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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20205L0401999-04-0909 April 1999 SER Accepting Util Relief Requests for Inservice Insp Second 10-year Interval for Beaver Valley Power Station, Unit 2 ML20203E1181999-02-10010 February 1999 SER Accepting Proposed Revs to Plant,Units 1 & 2 Quality Assurance Program Description ML20199F5341998-12-29029 December 1998 Safety Evaluation Granting Relief Requests 1-TYP-3-B3.140-1, 1-TYP-3-B5.70-1,1-TYP-3-RH-E-1-1,1-TYP-3-B-G-1, 1-TYP-3-APP-I-1,1-TYP-3-UT-1,1-TYP-3-N-509,1-TYP-3-N-521, 1-TYP-3-N-524,1-TYP-3-B3.120-1 & 1-TYP-3-C6.10-1 ML20198K8551998-12-21021 December 1998 SER Granting Relief Request PRR-5 for Third 10-year Inservice Testing for Beaver Valley Power Station,Unit 1 ML20198A1631998-12-0909 December 1998 SER Approving Implementation Program to Resolve USI A-46 at Facility That Has Adequately Addressed Purpose of 10CFR50.54(f) Request ML20195J3131998-11-12012 November 1998 Safety Evaluation Granting First & Second 10-yr Interval Inservice Insp Request for Relief ML20154R9121998-10-20020 October 1998 Safety Evaluation Accepting Proposed Changes to QA Program Description in Chapter 17.2 of BVPS-2 Ufsar.Proposed Changes Would Modify QA Organization to Allow Warehouse QC Inspectors to Report to Manager of Nuclear Procurement Dept ML20154P7491998-10-19019 October 1998 SE Accepting Second ten-year Interval Inservice Insp Request for Relief RR-1-TYP-2-B5.40-1,Rev 0,for Plant, Unit 1 ML20154C6711998-10-0101 October 1998 Safety Evaluation Concluding That Revised Model Identified in Dl Submittal Was Appropriate for Analysis of Installed Conduit Ampacity Limits.Determined That There Are No Outstanding Safety Concerns with Respect to Ampacity ML20202B8571997-11-18018 November 1997 SE Approving Relief Requests for Second 10-Yr Interval for Pumps & Valves Inservice Testing Program for Beaver Valley Power Station,Unit 2 ML20199F4641997-11-13013 November 1997 SER Related to Reactor Pressure Vessel,Pressurized Thermal Shock Assessment for Beaver Valley Power Station,Unit 2 ML20212G4961997-10-28028 October 1997 SER Accepting Pressurized Thermal Shock Assessment for Beaver Valley Unit 2 Reactor Vessel ML20217J5311997-10-0808 October 1997 Safety Evaluation Re First,Second & Third 10-year Interval Inservice Inspection Program Plan Requests for Relief for Plant,Units 1 & 2 ML20217J5891997-10-0707 October 1997 Safety Evaluation Related to Reactor Pressure Vessel Pressurized Thermal Shock for Beaver Valley Power Station, Unit 1 ML20211D8441997-09-17017 September 1997 SER Approving SG 90-day Rept Submitted by Duquesne Light Co for Beaver Valley Power Station,Unit 1,per GL 95-05 ML20216J5861997-09-0404 September 1997 Safety Evaluation Re Third 10-year IST Program.Approves Valve Relief Requests 1,3 & 4.Valve Relief Request 2 Not Required.Authorizes Pump Relief Requests 1,2,3 & 4 ML20148E1051997-05-28028 May 1997 Safety Evaluation Supporting Amend 204 to License DPR-66 ML20137X1441997-04-0909 April 1997 Safety Evaluation Supporting Proposed Rev to RPV Surveillance Capsule Withdrawal Schedule ML20057B0641993-09-13013 September 1993 Safety Evaluation Granting Relief for IST of Reactor Plant Component Cooling Water Pumps of Plant ML20056F3561993-08-12012 August 1993 Safety Evaluation Granting Licensee 930607 Request for Relief from Certain ASME Code Requirements for Temporary Repairs to Svc Water Sys ML20126H7601992-12-30030 December 1992 Safety Evaluation Approving Valve Relief Requests VRR-27, VRR-43 & VRR-44 & Will Provide Reasonable Assurance of Operational Readiness of Valves to Perform Intended