ML20059A689

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Safety Insp Rept 50-346/90-09 on 900417-0717.Violations Noted.Major Areas Inspected:Licensee Actions on Previous Insp Findings,Lers,Plant Operations,Refueling,Radiological Controls,Security,Emergency Preparedness & Maint
ML20059A689
Person / Time
Site: Davis Besse 
Issue date: 08/10/1990
From: Knop R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20059A687 List:
References
50-346-90-09, 50-346-90-9, NUDOCS 9008230171
Download: ML20059A689 (16)


See also: IR 05000346/1990009

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U.S. N)CiEAR REGULATORY COMMISSION

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REGION III

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Report No. 50-346/90009(DRP)

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Docket No. 50-346

Operating License No NPF-3-

Licensee: Toledo Edison Company

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Edison Plaza, 300 Madison Avenue

Toledo, OH 43652

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Facility Name: Davis-Besse 1

Inspection At: Oak Harbor, Ohio

Inspection Conducted:- April 17 through July 17, 1990

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Inspectors:

P. M. Byron

D. C. Kosloff

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R. K. Walton

P. L. Hiland

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Approved By

R.' V K

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Reactor Projects Branch 3

Date

Inspection Summary

Inspection on April 17 through July 17,1990(ReportNo.'50346/90009(DRP))

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Areas Inspected: A routine safety inspection by resident inspectors of

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licensee actions on previous inspection findings, licensee event reports,

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plant operations, refueling, radiological controls, maintenance / surveillance,-

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emergency preparedness, security, engineering and technical support, and

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safety assessment / quality verification was performed.

Results: Seven events occurred during the inspection period (Paragraphs 4,

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7,10 and 11), collectively these events demonstrated a weakness in task

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management, planning and control of plant activities.

The NRC is considering

this weakness for enforcement action.

In addition, a non-cited violation was

identified for failing to implement a Technical Specification requirement .

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(Paragraph 3) and another non-cited violation was identified for failing to

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'(Paragraph 7)plement a Technical Specification surveillance requirements

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9008230171 900813

ADOCK 0500

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DETAILS

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Persons Contacted

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Toledo Edison Company

D. Shelton, Vice President, Nuclear

  • G. Gibbs, Director, Quality Assurance
    • L. Stort, Plant Manager

H.-Heffley, Maintenance Manager

  • R.Brandt,-PlantOperationsManager(Acting)
  • H. Bezilla, Superintendent,-Operations

E. Salowitz, Director, Planning and Support

  • S. 'Jain, Director, DB Engineering.
  • K. Prasad,- Nuclear Engineering Manager (Acting)

'G. Grime, Industrial Security Director

D. Timms, Systems Engineering Manager.-

  • R. Uebbing, Maintenance Coordinator

J. Polyak, Radiological Control Manager

  • R. Coad, Radiological Protection Supervisor

J. Lash, Independent Safety Engineering Manager

  • H. Stevens,-Indeper. dent Safety Engineering

R. Schrauder, Nuclear: Licensing Manager

  • G. Honma, Compliance Supervisor
  • R. Gaston, Licensing. Technologist

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  • R. Seba, Licensing Engineer-

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USNRC-

'*P. Byron, Senior Resident. Inspector

  • D. Kosloff, Resident Inspec/or
  • R. Walton', Resident' Inspector

P. Hiland. Senior Resident Inspector, Perry

  • Denotes those personnel attending the. June-4 1990, exit meeting.

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' Denotes those personnel attending the July 17, 1990, exit meeting.

2.

Licensee Action on Previous Inspection Findings (92701)'

.(Closed)OpenItem(346/86032-13(DRP)):

Completion of.a plan' for

repairing and maintaining fire and ventilation boundary' doors and

balancing ventilation air flow. Completion of this item was related

to the. licensee's completion of plant modifications required to comply

with 10 CFR 50, Appendix R requirements.

The inspectors' have observed

numerous work and engineering activities related:to this item..

