ML20078H693

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Monthly Operating Rept for Sept 1983
ML20078H693
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 10/04/1983
From: Fields D, Graham D
FLORIDA POWER CORP.
To:
Shared Package
ML20078H630 List:
References
NUDOCS 8310140268
Download: ML20078H693 (4)


Text

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AVERAGE DAILY UNIT POWER LEVEL

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j DOCKET NO. 50-302 UNIT FLCRP-3 DATE 10/4/83 COMPLETED BY D. Graham TELEPHONE (904) 795-6486 MONTH September 1983 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 605 17 610' 2 612 18 618 606 3 39 g99 4 605 20 606 5 608 21 613 6

580 612 22 7 23 640 8 609 24 . 635 625 579 9 25 10 26 624 294 594

. II 27 12 28 608 590 13 29 563 609 560 14 30 15 31 16 602 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77) 8310140268 831011 PDR ADOCK 05000302 R PDR

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OPERATING DATA REPORT k DOCKET NO. 50-302 DATE 10/3/83 COMPLETED BY' D. Graham TELEPHONE (on6T 79s-6486 OPERATING STAT 13S Crystal River Unit #3 Notes

1. Unit Name:
2. Reporting Period: 9/1/83 - 9/30/83
3. Licensed Thermal Power (MWt): 2544
4. Nameplate Rating (Gross MWe): 890
5. Design Electrical Rating (Net MWe): 825
6. Maximum Dependable Capacity (Gross MWe): 850
7. Maximum Dependable Capacity (Net MWe): 811
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

N/A

9. Power Level To which Restricted,If Any (Net MWe): 608 MW
10. Reasons For Restrictions,1f Any: RCP-lC seal is bad.

, t This Month .Yr.-to-Date Cumulative 4

11. Hours In Reporting Period 720 6551 57431
12. Number Of Hours Reactor Was Critical 715.6 3457.6 35664.8
13. Reactor Reserve Shutdown Hours 0 0 1280.3 l

l 14. Hours Generator On.Line 710.6 3382.5 34849.4

15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 1319506 7212345 77737300 .
17. Gross Electrical Energy Generated (MWH) 449117 2479513 26446130
18. Net Electrical Energy Generated (MWH) 427638 __. 2360228 25105108
19. Unit Service Factor 98.7%. 51.6% 60.7%
20. Unit Availability Factor 98.7% 51.6% 60.7%
21. Unit Capacity Factor (Using MDC Net) - 73.2% 44.4% 55.4%
22. Unit Capacity Factor (Using DER Net) 72.0% 43.7% 53.0%

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23. Unit Forced Outage Rate 1.37 2.0% 24.2%
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each):

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25. If Shut Down At End Of Report Period. Estimated Date of Startup: 10/14/83 -
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved '

INITIAL CRITICALITY 1/14477.

. INITIAL ELECTRICITY 1/30/77-COMMERCIAL OPER ATION 3/13/77 (4/77) ,

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DOCKET NO. sn-an?

UNIT SHUTDOWNS AND POWER REDUCIlONS UNIT NAME FLCRP-3 DATE in/1/n1 COMPLETED BY D. Fields REPORT MONTil 9/g3 TELEPHONE (904) 795-64R6

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, 5E 3 y .Y 3 Licensee ,E*, 1, j3 Cause & Currective No. Date g gg s jg5 Event gg gu Action to I-dE 5 3ge e

Report # mO u

o Prevent Recurrence

.' 6 83-19 830906 F 36 A N/A N/A IIC llTEXCll Reduced power to locate leak in conden-ser waterbox D.

83-20 830911 S 9.1 B 1 N/A CB MOTORX Shutdown to add oil to A RCP motor.

83-21 830911 S 13 B N/A N/A IIC llTEXCil Reduced power to clean B waterbox.

83-22 830912 S 19 B N/A N/A IIC IITEXCII Reduced power to clean C waterbox.

83-23 830913 S 34 B N/A N/A IIC llTEXCll Reduced power to clean D waterbox.

83-24 830913 S 15 B- N/A N/A IIC IITEXCil Reduced power to clean A wate'rbox.

83-25 830927 F 63 A N/A N/A IIC llTEXCil Reduced power to locate condenser seawater leak in A waterbox.

83-26 830930 S .3 B 1 N/A CB PUMPXX Shutdown to replace seal packages in B and C RC pumps.

I 2 3 4 F: Forced Reason: Method: Exhibit G . instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event ReporI (LER) File (NUREG-D-Regulatory Restriction 4-Other ( Explain) 0161)

E-Operator Training & License Examination F Administrative 5 G-Operational Error (Explain) Exhibit I - Same Source 19/77) ll-0t her (Explain)

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4.

MONTHLY OPERATIONAL

SUMMARY

STATEMENT DOCKET NO. 50-302 UNIT FLCRp-3 DATE 10/3/83 COMPLETED BY D. Fields TELEPHONE (904) 795-6486 MONTH September,1983

SUMMARY

STATEMENT! The unit operated at reduced power the entire month with reactor coolant pump 1C secured. The plant was shutdown on September 30 for an estimated 2 week outage to replace the C and the B reactor coolant pump seals. Condenser tube leaks continue to be a problem with over 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> at a 30 MW electric power reduction to locate and repair 1

the leaks.

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