History,Fuel Burnup & Time Duration Provided1987-08-0303 August 1987 Special Rept 87-02:on 870702,reactor Trip Occurred from 88% Rated Thermal Power.Primary Coolant Sample Obtained & Analyzed for Iodine Activity,Per Tech Spec 4.4.8.Reactor Power History,Fuel Burnup & Time Duration Provided 3F0687-06, Special Rept 87-01:on 870519,auxiliary Bldg & Fuel Handling Area Exhaust Duct mid-range Noble Gas Monitor Inoperable for Seven or More Days.Caused by Alarm Circuit Repair Altering Calibr of Monitor,Rendering Instrument Inoperable1987-06-0909 June 1987 Special Rept 87-01:on 870519,auxiliary Bldg & Fuel Handling Area Exhaust Duct mid-range Noble Gas Monitor Inoperable for Seven or More Days.Caused by Alarm Circuit Repair Altering Calibr of Monitor,Rendering Instrument Inoperable 3F0287-17, Ro:On 870121,during Performance of Surveillance Procedure SP-110,CRD a Ac Breaker Failed to Trip.Caused by Malfunction of Undervoltage Trip Coil Device.Breaker Replaced & Successfully Tested1987-02-23023 February 1987 Ro:On 870121,during Performance of Surveillance Procedure SP-110,CRD a Ac Breaker Failed to Trip.Caused by Malfunction of Undervoltage Trip Coil Device.Breaker Replaced & Successfully Tested 3F0287-21, Ro:On 870112,6-month Interval for Containment Air Lock Type B Tests Found Exceeded Due to Inconsistencies Between Tech Specs & App J.Caused by Failure to Recognize Dual Sources of Requirements.Test Schedule Revised & Tech Spec Changed1987-02-23023 February 1987 Ro:On 870112,6-month Interval for Containment Air Lock Type B Tests Found Exceeded Due to Inconsistencies Between Tech Specs & App J.Caused by Failure to Recognize Dual Sources of Requirements.Test Schedule Revised & Tech Spec Changed 3F0187-07, Special Rept 86-01:on 861223,during Startup from Mode 5,unit Entered Mode 4 W/Noble Gas Activity Monitor & Fuel Handling Bldg Area Exhaust Duct Inoperable.Caused by Poor Response of Installed Check Source.Instrument Recalibr1987-01-0909 January 1987 Special Rept 86-01:on 861223,during Startup from Mode 5,unit Entered Mode 4 W/Noble Gas Activity Monitor & Fuel Handling Bldg Area Exhaust Duct Inoperable.Caused by Poor Response of Installed Check Source.Instrument Recalibr ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 3F0786-22, Ro:On 860629,reactor Bldg Vented to Relieve Long Term Pressure Buildup.Initially Reported on 860630.Draft LER Under Mgt Review to Determine Reporting Requirements.Next Rept Will Be Submitted by 8608081986-07-29029 July 1986 Ro:On 860629,reactor Bldg Vented to Relieve Long Term Pressure Buildup.Initially Reported on 860630.Draft LER Under Mgt Review to Determine Reporting Requirements.Next Rept Will Be Submitted by 860808 3F0386-13, Suppl 2 to Special Rept 85-03:on 850807,intermediate- & high-range Channels of Gaseous Release Monitors RM-A1 & RM-A2 Not Calibr.Mod to Achieve Overlap & Calibr of Intermediate Channels Completed1986-03-31031 March 1986 Suppl 2 to Special Rept 85-03:on 850807,intermediate- & high-range Channels of Gaseous Release Monitors RM-A1 & RM-A2 Not Calibr.Mod to Achieve Overlap & Calibr of Intermediate Channels Completed 3F0286-08, RO:86-002-00:on 860110,incident Occurred in Seawater Intake Area Resulting in Deaths of Two Divers.All Seawater Pumps Shut Off for 2 H 45 Minutes.Ler Will Be Sent by 8602211986-02-10010 February 1986 RO:86-002-00:on 860110,incident Occurred in Seawater Intake Area Resulting in Deaths of Two Divers.All Seawater Pumps Shut Off for 2 H 45 Minutes.Ler Will Be Sent by 860221 3F0885-10, Special Rept 85-03:on 850807,discovered That mid- & high- Range Channels of Gaseous Effluent Release Monitors Out of Calibr.Caused by Delays in Contractual Arrangements for Supplies.Action Taken to Obtain Matls.Part 21 Related1985-08-21021 August 