Inspections related to Appendix P have also' reviewed activities related

to'this item. lThe licensee-is continuing work in this-~ area;and it

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. appears that appropriate effort'is being expended to maintain doors.

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The inspectors will continue to' monitor the status of doors.- This' item

is . closed.-

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_(Closed)OpenItem(346/87022-01(DRP)): Determine if the licensee's

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method of operability determination for the Component Cooling Water

(CCW) Systems is appropriate during-inoperability of'CCW room ventilation.

After this item was identified, the NRC provided guidance to its staff

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on reviewing licensee operability decisions.

Based on that guidance,

the inspectors determined that the licensee's practice was appropriate.

This item is closed.

(Closed) Violation-(346/88014-02(DRP)): During a previous refueling

operation, an operator demonstrated a lack of sufficient knowledge to-

operate refueling equipment. A review of training records revealed

that the operator had not received hands-on training in the previous

four years. The licensee has since changed refueling

ensure that operators are trained prior to refueling. procedures. to

Training consists

of classrocm studies and operations with a dumnly assembly. The' operations

superintendent provides.a list of qualified personnel which is included-

in the Fuel Handling Directors log.

The inspectors have observed

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defueling and refueling operations. The operators were knowledgeable

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of their equipment and procedures.

This item is closed..

No violations or deviations were identified in this area.

3.

Licensee Event Reports followup (92700)

Through direct observation, discussions with licensee personnel,.

and review of records, the following licensee event reports (LERs)

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were reviewed to determine that reportability rcquirements were fulfilled,

that immediate corrective actions to prevent recurrence was accomplished

inaccordancewithTechnicalSpecifications(TS). The LERs listed below

are considered closed:

(Closed)LER90006:

Inadvertent Safety Features Actuation System (SFAS)

Actuation While T)efueled When Dreaker Switch HAAE2 Was Bumped Open.

This event was discussed in Inspection Report 50-346/90005. This LER

is closed.

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(Closed)LER90007:

Inadvertent Inconsequential Safety-Features Actuation

'5FstemActuationWhileDefueled.

Three SFAS actuations were reported in

this LER. This LER describes random spiking observed in containment

radiation monitor' RE 2005. The licensee has not yet-identified the cause

of these spikes.

The inspectors will continue to moniu r the licensee's

efforts to identify the cause of these spikes.

These SFAS actuations

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were discussed in Inspection Report No. 50-346/90005.- This LER is

closed.

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(Closedl LtR 0008:

Unnecessary Safety Features Actuation System Level 1

Acto:.tTon DurinfUore Support Assembly (CSA) flove. This SFAS actuation

wu caused by two SFAS radiation monitors being exposed to radiation from

the CSA. All fuel was removed from the reactor when this actuation

(ccurred. All equipment functioned as expected and the SFAS actuation

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had no safety significance. The radiation levels in containment during

the CSA move were higher than expected. The CSA move was discussed in

Inspection Report No. 50-346/90012.

This LER is closed.

(Closed) LER 90009: Source Check of Station Vent Radiation Monitors

Did Not Satisfy Technical Specification (TS) 3.3.3.10.

On March 16,

1979, the licensee submitted a license amendment request to include the

Radioactive Effluent Technical Specifications (RETS) in the Appendix A

TS. This request was supplemented by_the licensee with five letters

dated between December 23, 1982 and. November 1, 1984. On July 2, 1985,

in response to the license amenoment request, Amendment 86 was issued

(effectiveOctober 30,1985), incorporating definition 1.29, " Source

Check," which states that a source check uses a radioactive source,-

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and Table 4.3-16 which' requires that the ststion vent monitors be-

given a monthly source check,

in 1982, the licensee had installed the station vent monitors that

became the subject of Amendment 66

The licensee required that the

vendor supply the monitors with an installed radioactive check source.

The vendor, apparently unknown to the licensee, sup) lied monitors which

used an installed light emitting diode (LED) as a c1eck source instead

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of a radioactive source.

