ML20080A269
| ML20080A269 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 11/30/1983 |
| From: | Alden W, Cooney M PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| NUDOCS 8402030432 | |
| Download: ML20080A269 (3) | |
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- n. g UNIT SHUTDOWNS AND PONER REDUCTIONS DOCKET NO. 50 - 27d UNIT N AME PEACH UOTTOM UNIT 3 DATE DECEMBER 15,1983 REPORT MONTH N OV EM B ER, 1983 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY W.M.ALDEN ENGINEEL-IN-CHAkGE LICENSING SECTION GENERATION DIVISION-NUCLEAR TELEPHONE (215) 841-5022
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l METHOD OF l LICENSEE l SYSTEM l COMPONENT l CAUSE AND CORRECTIVE l
l TYPE l DURATION l REASON l SHUTTING DONNl EVENT l CODE I CODE I ACTION TO NO.l D AT E l (1) l (HOU RS) l (2) l REACTOR (3) l REPORT 8 l
(4) l (5) i PREVENT. RECURRENCE l
1 1
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11 l 831101 l S I 000.0 l
11 l 4
l NA l HC l ZZZZZZ l ROD PATTERN ADJUSTMENT.
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l 12 l 831111 l S l 000.0 l
H l
4 l
NA l
RC l ZZZZZZ l ROD PATTERN ADJUSTMENT.
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l 1
1 I
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1 j
13 l 831117 l S l 064.0 l
b l 3*
I NA I CC l VALVEI. l REPLACEMENT OF 71E RELIEF VALVE.*
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l 1
1 1
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l 13 l 831117 l P l 045.0 i
B l 3*
l NA I CC l VALVEX l REPLACEMENT OF 71E RELIEF VALVE.*
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1 I
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1 14 l 831124 l S I 000.0 I
h 1 4
l NA l RC l ZZZZZZ l ROD PATTERN ADJUSTMENT.
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l 109.0 l
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l o-DURING Tl!IS 5HUTDOWN, AT 16.5 PERCENT PONER, AN AUTOMATIC 3 CHAM OCCURRED ON HIGH WATER LEVEL IN Tile SCRAM DISCHARGE INSTRUMENT VOLUME AS A RESULT OF RAPID MANUAL SCRAMMING OF INDIVIDUAL CONTROL RODS.
(1)
(2)
(3)
(4)
F - FO!!C ED REASON METHOD EIHIBIT G - INSTRUCTIONS S - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANCAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE C - REFUELINC 3 - AUTOMATIC SCRAM.
EVENT REPORT (LEh)
D - REGULATORY N ESTRICT ION 4 - OTHER (EIPLAIN)
FILE (NUhEG-0161)
E - OPER ATOR TH AINING + LICENSE El&MINATION P-ADMINI STR ATI V E (5)
G - OPERATION AL ERROR (EXPLAIN)
H - OTHER (EXPLAIN)
EXI!IBIT I - SAME SOHECE 1
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/ 1 hr'(
^ 8402030432 B31130 i
PLR ADOCK O$000277 R
PENT l
4
t' Docket Nos. 50-277 50-278
}
Attachment to Monthly Operating Report for November, 1983 PEACH BOTTOM ATOMIC POWER STATION NAREATIVE SUPTARY OF OPERATING EXPERIENCES November, 1983 Unit 2 Unit 2 remained shutdown for the entire month of November for inspection of primary system piping welds and the application of weld repairs on the reactor recirculation system and shutdown cooling system.
On November 2, the E-1 diesel generator was out-of-service for repair of an oil leak.
On November 15, an unusual event was declared when a ventilation stack radioactive release of 31 of Tech Specs occurred.
The release occurred as a result of fuel pin puncturing work by General Electric in the f ue3 pool.
A previous occurrence on Unit 3 had resulted in a change to the procedures which resulted in some reduction in the release.
All such work has been halted until a signi ficantly better method can be found.
On November 25, Unit 2 Reactor Hydrostatic Testing was performed.
The unit ended the report period with final preparations for startup.
NRC authorization for plant restart was issued on November 30th.
Unit 3 The unit began the month at full power.
Reactor power was reduced to 770 MWe on November 1 for a control - rod adjustment.
The unit was returned to full power on November 3.
On November 10, the 3C main steam line radiation monitor failed causing a half scram and a half Group I isolation; the radiation monitor was returned to service that same morning.
Reactor power was reduced to 650 MWe on November 11 for a control rod adjustment.
The unit was returned to full power on November.13.
RCIC was taken out-of-service on November 14 to. repair the turbine trip / throttle valve and returned to service three days later.
On November 17, the unit was shut down for replacement of 71E main steam line relief valve due to acoustic leak indication.
During this shutdown, at 16.5 per cent power, an automatic scram occurred on high water level in the scram discharge instrument volume as a result of rapid manual scrarming of individual control rods.
The relief valve was replaced and startup began on November 20.
Reactor power was reduced to 600 MWe on November 24 for a control _ rod adjustment.
The unit achieved full power on November 26.
PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET P.O. BOX 8699 PHILADELPHIA. PA.19101 (2151841-4000 January 5, 1984 Docket Nos. 50-277/50-278 Director Office of Inspection & Enforcement US Nuclear Regulatory Comission Washington, DC 20555 Attention: Document Control Desk
Subject:
Peach Bottom Atomic Power Station Monthly Operating Report Gentlemen:
Attached are twelve copies of two revised pages to the Monthly
- Operating Report for Peach Bottom Units 2 and 3 for the month of November, 1983 previously forwarded to you by. letter dated December 15, 1983. Rese pages provide additional information relative to the Unit 3 November 17, 1983, outage. H e changes are identified by a vertical bar in the page margin.
Very truly yours, perintendent clear Generation Division Attachment cc: Dr. T. E. Murley, NRC Mr. A. R. Bicugh, NRC Site Inspector Mr. Stan P. Mangi, Dept. of Envir. Resources Mr. P. A. Ross, NRC INFO Records Center V
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