1985 Special Rept 85-03:on 850807,discovered That mid- & high- Range Channels of Gaseous Effluent Release Monitors Out of Calibr.Caused by Delays in Contractual Arrangements for Supplies.Action Taken to Obtain Matls.Part 21 Related 3F0785-29, Revised Special Rept 85-01 Re Inoperability of Three Triaxial Peak Accelographs.Installation of Reactor Vessel Head Device Delayed Until 850714 Due to Unforeseen Activities1985-07-24024 July 1985 Revised Special Rept 85-01 Re Inoperability of Three Triaxial Peak Accelographs.Installation of Reactor Vessel Head Device Delayed Until 850714 Due to Unforeseen Activities 3F0785-30, Suppl 1 to Special Rept 85-02:Halon Portion of Fire Suppression Sys Inoperable.Addl Work Required Due to Unanticipated Difficulties W/Asbestos Matls in Areas Being Modified.Operability Not Restored by 8507011985-07-24024 July 1985 Suppl 1 to Special Rept 85-02:Halon Portion of Fire Suppression Sys Inoperable.Addl Work Required Due to Unanticipated Difficulties W/Asbestos Matls in Areas Being Modified.Operability Not Restored by 850701 3F0585-14, Special Rept 85-02:on 850408,during Refueling & Mod Outage, Halon Portion of Fire Suppression Sys for Cable Spreading Room Taken Out of Svc in Support of Various Mods to Cable Spreading Room.Fire Watches Immediately Established1985-05-22022 May 1985 Special Rept 85-02:on 850408,during Refueling & Mod Outage, Halon Portion of Fire Suppression Sys for Cable Spreading Room Taken Out of Svc in Support of Various Mods to Cable Spreading Room.Fire Watches Immediately Established 3F0485-20, Special Rept 85-01:on 850317,during Performance of Refueling Interval Surveillance,All Three Triaxial Peak Accelographs Required by Tech Specs Discovered Inoperable.Cause Undetermined.Accelographs Will Be Repaired1985-04-26026 April 1985 Special Rept 85-01:on 850317,during Performance of Refueling Interval Surveillance,All Three Triaxial Peak Accelographs Required by Tech Specs Discovered Inoperable.Cause Undetermined.Accelographs Will Be Repaired 3F1284-04, Special Rept SR-84-5:on 841029,Halon Portion of Fire Suppression Sys for Cable Spreading Room Taken Out of Svc for Mod to Cable Spreading Room.Sys Will Be Out of Svc Periodically During Mod for Welding in Cable Spreading Room1984-12-0707 December 1984 Special Rept SR-84-5:on 841029,Halon Portion of Fire Suppression Sys for Cable Spreading Room Taken Out of Svc for Mod to Cable Spreading Room.Sys Will Be Out of Svc Periodically During Mod for Welding in Cable Spreading Room 3F1084-05, Special Rept 84-04:on 840919,fire Suppression Water Sys Placed in Degraded Mode of Operation to Support Sys Mod. Caused by Redundant Loop Flow Path Allowing Only One Fire Svc Sys Header to Remain in Svc.Loop Removed1984-10-0303 October 1984 Special Rept 84-04:on 840919,fire Suppression Water Sys Placed in Degraded Mode of Operation to Support Sys Mod. Caused by Redundant Loop Flow Path Allowing Only One Fire Svc Sys Header to Remain in Svc.Loop Removed 3F0784-16, Special Rept 84-03:on 840424,false Low & High Pressure Injection Occurred When Channel 2 Low Pressure Bistable Inadvertently Actuated.Cause Not Stated.Bistable Replaced. Plant Stabilized W/Injection of Borated Water Into RCS1984-07-23023 July 1984 Special Rept 84-03:on 840424,false Low & High Pressure Injection Occurred When Channel 2 Low Pressure Bistable Inadvertently Actuated.Cause Not Stated.Bistable Replaced. Plant Stabilized W/Injection of Borated Water Into RCS 3F0684-09, Special Rept 84-02:on 840312,engineered Safeguards High Pressure Injection Initiated.Caused by Spurious Actuation of Channel 2 Train B.Equipment Replaced & Borated Water Injected1984-06-13013 June 1984 Special Rept 84-02:on 840312,engineered Safeguards High Pressure Injection Initiated.Caused