To detect a radioactive release, the detector

uses a detector crystal which emits light when struck by ionizing

radiation, the light is detected by a photomultiplier tube. The LED

checked th' detector by activatin

activatin, the detector crystal. g the photomultiplier tube without

The licensee also performed an 18-month

calibration of the detectors using a radioactive source.

On April 26,.1990, a licensee system engineer determined that the LED

check was not a source check. The licensee declared the detectors-

inoperable and complied with the TS action statement.- The inspecto?

verified that on April 27, 1990, the monthly source check procedures,

DB-SC-03229 and DB-SC-03230, were revised to require use of a radioactive

source. The inspectors reviewed the procedures and verified that the use

of a radioactive source is now required.

The detectors were successfully

checked with a radioactive source on April 28, 1990.

The licensee

concluded that the root cause of the event was a failure to. conduct an

adequate review of installed equipment relative to the:TS requirement.

The licensee did not propose any corrective action for-this root cause

because there have been extensive improvements in the conduct of

activities since this inadequate review occurred.

Because the licensee had not performed the source check as required by

the TS, a violation of TS 3.3.3.10 (346/90009-01(DRP)) extsted at various

times from October 30, 1985 until April 28, 1990.

This 'icensee-identified

violation is not being cited because the criteria speci(ied in Sr.ction V.G.

of the Enforcement Policy were satisfied.

No other violations or deviations were identified.

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Plant Operations (71707, 71710, 64100, 93702)

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Operational Safety Verification

Inspections were routinely performed to ensure that the: licensee

conducts activities at the facility safely and in conformance:

with regulatory requirements. The inspections focused on the<

implementation and overall effe ,civeness of the licensee's- control

of operating activities, and on the performance;of licensed and

non-licensed operators and shift managers,

The inspections included

direct observation of activities, tours oi the facility. -intryiews

and Uscussions with licensee personnel, independent verification of

saf'n o stem status and limitin

revUn of facility procedures; _ g conditions of operation (LCO), a' d<

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records,'and reports. _The following.

items were corsidered during these-inspections:

' Adequacy c plant staffing and supervision.

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Control room professionalism,; including procedure adherence,-

op'erator attentiveness, and response to alarms, events, and

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off-normal conditions,

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Operability of selected safety-related systems, including;

attendant alarms, instrumentation, and controls.-

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Maintenance of quality records and reports.

The inspectors observed that control room shift supervisors,

shift managers, and operators were attentive to plant conditions,

performed frequent panel walk-downs and were responsive to-

off-normal alarms and conditions,

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On May 1,1990, the licensee drained the reactor' vessel about

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18 inches lower then' planned while draining the refueling-canal.

Prompt operator action

The reactor

vessel was refilled by. prevented further-draindown.

gravity drain from _the Borated Water Storage

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Tank (BWST). The reactor vessel internals indexing fixture was in

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place above the reactor vessel during the operation and the draindown

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occurred because there is very little flow from the canal to the-

vessel once the canal level drops to the . top of the indexing fixture. .

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Initially the operators thought that the indexing fixture was ;1ocated:

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elsewhere. The canal draining procedure did_not provide any guidance

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regarding the location or effects of the indexing fixture. This

event -is described in'more detail in Inspection- Report

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No.50-346/90012(DRSS), As stated in the report, the refueling'

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canal draining was accomplished utilizing procedure'DB-0P-06023,

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" Fill, Drain, and Purification of. Refueling Canal,". Revision 00,

dated February 14, 1990. Section 3.6 addresses' lowering the water

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level using a decay heat pump (DHP).

The inspectors reviewed

DB-0P-06023 and determined that the. procedure was not appropriate to

the circumstances in that it does -not address the indexing fixture nor

does it contain precautions about the loss of decay heat cooling

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from a partially filled reactor coolant system'as-described in

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Generic Letter 87-12. This is a violation of.10 CFR 50, Appendix B,

Criterion Y, which requires that activities effecting quality shall

beappropriatetothecircumstances(346/90012-03).

