ML20059D959

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 930923-25.Violations Noted: Failure to Follow Procedures Re Mispositioning of Spent Fuel Assembly in Unit 2 Spent Fuel Pool on 930913 & Inadequate Corrective Actions to Prevent Similiar May 1993 Event
ML20059D959
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 10/26/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20059D939 List:
References
50-373-93-28, 50-374-93-28, NUDOCS 9311030049
Download: ML20059D959 (2)


Text

~

k

~f i

t k

i

@TICE OF VIOLATION Commonwealth Edison Company Docket Nos. 50-373; 50-374 LaSalle County Station Units 1 and 2 License Nos. NPF-11; NPF-18 During an NRC inspection conducted on September 23 through September 25, 1993, ,

violations of NRC requirements were identified. In accordance with the

" General Statement of Policy and Procedure for NRC Enforcement Actions," 10  :

CFR Part 2, Appendix C, the violations are listed below:

1. LaSalle Technical Specification 6.2.A.a requires written procedures -

recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978, be established, implemented, and maintained. Regulatory Guide  !

1.33 includes procedures for preparation for refueling and refueling equipment operation.

LaSalle fuel Procedure (LFP)-100-2, " Administrative Control of Transfer i of Fuel or Special Nuclear Material Between or Within the Spent Fuel

  • Pool (s) or Vaults", requires, in part, that all steps in the Nuclear Component Transfer List be completed and verified by the Fuel Handling Supervisor.

Contrary to the above, on September 13, 1993, during defueling of the Unit 2 reactor, fuel handlers placed and verified a spent fuel bundle +

designated by the Nuclear Component Tranfer List to be placed in spent '

fuel pool position FFF-38 into position GGG-38. ,

This is a Severity Level IV violation (Supplement 1).

2. 10 CFR 50, Appendix B, Section XVI, states, in part, " Measures shall be established to assure that conditions adverse to quality ... are ,

promptly identified and corrected ... the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition."

Contrary to the above, corrective actions for a similar event in May l 1993, did not prevent fuel handlers from placing spent fuel in an -1 incorrect location in the Unit 2 spent fuel pool on September 13, 1993.

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Commonwealth Edison is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington D.C. 20555, with a copy to the Regional Administrator, Region III, and a copy to the NRC Resident Inspector at the facility that is the subject of this Notice, within _

9311030049 931026 ..

PDR ADOCK 05000373 .!

O PDR[j j

Notice of Violation 2 30 days of the date of the letter transmitting this Notice of Violation (Notice). . This reply should be clearly marked as a " Reply to a Notice of Violation" and should include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation, (2) the corrective steps that have been taken and the results achieved, (3) the-corrective steps that will be taken to avoid'further violations, and (4)'the date when full compliance will be achieved. If an adequate reply is not received within the time specified in this Notice, an order or a Demand for Information may be issued to show cause why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.

Dated at Glen Ellyn, Illinois this ;4C day of October 1993

= +--wr e er ev- e e- m- m s ,, v-.rw- -e-+-