by Spurious Actuation of Channel 2 Train B.Equipment Replaced & Borated Water Injected 3F0184-22, RO Special Rept 84-01:on 840114,leak Found in Fire Suppression Water Sys,Rendering Sys Inoperable.Caused by Compliance W/Tech Spec Limiting Condition for Operation.Sys Returned to Operable Status on 8401151984-01-23023 January 1984 RO Special Rept 84-01:on 840114,leak Found in Fire Suppression Water Sys,Rendering Sys Inoperable.Caused by Compliance W/Tech Spec Limiting Condition for Operation.Sys Returned to Operable Status on 840115 3F1283-06, RO 83-050:on 830719,mode Ascension Occurred (Mode 5 to 4) Prior to Completing Required Surveillance.Occurrence Analysis Continuing.Ler Will Be Submitted by 8312221983-12-0505 December 1983 RO 83-050:on 830719,mode Ascension Occurred (Mode 5 to 4) Prior to Completing Required Surveillance.Occurrence Analysis Continuing.Ler Will Be Submitted by 831222 1999-03-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G0191999-10-15015 October 1999 Safety Evaluation Concluding That Licensee Followed Analytical Methods Provided in GL 90-05.Grants Relief Until Next Refueling Outage,Scheduled to Start on 991001.Temporary non-Code Repair Must Then Be Replaced with Code Repair 3F1099-19, Part 21 Rept Re Damage on safety-grade Cable Provided to FPC by Bicc Brand-Rex Co.Damage Was Created During Cabling Process While Combining Three Conducters.Corrective Action Program Precursor Card PC99-2868 Was Initiated1999-10-13013 October 1999 Part 21 Rept Re Damage on safety-grade Cable Provided to FPC by Bicc Brand-Rex Co.Damage Was Created During Cabling Process While Combining Three Conducters.Corrective Action Program Precursor Card PC99-2868 Was Initiated ML20217B0931999-10-0606 October 1999 Part 21 Rept Re Damaged Safety Grade Electrical Cabling Found in Supply on 990831.Damage Created During Cabling Process While Combining Three Conductors Just Prior to Closing.Vendor Notified of Reporting of Issue ML20212L0881999-10-0404 October 1999 SER Accepting Licensee Requests for Relief 98-012 to 98-018 Related to Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp for Crystal River Unit 3 ML20212J8631999-10-0101 October 1999 Safety Evaluation Supporting Licensee Proposed Alternatives to Provide Reasonable Assurance of Structural Integrity of Subject Welds & Provide Acceptable Level of Quality & Safety.Relief Granted Per 10CFR50.55a(g)(6)(i) ML20212E9031999-09-30030 September 1999 FPC Crystal River Unit 3 Plant Reference Simulator Four Year Simulator Certification Rept Sept 1995-Sept 1999 3F1099-02, Monthly Operating Rept for Sept 1999 for Crystal River,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Crystal River,Unit 3.With ML20212E6911999-09-21021 September 1999 Safety Evaluation Supporting Proposed EALs Changes for Plant Unit 3.Changes Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML20211L1321999-08-31031 August 1999 EAL Basis Document 3F0999-02, Monthly Operating Rept for Aug 1999 for Crystal River,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Crystal River,Unit 3.With ML20212C1501999-08-31031 August 1999 Non-proprietary Version of Rev 0 to Crystal River Unit 3 Enhanced Spent Fuel Storage Engineering Input to LAR Number 239 ML20211B7291999-08-16016 August 1999 Rev 2 to Cycle 11 Colr ML20210P1111999-08-0505 August 1999 SER Accepting Evaluation of Third 10-year Interval Inservice Insp Program Requests for Relief for Plant,Unit 3 ML20210U5341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Crystal River,Unit 3 ML20209F5601999-07-31031 July 1999 EAL Basis Document, for Jul 1999 3F0799-01, Monthly Operating Rept for June 1999 for Crystal River,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Crystal River,Unit 3.With