Conduct of Operations Procedures DB-0P-00000,- Revision 01, dated.

April 2 1990,-Section 6.7.6 requires that prior to the performance

of critical, complicated, unusual, or infrequent.. operations, a

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procedure review shall' be performed, and briefings: shall be

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conducted by the individual in charge of_the evolution. The

licensee has determined that no: formal briefing was held nor was a'

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pre-evolution walkdown performed. The shift supervisor briefed

individuals separately, but did not identify' equipment which was

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involved as required by 6.7.6.c.

Since the draining of the refueling

canal is normally performed during refueling outages it meets the-

criteria of-infrequent operations. These are examples-of violations-

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of Technical Specification 6.8.1 (346/90012-04) which requires.that

procedures be adhered to.-

On May 18, 1990, a Safety Features' Activation System (SFAS)

initidion occurred as a result of maintenance being performed on

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one SFAS channel and a concurrent loss of power.to ansecond SFAS

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channel. The loss of. power occurred when an operator assumed that

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essential bus'Y3 was powered by an alternate power supply which

had been disconnected earlier in the day. The licensee was

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performing the' prerequisites for DB-SC-04053, "4160. System Transfer

and Lockout Test Buses;C1 and C2," Revision 00, dated May 3,1989. -

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Step 4.2.10, as changed by Temporary Approval, TA 90-3109, dated

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tiay 15,1990, requires that regulated rectifiers YRF1 and YRF3 be

israted and the' verification step references procedure DB-0P-06319,

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at' AC System Procedure." The o)erator went to the wrong.

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in DB-0P-06319 and isolated both tie rectifiers and associated

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inw ters rather than only the rectifiers. A11~four levels of

SFAS were #.itiated from the-loss of: power which resulted in--

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1000 gallons of water being injected 1nto the reactor ~

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ig of the emergency diesel generators, and the closure

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at isolation valves (refer-to paragraph 7.b for more.

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che 'icensee revealed that a temporary restricted change,

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.o0 to De-0P-06319 which related to alternate power supply-

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(YAM !.ad not beu cancelled nor' had maintenance work order (MWO) -

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2-86-0272-23 whici connected a new regulated alternate supply '(XY3)

and disconnected Y LR had not been closed out though the work was

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comCated. The paperwork indicated that YAR was still; connected.

In 4; tion, drawings for the-modification.had been' posted before

the work was completed and is documented in -PCAQR 90-0402, dated

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May 11, 1990. The operators, with the available information,

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assumed that TA 90-3109 had also been issued prematurely and

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performed step 4.2.10 as written prior to the temporary change which

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required both the rectifiers and associated inverters be isolated.'

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A review of the event.by the inspectors revealed that the event-

could have been prevented if the operators had followed DB-SC-04053,

step 4.2.10 as written. The inspectors also concluded;that the

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licensee inadequately controlled the NWO process and the temporary

arocedure- change process. This resulted in the operators not

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seing aware of plant configurations.

The failure to follow

procedures .is a violation of Technical Specification 6.8.1 which

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requires that written p ecedures be implemented.for electrical

systeens.which is listed in A

ndix- A, Section 3.5 of Regulatory

Gu W M 3 (346/90009-02(DRP

tiF4))22,1990,

at about 8:00 p.m. while lining up Decay Heat Remeval

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(04 Pump No. I to m lrculate to-the Borated Water Storage Tank

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(BWST , approximately 15O ga71ons of reactor coolant was inadvertently-

discharged into the BWST from the pressurizer. .The licensee found

that the suctions of both Decay Heat (Dli) systees (DH-32 and DH-33)

were open. These' inlet valves;from the makeup an purification

system cross connected both decay heat loops. When the discharge

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isolation valve to the BWST (DH-66) was opened, reactor coolant

flowed from operating DHR Loop No. 21through: the make-up 'and;

purification system. through DHR' Loop. No. I and into the, BWST. LThe

licensee has documented this event in Potential Condition Adverse to

Quality (PCAQ) 90-0437.