Functions.Relief Request PRR-11 Cannot Be Approved ML20127P2081992-11-20020 November 1992 SER Accepting Util Commitment to Entire GIP-2,including Both SQUG Commitments & Implementation Guidance ML20248D7681989-09-29029 September 1989 Supplemental Safety Evaluation Supporting Util Actions in Response to Open Items in 890510 Safety Evaluation Re Plant Safety Monitoring Sys ML20247N3561989-05-30030 May 1989 SER Supporting Util Actions to Comply W/Item 4.5.3 of Generic Ltr 83-28, Reactor Trip Sys Functional Testing ML20246M1791989-05-10010 May 1989 Safety Evaluation Re Verification & Validation Plan for Plant Safety Monitoring Sys.Hardware Design of Sys Found Acceptable.Verification & Validation Plan Found Incomplete & Unacceptable.Software Design Process Inadequate ML20246D5501989-04-26026 April 1989 Safety Evaluation Accepting Util Submittals on Natural Circulation Cooldown for Unit ML20206G0431988-11-17017 November 1988 Safety Evaluation Concluding That All Issues Raised Under Item Resolved & Item 4.3 Closed ML20153C0911988-08-17017 August 1988 Safety Evaluation Re Licensee 870731 Comments on Sser 5, Section 9.5.1.Fire Protection in Cable Rooms & Containment Constitutes Acceptable Deviations from Branch Technical Position Cmeb 9.5-1 ML20205T0021988-08-10010 August 1988 SER Accepting Util 831104,840330 & 870504 Responses to Item 2.2.1 of Generic Ltr 83-28 Re Equipment Classification Programs for All safety-related Components ML20154R4451988-05-31031 May 1988 Safety Evaluation Re Compliance W/Atws Rule 10CFR50.62.Util Proposed Design Acceptable Subj to Final Resolution of Tech Spec Issue ML20154P4341988-05-24024 May 1988 Safety Evaluation Concluding That Proposed Tech Spec Change Acceptable.No Amend Issued Since Conditions Resulting in Need for Amend to License NPF-73 No Longer Exist ML20154F9901988-05-12012 May 1988 Supplemental Safety Evaluation Concluding That Licensee 880322 Response to Open Issues Identified in 860722 Draft Technical Evaluation Rept of 840330 Submittal Re Salem ATWS Event Action Item 1.2, Post-Trip Review Satisfactory ML20154F9841988-05-12012 May 1988 Supplemental Safety Evaluation Concluding That Licensee 851114 Response to Open Issues Noted in 851017 Draft Technical Evaluation Rept of 831104 Submittal Re Salem ATWS Event Action Item 1.2, Post-Trip Review Satisfactory ML20153B6291988-04-25025 April 1988 Safety Evaluation Granting Util 870616 & 871110 Requests for Inservice Insp Relief for Welds on Nonregenerative Hxs,Per 10CFR50.55a(g)(6)(i) ML20148K5231988-03-18018 March 1988 Safety Evaluation Supporting Util Inservice Testing Program & Requests for Relief ML20234E0531987-12-0808 December 1987 Safety Evaluation Accepting Design Changes to Be Implemented During Unit 1 Cycle 7 Fuel Reload.Tech Spec Change Unnecessary ML20236X4941987-11-0909 November 1987 Safety Evaluation Granting Util 860617 Relief Request from Performing Volumetric & Visual Exam Requirements of ASME Section XI for Reactor Coolant Pumps Casing Welds & Internal Surfaces ML20237B1651987-10-21021 October 1987 Safety Evaluation Supporting Elimination of Primary Component Support Snubbers from Primary Coolant Loops ML20204H7181987-03-18018 March 1987 Interim Safety Evaluation Re Pump & Valve Operability Assurance (SER Confirmatory Issue 13).Pages from Pvort Audit Encl ML20206G2231987-03-12012 March 1987 SER Accepting Licensee Request to Use Damping Values from ASME Code Case N-411 Per Conditions Outlined in Util ML20207P6551987-01-0202 January 1987 SER Accepting Licensee Compliance W/Generic Ltr 83-28,Item 2.1,Part 2 Re Vendor Interface Program for Reactor Trip Sys (RTS) Components & Item 4.5.2 