ML20210U5411999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Crystal River,Unit 3 3F0699-07, Monthly Operating Rept for May 1999 for Crystal River,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Crystal River,Unit 3.With ML20210U5601999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Crystal River,Unit 3 ML20195C6271999-05-28028 May 1999 Non-proprietary Rev 0 to Addendum to Topical Rept BAW-2346P, CR-3 Plant Specific MSLB Leak Rates ML20196L2031999-05-19019 May 1999 Non-proprietary Rev 0 to BAW-2346NP, Alternate Repair Criteria for Tube End Cracking in Tube-to-Tubesheet Roll Joint of Once-Through Sgs 3F0599-04, Monthly Operating Rept for Apr 1999 for Crystal River Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Crystal River Unit 3.With ML20210U5631999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Crystal River,Unit 3 3F0499-04, Monthly Operating Rept for Mar 1999 for Crystal River Unit 3.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Crystal River Unit 3.With ML20204D9661999-03-31031 March 1999 Non-proprietary Rev 1,Addendum a to BAW-2342, OTSG Repair Roll Qualification Rept 3F0399-04, Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease1999-03-10010 March 1999 Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease 3F0399-03, Monthly Operating Rept for Feb 1999 for Crystal River Unit 3.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Crystal River Unit 3.With ML20203A4381999-02-0303 February 1999 Safety Evaluation Supporting EAL Changes for License DPR-72, Per 10CFR50.47(b)(4) & App E to 10CFR50 ML20206E9891998-12-31031 December 1998 Kissimmee Utility Authority 1998 Annual Rept ML20206E9021998-12-31031 December 1998 Florida Progress Corp 1998 Annual Rept ML20206E9701998-12-31031 December 1998 Ouc 1998 Annual Rept. with Financial Statements from Seminole Electric Cooperative,Inc 3F0199-05, Monthly Operating Rept for Dec 1998 for Crystal River Unit 3.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Crystal River Unit 3.With ML20206E9261998-12-31031 December 1998 Gainesville Regional Utilities 1998 Annual Rept 3F1298-13, Monthly Operating Rept for Nov 1998 for Crystal River,Unit 3.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Crystal River,Unit 3.With 3F1198-05, Monthly Operating Rept for Oct 1998 for Crystal River,Unit 3.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Crystal River,Unit 3.With ML20155F4071998-10-31031 October 1998 Rev 2 to Pressure/Temp Limits Rept ML20155J2701998-10-28028 October 1998 Second Ten-Year Insp Interval Closeout Summary Rept 3F1098-06, Monthly Operating Rept for Sept 1998 for Crystal River Unit 3.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Crystal River Unit 3.With ML20206E9461998-09-30030 September 1998 Utilities Commission City of New Smyrna Beach,Fl Comprehensive Annual Financial Rept Sept 30,1998 & 1997 ML20206E9561998-09-30030 September 1998 City of Ocala Comprehensive Annual Financial Rept for Yr Ended 980930 ML20206E9101998-09-30030 September 1998 City of Bushnell Fl Comprehensive Annual Financial Rept for Fiscal Yr Ended 980930 ML20206E9811998-09-30030 September 1998 City of Tallahassee,Fl Comprehensive Annual Financial Rept for Yr Ended 980930 ML20195E3121998-09-30030 September 1998 Comprehensive Annual Financial Rept for City of Leesburg,Fl Fiscal Yr Ended 980930 3F0998-07, Monthly Operating Rept for Aug 1998 for Crystal River Unit 3.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Crystal River Unit 3.With ML20236W6501998-07-31031 July 1998 Emergency Action Level Basis Document 3F0898-02, Monthly Operating Rept for Jul 1998 for Crystal River,Unit 11998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Crystal River,Unit 1 ML20236V8801998-07-30030 July 1998 Control Room Habitability Rept 3F0798-01, Monthly Operating Rept for June 1998 for Crystal River Unit 31998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Crystal River Unit 3 ML20236Q4611998-06-30030 June 1998 SER for Crystal River Power Station,Unit 3,individual Plant Exam (Ipe).Concludes That Plant IPE Complete Re Info Requested by GL 88-20 & IPE Results Reasonable Given Plant Design,Operation & History 3F0698-02, Monthly Operating Rept for May 1998 for Crystal River Unit 31998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Crystal River Unit 3 1999-09-30
