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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARNPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable NPL-97-0831, Special Rept:On 971201,fire Protection Wrap Required for Svc Water Pump Motor Cables Had Been Rendered Inoperable for More than Seven Days.Caused by Planned Repair activity.Once- per-hour Fire Patrol Established1997-12-23023 December 1997 Special Rept:On 971201,fire Protection Wrap Required for Svc Water Pump Motor Cables Had Been Rendered Inoperable for More than Seven Days.Caused by Planned Repair activity.Once- per-hour Fire Patrol Established NPL-97-0751, Special Rept:On 971023,low Temp Overpressure Protection Sys Operation Occurred.Caused by Starting Reactor Coolant Pump w/water-solid Reactor Coolant Sys.Operating Personnel Will Be Briefed on Event1997-11-21021 November 1997 Special Rept:On 971023,low Temp Overpressure Protection Sys Operation Occurred.Caused by Starting Reactor Coolant Pump w/water-solid Reactor Coolant Sys.Operating Personnel Will Be Briefed on Event NPL-97-0287, Special Rept:On 970421,fire Door 106A in DG Bldg,Separating Mechanical Equipment Room from Unit 2,B-train,4KV Switchgear Room,Found in Open Position (Closed But Not Latched)1997-05-21021 May 1997 Special Rept:On 970421,fire Door 106A in DG Bldg,Separating Mechanical Equipment Room from Unit 2,B-train,4KV Switchgear Room,Found in Open Position (Closed But Not Latched) ML20132E0681996-12-17017 December 1996 Ro:On 961114,declared Noble Gas Monitor Inoperable.Caused by Necessary Addl Repairs on Failed Pump & Subsequent re- Testing of Sys.Will Repair P-707A Pump & Perform in-service Test by 961220 ML20080P9591995-03-0303 March 1995 Special Rept:On 950207,control Rod H8 in Control Bank B Dropped.Investigation Revealed No Abnormal Conditions. Decision Was Made to Recover Dropped Rod ML20099B9551992-07-29029 July 1992 Ro:Fire Penetration Seal Degraded & Inoperable for More than 7 Days.Caused by Voids in Seal Structure.Hourly Fire Watch Established & Mod to Seal Completed on 920720 ML20195B7271988-10-26026 October 1988 Special Rept:On 880831,emergency Diesel Generator Unexpectedly Returned to Full Speed & Voltage Condition. on 880929 & 1012,event Recurred.Exact Cause Not Determined. Addl Testing Planned Over Next 90 Days to Pinpoint Cause ML20072U4281983-03-30030 March 1983 Ro:On 830308,turbine Trip & Subsequent Reactor Trip Experienced.Caused by Bumping of Main Steam Stop Valve Relay by Contractor Employee While Working on Control Panel. Cleanup Flow Maintained.On 830306,I-131 Limit Exceeded ML20087L1071975-02-0404 February 1975 Telecopy Ro:On 750203,Nuclear Fuel Svcs Spent Fuel Shipping Cask 4B Received & Found in Excess of 22,000 Disintegrations Per Minute 100 Centimeters Squared Removable Contamination on Cask Surface ML20087L1121975-02-0404 February 1975 RO 75-2:on 750224,test of Containment Purge Inlet & Exhaust Valves Closing Time Disclosed That Valves 1CV-3212 & 1CV-3244 Exceeded 3-5 Min Closing Time.Caused by Sticking Pneumatic Relays in Valve Air Operators ML20087L1881975-01-24024 January 1975 Ro:On 741219,discovered That One Insp of Station Batteries Not Completed within Prescribed 30 Day Frequency or within Allowable 25% Grace Period.Caused by Scheduling Difficulty Due to New Supervisor ML20087L6331974-02-0606 February 1974 Ro:On 740102,during Quarterly Functional Testing of Emergency Diesel Backup Relays 4D,fast Start Backup Relays SFB1 & SFB2 Would Not Perform Intended Function.Caused by Neoprene Bellows in Timing Chamber ML20085M3951973-10-29029 October 1973 Ro:Describing Possible Backseating Disc Mislocation Problem on 2-inch Darling Valves on S-350 Wdd Welding End.Valves Repaired.Valve Stems Will Be Changed During Next Refueling Outage ML20087L6351973-05-14014 May 1973 Ro:On 730303 & 0426,test of Undervoltage Relays of 1A01 & 1A02 Nonsafeguards Bus Undervoltage Relays Disclosed Three Out of Four Malfunctional.Caused by Setting of Shaft in Guide Bearing.Relays Removed & Returned to Vendor for Exam ML20087L6551973-03-0909 March 1973 Ro:On 730208,during Performance of Functional Test on Purge Valves,Two Containment Purge Inlet Valves Open When Placing Manual Switch to Open Position But Did Not Close.Caused by Loose Screw on Switch.Mod Made to Valve Circuits 1998-03-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
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Mscomun Electnc mcwm 231 W. MICHIGAN, P.O. BOK 2046, MILWAUKEE, WI 53201 March 30, 1983 Mr. J. G. Keppler, Regional Administrator Office of Inspection and Enforcement, i
Region III U. S. NUCLEAR REGULATORY COMMISSION 799 Roosevelt Road Glen Ellyn, Illinois 60137
Dear Mr. Keppler:
DOCKET NO. 50-266 REACTOR COOLANT ACTIVITY LIMITATIONS POINT BEACH NUCLEAR PLANT, UNIT 1 This letter serves as notification of a reportable occurrence at Point Beach Nuclear Plant, Unit 1, in accordance with the Confirmatory Order of November 30, 1979, as modified.