Review-of the event reveals that affected;

procedures could be more clear in giving direction.:

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Section 14 of Procedure DB-0P-06012 " Decay Heat and Low: Pressure

Injection Operating Procedure", is used to lineu(DH Pump 1-1 to the-

BWST.

Section 14.1.1 has a caution to'be sure t1at DH pump suction

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valves are closed before opening test flow valves ~to ensure that

water cannot be forced from the reactor coolant'-system (RCS) to:the -

BWST.

Section 14.2.3 requires the operator to perform valve:

verification ~ list B-l'unless otherwise directed by the' Shift

Supervisor.

Vertification list B-1 lists valve ~DH-33 to be in the

closed position. The assistant shift: supervisor decided that this

step was not applicable as he believed.the valve. lineup to be as

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described in verification. list B-1.

However, both DH-32 and:32 were

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found open. This is an apparent violation'since the operators did

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not follow the procedure as req'uired by' Technical Specification 6.8.1 in that they did not verify the' pos' tion of

DH32and33(346/90009-03).

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On May 27, 1990, at about 00:03 a.m. , while. setting up to perform an-

Integrated Safety Features Actuation System (SFAS) test; operators

were again lining up DHR Loop No. 1 in a recirculation mode in

accordance with procedure DB-0P-03136, " Decay Heat Pump #1 Quarterly

Pump and Valve Test.". Section 5.1.1'.d requires DH66 to be opened-

,and section 5.1.1.b requires DH 68 to be opened.

When DH 68-was opened,

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pressurizer level dropped approximately 65 inches (1600. gallons)

before DH-66 was closed.

In this' event, theLDH loop 1 suction

valve (DH1517) to the reactor coolant system (RCS) was open when the

operator opened DH-68 (this valve is in series with DH-66).

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RCS pressure at.approximately 45 psig and the BWST'at atmospheric

pressure, a flow path existed from the RCS through DH loop 1 piping

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to the BWST via the open DH' loop-1 suction valve from the RCS.

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operator closed the discharge valve-to the-BWST and the pressurizer-

was refilled.

The root = cause of loss of pressurizer level appears

to be that the procedure was inadequate because it required DH-66 and

DH-68 to be opened with the DH loop 1 suction valve to the RCS open.

However, in preparing for this evolution the operators had an opportunity

to review the lineup and identify this procedural weakness. The

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procedures in use have a precaution regarding the potential for cross

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connecting the BWST with the RCS. An adequate review of the lineup

and precautions in the procedure could have prevented this event.

The licensee documented the event in PCAQ 90-0437. This is an

a] parent violation of Technical Specification 6.8.1 which requires.

t1at written procedures shall be implemented covering operation 'of -

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safety-related systems (346/90009-04).

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On May 30, 1990, at about 5:30 a.m., equipment operators started the

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motor driven feedwater pump to perform feedwater system clean up and

oxygen reraoval. The control- room operator raised hotwell level

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several times, -indicating that water was -leaving the system.

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the shift. supervisor requested that the system be checked for leakage,

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the equipment operators found water issuing from'the condensate

storage tank (CST) vent line and draining to the floor drain. A

minimum recirculation line on the discharge of the motor driven feed

pump, by procedure, was directed to both the deareator storage tank

and the CST.

A minimum flow rate of 180 gpm passed through the line

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for at least 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> before pumping operations were secured at about

1:40 p.m.

The licensee estimates that approximately 30,000 gallons

of water issued from the CST into the floor drains and into the

training building pond.

No detectable' radioactivity was; discharged

into the pond, but the water was chemically contaminated with-

approximately 3 ppm hydrazine. The. licensee informed the Environ-

mental Protection Agency (EPA)- of the chemical. release- to the pond.