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October 3, 1983 3F-1083-01 Regional Administrator, Region II Attention: R. C. Lewis, Director Division of Project and Resident Programs U.S. Nuclear Regulatory Commission 101 Marietta Street, N.W., Suite 2900 Atlanta, GA 30303
Subject:
Crystal River Unit 3 Docket No. 50-302 Operating License No. DPR-72 Licensee Event Report No.83-023 Gentlemen:
Florida Power Corporation (FPC) offers the following responses to your letter of August 17, 1983, concerning fire damper discrepancies at Crystal River Unit 3 (CR-3).
Item 1: Provision of sufficient justification to assure that no additional design and construction deviations exist on the fire protection systems and features provided for the safety-related areas of the plant.
Response 1: Since January 1,1971, thirty-seven (37) separate audits /
inspections of the CR-3 fire protection systems and features have been performed. Sixteen (16) of these inspections were performed by the Nuclear Energy Property Insurance Association (NEPIA); nine (9) inspections were performed by the NRC; five (5) inspections by an outside fire protection consultant, Professional Loss Control l (PLC); and seven (7) inspections by American Nuclear Insurers (ANI). These inspections / audits did not reveal any generic design deviations in the CR-3 fire protection l systems and features. A chronology of CR-3 fire inspec-tions/ audits is provided in Attachment 1. Summaries of the NRC and PLC inspection / audit reports are provided in Attachment 2. ,
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General Office 3201 Thirty-lourth Street South e P.O. Box 14o42, St. Petersburo. Florda 33733 e 813-866- g/
l R. C. Lewis October 3, 1983 J Page 2 During construction, Gilbert Associates drawings were sent to NEPIA for review and approval. No generic deviations in the CR-3 fire protection systems and features were identi-fied by this design review. In addition NUS Corporation performed two reviews of the CR-3 fire protection systems and features (1976 and 1977) and identified no generic deviations in the CR-3 fire protection systems- and features.
As a result of the discrepancy identified on June 13, 1983, FPC personnel have conducted an investigation and walkdown which resulted in the additional discrepancies described in LER No.83-023.
New fire protection systems and features are being designed by qualified fire protection engineers as a result of 10 CFR Part 50 Appendix R modifications to protect safe shut down systems. The new fire protection systems and features will add to or completely replace existing systems, thus lessening the probability that any generic design devia-tions exist at CR-3.
Proposals are being reviewed in-house to commission a new Fire Protection Program Review by a consultant independent of the one who performed the original review to assure FPC that no generic design or installation deviations exist in the CR-3 fire protection systems and features and to comply with the applicable provisions of Appendix R.
Item 2: Performance of sufficient quality assurance audits of your architectural and engineering organizations to assure that adequate design control is provided in the area of fire protection.