Concerning RTS Online Reliability Testing ML20212B0111986-11-30030 November 1986 Safety Evaluation Granting Util Request for Exemptions from App R Requirements Re Separation of Cables & Equipment & Associated Circuits ML20205G4491986-08-31031 August 1986 Safety Evaluation Accepting Projected Values of Matl Properties for Fracture Toughness Requirements for Protection Against Pressurized Thermal Shock Events ML20204G9281986-07-31031 July 1986 Safety Evaluation Supporting Util 860502 Submittal of Westinghouse Reload Safety Evaluation,Beaver Valley Nuclear Plant,Unit 1 Cycle 6 ML20203G2371986-07-28028 July 1986 Interim SER Re Dcrdr Summary Rept & Preimplementation Audit on 860211 & 12.Requirements of Suppl 1 to NUREG-0737 Generally Satisfied.Several Items Remain to Be Completed ML20206H4931986-06-19019 June 1986 Safety Evaluation on Generic Ltr 83-28,Item 4.2.3 & 4.2.4, Preventive Maint Program for Reactor Trip Breakers/Life Testing. Licensee Position Unacceptable ML20205N1151986-04-22022 April 1986 Interim Rept Re Review of Util Response to Generic Ltr 85-12 on Reactor Coolant Pump Trip Criteria.Addl Info Required ML20202C5721986-04-0303 April 1986 Sser Accepting Util 860304 Response to Generic Ltr 83-28, Item 4.3, Seismic Qualification of Shunt Trip Components ML20214E3631986-03-17017 March 1986 Safety Evaluation Supporting Amend 2 to CPPR-105 ML20154N7451986-03-10010 March 1986 Safety Evaluation Supporting Util 850819 Request to Withdraw Original Commitment to Provide Steam Leakage Collection Sys Around Certain Steam Valves 1999-04-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARL-99-154, Monthly Operating Repts for Sept 199 for Bvps,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 199 for Bvps,Units 1 & 2. with L-99-139, LER 99-S01-00:on 990813,uncompensated Loss of Ability to Detect within Single Intrusion Security Detection Zone Occurred.Caused by Procedure non-compliance.Involved Personnel Received Counseling Re Event.With1999-09-0202 September 1999 LER 99-S01-00:on 990813,uncompensated Loss of Ability to Detect within Single Intrusion Security Detection Zone Occurred.Caused by Procedure non-compliance.Involved Personnel Received Counseling Re Event.With L-99-140, Monthly Operating Repts for Aug 1999 for Bvps,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Bvps,Units 1 & 2. with L-99-126, Monthly Operating Repts for Jul 1999 for Beaver Valley Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Beaver Valley Power Station,Units 1 & 2.With L-99-107, Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with ML20209D9531999-06-27027 June 1999 Inservice Insp Ninety-Day Rept Bvps,Unit 2 Outage 7,Year 1999 L-99-096, Monthly Operating Repts for May 1999 for BVPS Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for BVPS Units 1 & 2. with L-99-078, Special Rept:On 990326,seismic Monitoring Instruments Were Declared Inoperable.Caused by Resolution of Potential TS Compliance Issue & Work Scheduling Issue.Instrumentation Was Returned to Svc Following Calibr & Declared Operable1999-05-0303 May 1999 Special Rept:On 990326,seismic Monitoring Instruments Were Declared Inoperable.Caused by Resolution of Potential TS Compliance Issue & Work Scheduling Issue.Instrumentation Was Returned to Svc Following Calibr & Declared Operable L-99-079, Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With ML20205L0401999-04-0909 April 1999 SER Accepting Util Relief Requests for Inservice Insp Second 10-year Interval for Beaver Valley Power Station, Unit 2 L-99-054, Special Rept:On 990320,meteorological Tower Wind Speed Sensors Were Declared Inoperable.Caused by Calibration Completed