ML20066G496
| ML20066G496 | |
| Person / Time | |
|---|---|
| Site: | Fort Calhoun |
| Issue date: | 01/31/1991 |
| From: | Edwards M, Gates W OMAHA PUBLIC POWER DISTRICT |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| LIC-91-067R, LIC-91-67R, NUDOCS 9102190153 | |
| Download: ML20066G496 (7) | |
Text
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Omaha Public Power District 444 South 16th Street Mall Omaha Nebraska 68102-2247 402/636-2000 February 14, 1991 LIC-91 067R V. S. Nuclear _ Regulatory Commission Attn: Document Control Desk Mail Station PI-137 Washington, DC 20555
Reference:
Docket No. 50-285
' Gentlemen:
l
SUBJECT:
January Monthly Operating Report (MOR)
L Please find enclosed the January 1991 Monthly Operating Report for the Fort j..
Calhoun Station Unit No.1 as. required by Technical Specification Section l
5.9.1.
l L
If you should have any questions, please contact me.
Sincerely,
- p. 7I 2A
\\
W, G. Gates Division Manager Nuclear Operations
'WGG/sel Enclosures o
c:
LeBoeuf, Lamb,.Leiby & MacRae R. D. ' Martin, NRC Regional Administrator, Region IV P. P. Mullikin, NRC Senior Resident Inspector D.
K'. Sentell, Combustion Engineering R. J.-Simon, Westinghouse Office of Management &' Program Analysis (2)
INP0 Records Center l-American Nuclear Insurers 9102190153 910131 PDR ADOCK 05000285
/
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AVERAGE DAILY VNIT POWER LEVEL i
DOCKET NO.
50-285
'JNIT Fort Calhoun Station DATE February 6, 1991 COMPLETED BY M. L. EDWARDS TELEPHONE T402)636-2451 MONTH January 1991 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0
17 488 2-0 18 489 3-0 19 489 4
0 20 488 J
5 0
21 488 6
0 22-488 7
0 23 488 8
0~
24 488
=9 101 25 488 10 116 26 489 11 403 27 488 12 462 28 488
- 13 463-29 488 14 476 30 488 15 488 31 488 16-488-
' INSTRUCTIONS L
On this form,: list the average daily unit rower level in MWe-Net for each day in the reporting month.
Compute to the r.earest whole megawatt.
L l
l..
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OPERATING DATA REPORT DOCKET N0.
50-285 UNIT Fort Calhoun Station DATE February 6. 1991 COMPLETED BY M. L. EDWARDS TELEPHONE (402)336-2451 OPERATING STATUS 1.
Unit Name:
Fort Calhoun Station Notes 2.
Reporting Period:
January 1991 y
3.
Licensed Thermal Power (MWt):
1500
[
4.
Nameplate Rating (Gross MWe):
502
>A 5.
Design Electrical Rating (Net MWe): 478
{
6.
Maximum Dependable Capacity (Gross MWe):
502 7.
Maximum Dependable Capacity (Net MWe): - 478
- 8. 'If changes occur in Capacity Ratings (1 tem Numbers 3 through 7) Sin ~ce Last Report, Give Reasons:
N/A-9.
PowerLeveltoWhichRestricted,IfAny(NetMWe): N/A
- 10. Reasons for Restrictions, If Any: N/A This Month Yr-to-Date Cumulative
- 11.. Hours in Reporting Period 744.0 744.0 152.114.0
- 12. Number of Hours Reactor was Critical 564.0 564.0 117,352.7 13.. Reactor Reserve Shutt'.own Hours 0.0 0.0 1,309.5 14.
Hturs Generator On-Line 553.2 553.2 115,983.1
- 15. Unit Reserve Shutdown Hours 788,2*f!E~
788,242.8 152,071,732.1 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH)
- 17. Gross Electrical Ene if Generated (MWH)
-259,966.0 259,966.0 50 47,010,092.2
-18 ; Net Electrical. Energy Generated.(MWH) 247,636._9_
247,636.9
,732,413.2
'19.
Unit Service Factor 74.4 74.4 76.2
-20.