At 1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br /> on March 8, 1983, Unit 1 experienced a turbine trip and a subsequent reactor trip. The trip was apparently caused by the bumping of a Unit 1 main steam stop valve relay by a contractor employee while working on a control panel; this sent a trip signal to the turbino. This event was reported via the Emergency Notification System as required by 10 CFR 50.72. A reactor coolant sample was obtained and analyzed at 1318 hours0.0153 days <br />0.366 hours <br />0.00218 weeks <br />5.01499e-4 months <br /> on March 8. Specific activity was found to be 0.907 pCi/g dose equivalent I-131, which is less than the 1.0 pCi/g dose equivalent i I-131 limitation set forth in paragraph IV.2 of the Confirmatory Order. It was later verified that, according to our administrative procedure for fulfilling the sampling requirements of the Confirmatory Order, the primary coolant sample must be taken between two and six hours after the trip occurred. The initial sample was taken less than two hours after the trip; therefore, another two samples were taken and analyzed at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br /> on March 8, meeting the time require-ments of the procedure. These samples showed an average specific activity of 1.47 pCi/g dose equivalent I-131. Per the procedure, samples were taken and analyzed in intervals of not greater than four hours until at 2240 hours0.0259 days <br />0.622 hours <br />0.0037 weeks <br />8.5232e-4 months <br /> on March 8 a sample taken showed a specific activity of 0.963 pCi/g dose equivalent I-131. Detailed results of the specific activity analysis obtained on March 8 are as follows:
. cif y
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F304110311 830330 PDR ADDCK 05000266 S PDR APR 4 g33
. - - - - _ - . =. . _ - -__ -
- Mr. J. G. Keppler -
2- March 30, 1983 Concentrations, pCi/g Isotope 1318 1640 1730 2126 2240 I-131 0.590 1.04* 1.01 0.747 0.706 I-132 0.448 0.477* 0.410 0.221 0.222 I-133 0.874 1.27* - 1.17 0.823 0.766 I-134 0.270 0.0508* 0.0566 0.206 0.276 I-135 0.730 0.866* 0.802 0.470 0.433 TOTAL 2.91 3.70* 3.45 2.47 2.41 Dose Equivalent I-131, pCi/g 0.907 1.47* 1.41 1.02 0.963 i
- Average of two samples taken at'this time.
Based on the times the first and last samples were taken,
' the specific activity of the primary coolant is conservatively-3 estimated to have exceeded 1.0 pCi/g dose equivalent I-131 for approximately 9-1/3 hours.
I On March 6, 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the time the first sample was taken in'which the 1.0 pCi/g dose equivalent I-131 limit was exceeded, the reactor was operated at 1169 MW thermal. power. Load was reduced to 926 MW thermal for approximately six hours on March 7 at the request of the Power Systems Supervisor. The load reduction commenced at approximately 0031 hours3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br />. At 0822 hours0.00951 days <br />0.228 hours <br />0.00136 weeks <br />3.12771e-4 months <br />, the unit was back'at 1169 MW thermal and remained there until the trip at 1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br /> on March 8. Reactor startup commenced later the same day at.1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br /> and at 2122 hours0.0246 days <br />0.589 hours <br />0.00351 weeks <br />8.07421e-4 months <br /> the reactor was'back at 1169 MW thermal.
Cleanup flow 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to finding the limit exceeded i consisted of a 35 gpm flow through the lithium hydroxide mixed bed demineralizer and then through the gas stripper. Cleanup l
i' -flow, including degassing, was maintained during the period of I the_ reactor trip and subsequent return to power. Cleanup flow was doubled to 70 gpm during reactor startup from approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> until 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on March 8.
e---W+m--T- + - - + --my ----+a - - . - em-g.-yy-- -+=.. - + , y- ,i. - - w -.re-v1 g. -yeyaes.-"w+-- g q-p,vwy 3y game-eg- y-3 wew,+yq-m,yy? re*yl---'---t*"ur.f+WS4ei*e-ty*$r---->'tgW+ 4N
Mr. J. G. Keppler March 30, 1983 As of March 1, the fuel burnup by core region was as follows:
Region Average Burnup, MWD /MTU 8A 19,916 10 33,356 11 25,945 12 18,625' 12A 10,053 13 11,299 13A 2,188 This occurrence is an example of icdine spiking following a power reduction or reactor trip. Similar occurrences have been observed frequently in pressurized water reactors in the past.
Westinghouse Topical Report WCAP-8637 dated November 1975 has presented a discussion and analysis of this phenomenon. Subsequent to this reactor trip and iodine spike, the Point Beach Unit 1 primary coolant activity has remained below the 1.0 pCi/g dose-equivalent I-131 limit.
Very truly yours,
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[$l'I' /
Vice President-Nuclear Power C. W. Fay
' Copy to NRC Resident Inspector