by Vendor Did Not Adequately Cover Full Operating Range of Sensors.Removed Sensors & Sent Offsite1999-04-0505 April 1999 Special Rept:On 990320,meteorological Tower Wind Speed Sensors Were Declared Inoperable.Caused by Calibration Completed by Vendor Did Not Adequately Cover Full Operating Range of Sensors.Removed Sensors & Sent Offsite L-99-058, Monthly Operating Repts for Mar 1999 for Bvps,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bvps,Units 1 & 2. with ML20196K7981999-03-25025 March 1999 Rev 4 to COLR, for Cycle 8 L-99-038, Monthly Operating Repts for Feb 1999 for Bvps,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Bvps,Units 1 & 2. with ML20203E1181999-02-10010 February 1999 SER Accepting Proposed Revs to Plant,Units 1 & 2 Quality Assurance Program Description L-99-019, Special Rept:On 990120,meteorological Tower Wind Speed Sensors Declared Inoperable.Caused by Processor Card for Sensor Locked Up & Needed to Be Reset.Heater That Fit Around Shaft of Sensor Replaced1999-02-0505 February 1999 Special Rept:On 990120,meteorological Tower Wind Speed Sensors Declared Inoperable.Caused by Processor Card for Sensor Locked Up & Needed to Be Reset.Heater That Fit Around Shaft of Sensor Replaced ML20196F7011999-01-31031 January 1999 BVPS Unit 2 Heatup & Cooldown Limit Curves During Normal Operation at 15 EFPY Using Code Case N-626 ML20203D4811999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Bvps,Units 1 & 2, in Accordance with NRC GL 97-02.With ML20207E6631999-01-28028 January 1999 Rev 0 to EMECH-0713-1, Operational Assessment of SG Tubing at Beaver Valley Unit 1,Cycle 13 ML20210G7041999-01-22022 January 1999 BVPS Unit 1 Facility Changes,Tests & Experiments for 980123-990122 ML20207E5861998-12-31031 December 1998 Annual Rept 1998 for Toledo Edison ML20207E5601998-12-31031 December 1998 Annual Rept 1998 for Pennpower ML20198B9021998-12-31031 December 1998 BVPS Unit 1 Simulator Four Yr Certification Rept for 1995-1998 ML20207E5901998-12-31031 December 1998 Dqe 1998 Annual Rept to Shareholders ML20199C9971998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Bvps,Units 1 & 2. with ML20207E5521998-12-31031 December 1998 Annual Rept 1998 for Ohio Edison ML20207E5761998-12-31031 December 1998 Annual Rept 1998 for Illuminating Co ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199F5341998-12-29029 December 1998 Safety Evaluation Granting Relief Requests 1-TYP-3-B3.140-1, 1-TYP-3-B5.70-1,1-TYP-3-RH-E-1-1,1-TYP-3-B-G-1, 1-TYP-3-APP-I-1,1-TYP-3-UT-1,1-TYP-3-N-509,1-TYP-3-N-521, 1-TYP-3-N-524,1-TYP-3-B3.120-1 & 1-TYP-3-C6.10-1 ML20198K8551998-12-21021 December 1998 SER Granting Relief Request PRR-5 for Third 10-year Inservice Testing for Beaver Valley Power Station,Unit 1 ML20198A1631998-12-0909 December 1998 SER Approving Implementation Program to Resolve USI A-46 at Facility That Has Adequately Addressed Purpose of 10CFR50.54(f) Request L-98-229, Monthly Operating Repts for Nov 1998 for Bvps,Units 1 & 2. with1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bvps,Units 1 & 2. with ML20195J3131998-11-12012 November 1998 Safety Evaluation Granting First & Second 10-yr Interval Inservice Insp Request for Relief L-98-210, Monthly Operating Repts for Oct 1998 for Bvps,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bvps,Units 1 & 2. with ML20206G0291998-10-31031 October 1998 BVPS Unit 2 Facility Changes,Tests & Experiments for Period 971101-981031 ML20154R9121998-10-20020 October 1998 Safety Evaluation Accepting Proposed Changes to QA Program Description in Chapter 17.2 of BVPS-2 Ufsar.Proposed Changes Would Modify QA Organization to Allow Warehouse QC