!! nit _ Availability Factor 74.4 74.4 76.2
.21.
UnitCapacityFactor(UsingMDCNet) 69.6 69.6 68.0
- 22. Unit Capacity Factor (Using DER Net)
___ 69.6-69.6 66.5
- 23. Unit Forced Outage Rate
.5.6 25.6 3.6 24.
Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
None-25,-
If Shut Down at End of Report Period, Estimated Date of Startup: N/A
- 26. Units In Test Status (Prior to Commercial Operation): Forcast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY N/A
~
COMMERCIAL OPERATION
-.-..~
~. -....
~* '
. Refueling Information-Fort Calhoun - Unit No.1 Report for the month ending January 1991 l'. - Scheduled date for' next refueling shutdown.
Seotember 1991
- 2.
Scheduled date for restart following-refueling.
November 1991
,3. -Will refueling or resumption of operation thereaf ter. require -a technical specification
. change or other license amendment?
.Y_es
_a..
If answer is yes, what, in' general, will these be?
1 Incorporate-specific requirements resulting
- from reload safety analysis.
~ b.
'-If answer is no, has the reload fuel design and core r.onfiguration' been reviewed 'by-your Plant Safety Review-Committee to determine whether
- ar.y unreviewed' safety questions'are associated with the core reload. '
N/A q
}fR c.
1f no such review has =taken place, when is-1
-~
it: scheduled?
N/A
- 4.-
Scheduled date(s)- for submitting. proposed licensing = action arid support information.
June 1991
. 5.
- Important-licensing consideration's associated Lwith refueling,~ e.g.,; new or different fuel Ldesignior supplier, unreviewed design ort 4
per'formance-analysis methods, significant-
' changes in fuel design, new operating procedures..
' New fuel supplier A
f New LOCA Analysis y
- 16. - The. number of fuel assemblies: a) in the core 133' Assemblies i
b) -in:the. spent fuel pool
. 477 Assemblies c)_ spent fuel-poolz storage
'-729...As sembl ies.
l capacity-d) planned spent fuel pool
'with higher density. spent Planned:to be::increasedt
, torage capacityv s
fuel; racks.
7.
The1 projected date of the last-refueling that can be-
- discharged to. the spent fuelipool assuming the present
-licensed : capacity. ~
1994*
- o
! Capability of full; core offload of 133 assemb7 'es lost.
- Prepared by' Y Date 2-s-9 r i
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DOCKET NO. 50-285-UNIT NAME Fort Calhoun Station.
DATE February 7, 1991 UNIT..SitUIDOWNS AND POWER REDUCTIONS-COMPLETED BY.. M.I _ Edwards TELEP110ME (4021 636-2451 REPORT HONill January 1991 E
c E
g7 gg
' Ucensee gI fg
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o
- Cause a Corrective No.
Date
~jg 5-Eg Event ge g g Action to R
') E gh fleport #
SEg g
Prevent Rectarence 5
90-08 901215 F-190.8 H
1 LER 90-028 XX PSX, AA On December 15, 1990, a through-wall feak on an installed spare Control Element Drive Mechanism (CEDM) pressure housing was identified and a.
s cooldown to cold shutdown was initiated.
The 'affected CEDM housing and a I
second installed spare housing were removed and replaced with blank flanges.
FCS was returned to service on January 8,
1991.
- See LER 90-028 for further muse and corrective ' actions.
1" ^
2 a
F-Forced Heatorr Method Exf*lt G - Instrvetion, S-Scheduled A-E<ripment failure (Explain) 1-Manual for Preparatien of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Ucensee C-Ilefuefno 3-Automatic Scram Event Report (1.ER) ne (NUREO-olet)
D-Regulatory Hestrictfen 4-Other (Explain)
.E-Operator Tralrdno a Ucense Examination 6
F-Administative Exteit 1 - Same Source G-Operational Erre St-other (Expfair.)
.-+
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+
5 N.
U 10MAHA PVBLIC POWER DISTRICT Fort Calhoun Station Unit No.-l r
y y.