Response ~2: Gilbert Associates was the original plant design agent and has been the primary engineering firm used for the design of backfit modifications, including any related to fire protection. The only design work related to fire protec-tion not performed by GAI are as follows:
a) NUS: During preparation of FPC's response to the July 27, 1979 Fire Safety Evaluation Report (SER), NUS designed some fi re stops. This basically took approved methods and applied them to plant specific areas. NUS also designed the Lube Oil Collection System for Reactor Coolant Pump- Motors completed during Refuel IV.
R. C. Lewis October 3, 1983 Page 3 b) Professional Loss Control (PLC): During SER response preparation PLC provided locations for fire detec-tors. GAI performed engineering to implement PLC recommendation.
c) Stone & Webster: Presently working on several Appendix R tests.
FPC internal engineering organizations have not performed design changes to fire protection systems without the assistance of Gilbert Associates. A recent fire protection audit by FPC Quality Programs has identified a weakness in the FPC overall Design Control Program with respect to design changes not classified as safety-related. Interim corrective actions have been taken to assure these design changes consider fire protection adequately. There is no indication that this item has caused any condition that could be a concern from a fire protection perspective. The Fire Protection Program Review identi fied in response 1 above will assure no adverse conditions exist.
The Florida Power Corporation Quality Programs includes requirements for a yearly vendor evaluation to assure their overall corporate quality program meets the requirements of 10CFR50 Appendix B and other FPC regulatory commitments on design. In addition, an annual audit is performed of the CR-3 specific design control program to assure that an effective design control process is in place. This audit is essentially based on ANSI-N45.2.11-1974. Although these audits have not specifically addressed fire protection, fire protection is a design criteria identified to be con-sidered. The process is designed to assure the require-ments for design control are established. The audit assesses the effectiveness of the process. Fire protection criteria are part of the design process just as seismic, environmental, etc. No major findings which could have significantly degraded the program have been made.
In addition, an audit was performed in early September to verify the consideration of fire protection criteria in designs and to evaluate the design process as applied to the design and modifications of fire systems. Fire systems are classified non-safety related and are not subject to a full 10CFR50 Appendix B program. A design control process does exist however that ensures appropriate review of these design drawings.
R. C. Lewis October 3, 1983 Page 4 Based on the above work already performed, FPC believes that the Fire Protection Program at CR-3 is adequate. Continued design verification will be ensured by the new Fire Protection Program Review and quality assuranca audits.
If you have any questions or would desire to meet with us, please contact this office.
Sincerely, y
G. R. Westafer Manager, Nuclear Operations Licensing and Fuel Management Westafer(W01)C5-1 Attachments
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ATTACHMENT 1 CHRONOLOGY OF CR-3 FIRE INSPECTIONS ANI NEPIA NRC PLC Feb. 18, 1971 Sept. 22, 1971 Dec. 10, 1971 Dec. 14-15, 1972 Apr. 30 - May 1, 1973 Aug. 16,27,28, 1973 Dec. 19-20, 1973 Apr. 3-5, 1974 Aug. 1-2, 1974
. Nov. 18-19, 1974 Mar. 25-26,1975 June 26, 1975 Sept. 29-30, 1975 Sept. 29 - Oct.1,1975 Dec. 1, 1975 Mar. 15, 17, 1976 June 23-24,1976 July 20-22 & Aug. 2-5,1977 Dec. 5-9,1977 & Jan.11-12,1978 Apr. 3-6, 1978 April 17-21,1978 Oct. 2-6, 1978 Nov. 28 - Dec.1,1978 Mar. 27-28, 1979 Apr. 9-13, 1979 May 24-26, 1979 Mar. 17-20, 1980 May 26-28, 1980 1
! Nov. 17-20, 1980 Dec. 2-5, 1980 l Mar. 2-4, 1981 May 4-7,1981 Nov. 16-20, 1981 Nov. 17-20, 1981 June 14-16, 1981 Aug. 9-12, 1982 May 3-5,1983 l
Thompson (Attl)ND117
.. . ATTACHMENT 2 PROFESSIONAL LOSS CONTROL (PLC) FIRE AUDIT SUMMARIES
- 1. " April 1978" - PLC - Annual Fire Protection Inspection Section 2.1 Inspection of Plant Facilities
... an inspection of plant safety related areas was conducted. The emphasis of this inspection was an assessment of the effectiveness of the plant's Fire Protection Program to control fire hazards and maintain fire protection equipment in these areas."