Inspectors to Report to Manager of Nuclear Procurement Dept ML20154P7491998-10-19019 October 1998 SE Accepting Second ten-year Interval Inservice Insp Request for Relief RR-1-TYP-2-B5.40-1,Rev 0,for Plant, Unit 1 ML20198F7611998-10-0606 October 1998 Duquesne Light Co,Beaver Valley Power Station 1998 Emergency Preparedness Ingestion Zone Exercise, Conducted on 981006 ML20154C6711998-10-0101 October 1998 Safety Evaluation Concluding That Revised Model Identified in Dl Submittal Was Appropriate for Analysis of Installed Conduit Ampacity Limits.Determined That There Are No Outstanding Safety Concerns with Respect to Ampacity ML20154D5001998-09-30030 September 1998 Special Rept on Overview of BVPS-1 & BVPS-2 TS Compliance Issues & Corrective Action Taken L-98-197, Monthly Operating Repts for Sept 1998 for Beaver Valley Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Beaver Valley Power Station,Units 1 & 2.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods L-98-188, Special Rept:During 1998,Unit 2 SG Eddy Current exam,26 Tubes Were Improperly Encoded in SG 2RCS-SG21C During Previous Outage.Use of Independent Databases to Track New Indications Being Implemented as Preventive Measure1998-09-21021 September 1998 Special Rept:During 1998,Unit 2 SG Eddy Current exam,26 Tubes Were Improperly Encoded in SG 2RCS-SG21C During Previous Outage.Use of Independent Databases to Track New Indications Being Implemented as Preventive Measure L-98-178, Monthly Operating Repts for Aug 1998 for Bvps,Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Bvps,Units 1 & 2. with ML20155B5871998-08-28028 August 1998 Non-proprietary Rev 1 to 51-5001925-01, Risk Assessment for Installation of Electrosleeves at BVPS & Callaway Plant ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed L-98-168, Monthly Operating Repts for July 1998 for Bvps,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Bvps,Units 1 & 2 L-98-157, Special Rept:On 980423,inoperability of Seismic Monitoring Instrument Noted.Caused by Obsolescence of Instrument & Inability to Obtain Necessary Spare Parts.Design Change Is Being Pursued to Obtain Replacement Product1998-07-29029 July 1998 Special Rept:On 980423,inoperability of Seismic Monitoring Instrument Noted.Caused by Obsolescence of Instrument & Inability to Obtain Necessary Spare Parts.Design Change Is Being Pursued to Obtain Replacement Product L-98-139, Monthly Operating Repts for June 1998 for Bvps,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Bvps,Units 1 & 2 L-98-119, Monthly Operating Repts for Bvps,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for Bvps,Units 1 & 2 1999-09-30
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- SAFETY EVALUATION REPORT OFFICE OF NUCLEAR REACTOR REGULATION UNITED STATES NUCLEAR REGULATORY COMMISSION MAIN STEAM LINE BREAK WITH CONTINUED FEEDWATER ADDITION BEAVER VALLEY NUCLEAR PLANT, UNIT 1 DOCKET N0. 50-334 Introduction In the summer of 1979, a pressurized water reactor (PWR) licensee submitted a report to the NRC that identified a deficiency in his original analysis of the containment pressurization resulting from a postulated main steam line break (MSLB). A reanalysis of the containment pressure response following a MSLB was performed, and -
it was determined that, if the auxiliary feedwater (AFW) system continued to supply feedwater at runout conditions to the steam generator that had experienced the steam line break, the containment design pressure would be exceeded in approximately 10 minutes. In other words, the long-term blowdown of the water supplied by the AFW system had not been considered in the earlier analysis.