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Seven events occurred between April 25 and May 29,-1990, which have-

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caused the inspectors to be concerned. The' events were:

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CoreSupportAssembly(Paragraph 4)..liftradiationexposure-(Paragraph

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Reactor vessel drain

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Safety Features Actuation System actuation (Paragraph 4 and 7).

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Twopressurizerleveldecreases(Paragraph 4).

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Steamgeneratoroverfill(Paragraph 10),

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Condensate storage tank overfill (Paragraph 4).

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Collectively these events indicate weaknesses in task management

and planning. They also indicate operational and procedural

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weaknesses.. The inspectors' concluded that most were caused by

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inattention to detail and by making assumptions without

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verification. The inspectors have concluded that for several of

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the events the responsibility must be shared by more than one.

organization (i.e., operations, maintenance,outageplanning).

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inspectors' concerns were elevated after.five events occurred in

a 12-day period. Collectively, these events total 5 ap)arent

violations relating to a management breakdown and will ae reviewed

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regarding enforcement' action,

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On May 30, 1990,- the Plant Manager stopped'all work affecting plant

operations.. Work could only be-implemented after review by the

shift supervisor or shift managera

It was planned that work effort

would increase' gradually to give. j! operatorsian opportunity to

regain control.

Operations management met with all crews and each

crew met separately to discuss recent events and possible actions to

prevent recurrence.

The inspectors observed that operations

managers emphasized that successful operation required-all operators.

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to maintain a constant high level of vigilance and-personal

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responsibility for the proper conduct of all plant activities. On

June 1, 1990, the licensee discussed these events-and its: corrective:

actions with-Region III staff.'

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The inspectors will provide augmented coverage during restart _to.

observe and evaluate licensee performance.

Restart is expected.to.

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occur during the next inspection period,

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b.

Off-shift Inspection of Control Rooms

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The inspectors performed routine inspections of the control. room

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during off-shift and weekend periods; these included inspections 7

between the hours of 10:00 p.m. and 5:00 a.m. _ The: inspections were

conducted to assess overall crew performance and, specifically,

control room operator attentiveness during night shifts.

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The inspectors determined that both licensed and non-licensed

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operators were alert and attentive to their duties, and that the

administrative cor.trols' relating to the conduct of operation _were

being adhered to.

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Operator Requalification-

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From May 16 to May 24, 1990, the licensee gave its requalification

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examination to 20-licensed operators. This was'the first use of' thel

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new NRC examination method _ Region III operator-licensing examiners

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observed the requalification examination and' evaluated the" examination

process. The. examinees included two onshift crews land:three, crews of

offshif t personnel.

Four individuals failed to requalify.' 'Three-

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failed the written examination, and one failed the simulator section.-

The individuals who failed will be remediated and retested before

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being allowed to perform licensed duties.

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d.

ESF System Walkdown

The operability of selected engineered safety features was confirmed,

by the inspectors during walk-downs of the accessible portions' of

several systems.

The following items were included:

verificatior,

that procedures match the plant drawings, that equipment,_

instrumentation, valve and electrical breaker line-up status was .in:

agreement with procedure checklists, and verification that locks,

tags, jumpers, etc., were properly attached and identifiable.

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The following systems were walked down during this inspection

period:

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480 Volt-AC Electrical Distribution System

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Component Cooling llater System

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Emergency Diesel Generator-System

DC Electric Distribution System

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Service Water System

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c.

Plant Material Conditions / Housekeeping

The inspectors performed routine plant tours to assess

material conditions within the plant, ongoing quality activities

and plant-wide housekeeping.

Housekeeping.is good for an outage.

However, a housekeeping violation was~ identified and is discussed

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in Paragraph 7.

Plant deficiencies were appropriately tagged for_ deficiency

correction.

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No other violations or' deviations were identified.

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Refueling (60710)-

On April 27, 1990, the licensee commenced refueling operations. The-

inspectors observed operators performing fuel handling activities and.

noted that refueling practices,and radiological controls were in place.