~
January 1991 Monthly 0parating: Report l'.. OPERATIONS
SUMMARY
In-January, Fort Calhoun Station wasistarting 'up from cold shutdown
~i following repair of a Reactor Coolant System -(RCS) leak on the control element 1 drive mechanism (CEDM) housing.
During tne RCS hot hydrostatic test,.a pressurizer to code safety valve loop' seal _ inlet flange was found to be leaking.
The RCS was cooled down and depressurized for repairs to the flange.. The hydrostatic test performed during the following heat-up still showed some leakage on the flange but at an acceptable rate. Weekly L
monitoring of the leak was ' scheduled and continues to be performed.-
The reactor was taken critical and the generator 'placed on-line January 8, 1991.: A nominal-100% power was attained January 14,-1991. The scheduled monitoring ofmthe' flange leak on January 17 showed the leak had increased, j
Furmanite was used to seal the leakage area and this decreased the leak rateLto approximately one drip per minute.
JThe1following NRC inspections took place in January:
[
IR_90-45 MonthlfEinspection_(fromDecember5,1990toJanuary 14,1991)~
J b
IR 91-02' Service' Water Systems. Team Inspection O
IR 91 : Monthly Inspection (Continued from January 15,1991) u
_.The following iERs were submitted:
LER 90 -Inadequate = Hourly Fire Patrols-
,1
'LER-90-28:
Leakage' Through Control-' Element Drive Mechanism Housing;(Voluntary Report)
A.
. SAFETY VALVES 0R PORY CHALLENGES OR FAILVRES WHICH OCCURRED.
NONE B.; cRESULTS OF LEAK RATE TESTS i
h n
LThe'results of the; Reactor Coolant System; teak Rate Tests for January; =
1 1991 indicate' that the removal of CEDM pressure, housings #9 and L#13:
with the4subsequentLinstallation of blind flanges on these...
penetrations has corrected the high:RCS leakages e'xperiencedilast!
fall. Total RCSfleakage' averaged 0;08 gpm divided equally between "known" and " unknown" leakage'.
.The Leak Rate-Tests for the' month began'on January 8, 1991.
Because:
.of the " feed and. bleed" operations and RCS4 specific' volume changes
- e associated with, plantc start-up and power ascension, the -RCS leak rates
'during this period.were:relatively less accurate; Afteria few days, equilibrium conditions ucre achieved and the negative leak ratesf.no 4
longer appeared.
The minimum calculated leak rate for the month
' appeared;o_n January 12,1991. ;This_ leak rate was -0.253 gpm total and 2
' 0;310:gpm unknown - The maximum leak rate was calculated during a plant transient and is not representative of the actual leak rate.
The maximum leak rate of 0.337 gpm total and 0.271 gpmL" unknown"Lwas calculated on January 25, 1991.
3
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CHANGES, TESTS AND EXPERIMENTS REQUIRING NUCLEAR REGULATORY COMMISSION AUTH0KniATION-PURSUANT TO 10CFR50.59-Amendment No.
Description None D.
SIGNIFICANT' SAFETY RELATED MAINTENANCE FOR THE MONTH OF JANUARY, 1991
-During the forced outage ending January 8, 1991, many maintenance items were completed / corrected including the following:
Replace the solenoid valve and rebuilt the air cylinders on the steam generator RC-2A main steam isolation valve (HCV-1041A).
The raw water (RW) pump strainer (AC-12B) was replaced with a rebuilt strainer.
Rebuilt the valve actuat'
.i the Component Cooling Water (CCW). inlet valve-(HCV-491A) for hea
. changer AC-lC.
Rebuilt the operator on the CCW inlet valve (HCV-489A) for heat
' exchanger AC-1A.
Rebuilt positioner air relays for the containment cooling coil outlet isolation valve:(HCV-400C).
Nachined a pressurizer to code safety valve loop seal inlet flange (RC-142) and replaced gasket.
A' slight leak remained and Furmanite was used to seal it.
CCW/RW heat exchanger (AC-lD) was taken out of service to replace the lifting lugs on the end bell flanges. -The raw water relief valve-(RW-223) was rebuilt.
e 3
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