On October 1, 1979, the foregoing information was provided to all holders of operating licenses and construction permits in IE Information Notice 79-24 (2). Another licensee performed an accident analysis review pursuant to the information furnished in the above cited notice and discovered that, with offsite electrical power available, the condensate pumps would feed the affected steam generator at an excessive rate. This excessive feed had not been considered in his analysis of the postulated MSLB accident.
A third licensee informed the NRC of an error in the MSLB analysis for his plant. For a zero or low power condition at the end of core life, the licensee identified an incorrect postulation that the startup feedwater control valves would remain positioned "as is" during the transient. In reality, the startup feedwater control valves will ramp to 80% full open due to an override signal ,
resulting from the low steam generator pressure reactor trip signal.
Reanalysis of the events showed that the rate of feedwater addition to the affected steam generator associated with the opening of the startup valve would cause a rapid reactor cooldown and resultant reactor-return-to-power response, a condition which is beyond the .
plant's design basis.
r C208130436 820804 :
PDR ADOCK 05000334 l C PDR
y Following the identification of these deficiencies in the original MSLB accident analysis, the NRC issued IE Bulletin 80-04 on February 8, 1980. This bulletin required all licensees of PWRs and certain near-term PWR operating license applicants to do the following: :
"1. Review the containment pressure response analysis to determine !
if the potential for containment overpressure for MSLB inside containment included the impact of runout flow from the auxiliary feedwater system and the impact of other energy ,
sources such as continuation of feedwater or condensate flow. !
In your review, consider your ability to detect and isolate the damaged steam generator from these sources and the ability of the pumps to remain operable after extended operation at runout flow.
- 2. Review your analysis of the reactivity increase which results l from a MSLB inside or outside containment. This review should
! consider the reactor ccoldown rate and the potential for the reactor to return to power with the most reactive control rod in the fully withdrawn position. If your previous analysis did not consider all potential water sources (such as those listed in 1 above) and if the reactivity increase is greater than ~,
previous analysis indicated, the report of this review should '
include: ;
- a. The boundary conditions for the analysis, e.g., the end of life shutdown margin, the moderator temperature coefficient, power level and the net effect of the associated steam f generator water inventory on the reactor system cooling, !
etc.;
- b. The most restrictive single active failure in the safety injection system and the effect of that failure on , !
- delaying the delivery of high concentration boric acid t solution to the reactor coolant system l c. The effect of extended water supply to the affected steam i j
generator on the core criticality and return to power; and !
- d. The hot channel facters corresponding to.the most reactive l rod in the fully withdrawn positions at the end of life, :
and the Minimum Departure trom Nucleate Boiling Ratio !
(MDNBR) values for the analyzed transient. ;
I
- 3. If the potential for containment overpressure exists or the i
, reactor return-to-power response worsens, provide a proposed j corrective action and a schedule for completion of the ;
- corrective action. If the unit is operating, provide a !
description of any interim action that will be taken until j j the proposed corrective action is completed." ;
i i
t t
Following the licensee's initial response to IE Bulletin 80-04, a request for additional information was developed to obtain all the information necessary to evaluate the licensee's analysis.