- 2. April 1979 - Annual Fire Audit The plant audit included general inspections of installed fire supression, fire detection and alarm systems.
- 3. May 1980 - Triennial Audit 1.0 Introduction "The inspection consisted of a review of the plant Safety Evalu-ation Report, review of procedures relating to fire protection, review of fire brigade organization and training, and an on-site inspection of all plant facilities."
- 4. March 1981 - Annual Fire Audit The inspection consisted of a review of the plant Fire Hazards Analysis and comparison to APCS BTP 9.5-1 Appendix A, review of procedures related to fire protection, revi ew of fire brigade organization and training, and on-site inspection of plant facili-ties.
- 5. " June 1982" - Fire Protection Audit Section 3.3 Fire Protection Systems and Equipment "The plant audit included general inspection of the installed water supply and distribution system, fire detection and alarm systems, and fire suppression system."
l Schmiedel(Inspect)DN6-2 Attachment 2 (Cont'd)
NRC FIRE INSPECTION REPORT / AUDIT SUMMARIES
- 1. September 29 - October 1,1975 (Report No. 75-14): This special inspection was made to inspect the fire prevention and fire protection type activities relating to construction, testing and start-up and early plans for these activities during operation of the plant.
During a walk-through inspection of the plant, attention was directed to the fire protection equipment.
No substantive deficiencies were identified in this inspection of the fire prevention and fire protection activities.
- 2. July 20-22 and August 2-5,1977 (Report - No. 77-13): The plant was toured to inspect rafety-related areas; examine portions of the fire system; and observe activities related to fire protection.
- 3. December 5-9, 1977 and January 11-12,1978 (Report No. 77-24): Inspection included a discussion with licensee personnel regarding the FPC response to the NRC BTP on Fire Protection.
- 4. April 3-6,1978 (Report No. 78-08): The inspector reviewed certain Admini-strative Procedures, Surveillance Procedures, Maintenance Procedures, held discussions with the licensee, and toured certain portions of the plant to determine the status of the fire prevention and protection system. No items of noncompliance or deviations were observed.
The inspector toured various areas of the plant to observe the following:
- a. Plant cleanliness
-b. Fuel inspection in the Fuel Storage Building
- c. Operating activities in the Reactor Building
- d. Fire detection and fire protection systems in various portions of the plant which included the control room, cable spreading room and auxiliary building.
No items of noncompliance or deviations were found.
- 5. October 2-6, 1978 (Report No. 78-24): The inspectors conducted a preliminary fire protection survey of the plant in preparation for the NRC. Fire Team Site Visit in November 1978.
"The inspector reviewed the results of the latest fire insurance inspection which was conducted on April 17-21, 1978."
"The inspector toured various areas of the facility to observe. .. fire protection / prevention systems and conditions."
6.- November 28 - December 1, 1978: NRC Fire Team Site Visit to review the fire protection program. Revised their list of questions as a -result of their visit. Performed extensive review of site physical fire protection features.
o, Attachment 2 (Cont'd)
- 7. ' March 27-28,1979. (NRC Fire Team Site Visit): Reviewed some areas of the plant in detail and discussed the draft of the SER for CR-3.
8.- December 2-5, 1980 (Report No. 80-40): The plant was toured to:
A. Review the progress and action on the fire protection commitments made-to the NRC.
B. Assure that the fire protection systems required by Technical Specifica-tion were in service.
C. Evaluate the effectiveness of the implementation of the fire protection administrative control procedures.
- 9. November 17-20, 1981 (Report No. 81-25): A tour of the plant was made by the inspector to review the fire protection modifications of the detection _ system and reactor _ building standpipe and to review the general fire protection features provided for the plant.
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