The results of our evaluation for Beaver Valley Power Station, Unit 1 (Beaver Valley 1) are provided below.
Evaluation ,
i Our consultant, the Franklin Research Center (FRC), has reviewed the submittals made by the licensee in resoonse to IE Bulletin '
80-04, and prepared the attached Technical Evaluation Report. We ;
have reviewed this evaluation and concur in its bases and findings. (
i' Conclusion ;
Based on our review of the enclosed Technical Evaluation Report, I the following conclusions are made regarding the postulated MSLB with i continued feedwater addition f
- 1. There is no potential for containment overpressurization l resulting from a MSLB with continued auxiliary feedwater '
addition; the steam line break protection system-provides actuation signals which, in fact, isolate the main feedwater i
lines; {
- 2. The AFW pumps will experience runout conditions; however, based on evaluation of data from a 10-minute run under runout conditions, !
the licensee concluded that the pump will not be damaged and [
will remain available after extended operation at runout flow '
conditions; i,
- 3. All potential water sources were identified and no reactor !
i return-to-power or DNBR violation occurs; therefore, the ;
FSAR reactivity increase analysis remains valid. z
- References
- 1. IE Bulletin 80-04, " Analysis of a PWR Main Steam Line Break r with Continued Feedwater Addition," NRC Office of Inspection ;
and Enforcement, February 8,1980 ;
IE Information Notice 79-24, "0verpressurization of the 2.
Containment of a PWR Plant After a Main Steam Line Break," i NRC Office of Inspection and Enforcement, October 1,1979 '
i I
l
r
- 3. C. N. Dunn (DLC) Letter to B. H. Grier (NRC, Region 1),
Subject:
Beaver Valley Power Station, Unit 1 Response to IE Bulletin No. 80-04, April 28, 1980
- 4. Beaver Valley Power Station, Unit 1, Final Safety Analysis Report, through; Amendments.9,.Duquesne Light Compar.y, June 1974
- 5. S. A. Varga (NRC) Letter to C. N. Dunn (DLC),
Subject:
Amendment No. 30 to Facility Operating License No. DPR-66 for the Beaver Valley Nuclear Power Station, Unit No.1, September 10, 1980
- 6. Technical Evaluation Report, TER-c5506-119, "PWR Main Steam Line Break with Continued Feedwater Addition - Review of Acceptance Criteria," Franklin Research Center, November 17, 1981
- 7. IEEE Standard 279-1971, " Criteria for Protection Systems for Nuclear Power Generating Stations," Institute of Electrical and Electronics Engineers, New York, NY,1971
- 8. NUREG-0800, Standard Review Plan, Section 15.1.5, " Steam System Piping Failures Inside and Outside of Containment -
(PWR)," NRC, July 1971
- 9. ANS/ ANSI-4.5-1980, " Criteria for Accident Monitoring Functions in Light-Water-Cooled Reactors," American Nuclear Society, Hinsdale, IL, December 1980
- 10. Regulatory Guide 1.97, " Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess P.lant and Environs Conditions During and Following an Accident," Revision 2, NRC, December 1980
- 11. ANS-51.7/N658-1976,'" Single Failure Criteria for PWR Flu'id Systems," American Nuclear Society, Hinsdale, IL, June 1976
- 12. Regulatory Guide 1.26, " Quality Group Classifications and Standards for Water, Steam, and Radioactive-Waste-Containing Components of Nuclear Power Plants," Revision 3, NRC, February 1976
- 13. NUREG-0588, " Interim Staff Position on Environmental Qualifi-cation of Safety-Related Electrical Equipment," Revision 1, NRC, July 1981
- 14. J. J. Carey (DLC) Letter to S. A. Varga (NRC),
Subject:
Potential for Damage to the AFW Pumps Due to Operation at Runout Flow For 30 minutes, July 21, 1982 Principal Contributor P. Hearn
.