Refueling of the reactor was completed on April 29, 1990._ The licensee

entered Mode 5 on May 4,1990,- at _7:22 p.m. and a vacuum was drawn in-

the condenser on May 14, 1990.

No violations or devistions were identified.

6.

Radiological Controls (71707, 92720, 84750)

The licensee now estimates a total dose for the outage of 470. person-rem

and 500 person-rem for the year.

However, the dose' for the outage will

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exceed the licensee's revised estimate as the total, dose was 470. person-rem

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at the end of the inspection. period. The most significant' contributors,to

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this- dose level are the tasks associated with- the steam. generators, _

pressurizer, reictor vessel bolt replacement and reactor coolant pumps,

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as well as the high pressure nozzle and inservice inspections.

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The-inspectors toured the emergency containment sump area on May 11,

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1990, and noted that an alarming dosimeter had: fallen into the: area. The

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inspectors notified the licensee of this fact. The licensee has remove'd-

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the dosimeter # rom the sump and.is investigating the cause. Work in .

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containment is nearly complete and containment closure is scheduled for

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May 31,-1990.

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The licensee's radiological controls and practices were routinely observed

by the inspectors during ~ plant' tours and during the inspection of selected

work activities. :The inspection included direct observations of health

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physics (iP) activities relating to radiological surveys and monitoring,

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maintenance of radiological control signs and barriers, contamination,.

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and radioactive waste controls. The inspection also included a routine

review of the licensee's radiological and water chemistry control records

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and reports.

Health physics controls and practices were satisfactory.

Knowledge and-

training of personnel were satisfactory;

No violations or deviations were. identified.

7.

Maintenance / Surveillance (37828, 61726, 62703, 37828, 60710; 73756,

92701, 93702)

Selected portions of plant surveillance, test and maintenance activities

on systems and components important'to safety were observed or reviewed

to ascertain that the activities were performed in accordance with approved

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procedures, regulatory guides, industry codes and standards, and-the

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Technical Specifications.. The following items were considered during these

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inspections:

limiting conditions for operation were met while components-

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or systems were removed from service; approvals were obtained prior'to

initiating work; activities were accomplished using approved procedures

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and were inspected as applicable; functional testing or calibration was

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performed pri7r_ to returning the components or systems to service; parts

and materials used were properly certified; and appropriate fire prevention,

radiological, and housekeeping conditions were maintained,

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flaintenance

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The reviewed maintenance activities included:

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Control room annunciator panel modification.

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Inspection and repair of main steam' check valves.

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Troubleshooting of service water (SW) flow control valve-

(SW1424) for component' cooling water to SW' heat exchanger.

Troubleshooting of containment wide' range sump level

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indica tion.

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Installation of new essential inverters.

Replacement of auxiliary feedwater (AFW) Valves AF599 and

608.

On May 16, 1990, the inspectors toured the AFW pump room and observed

. that the cavitating venturi was removed from the _ AFW pipe.and stored:

end up. The upward . facing end of the venturi was not protected by any

cleanliness covers and its internals were observed to be dirty.

DB-MN-00005, " Housekeeping Control," Rev 0, dated May 24, 1990, requires

that openings be covered to prevent foreign materia'l from entering in

areas from which-retrieval would be difficult. The maintenance manager

was notified of this condition.

Remedial action was to clean the venturi

prior to its installation back to the AFW system. Additional corrective

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action was to counsel the personnel involved in this activity. The

inspectors noted the following day that a cleanliness cover was installed

on the venturi. Thisisaviolation'(346/90009-05(DRP))ofTS6.8.1,

failure to properly implement DB-11N-00005.

The root cause of this

violation was inattention to detail.

The violation is not being cited

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because the criteria specified in 10 CFR 2 Appendix C, Section V.A.

of the Enforcement Policy were satisfied (isolated Severity Level V).

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b.

Surveillance

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The reviewed surveillances included:

Procedure No.

Activity

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DB-MI-03013

Test of RPS and Reactor Trip Breaker

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DB-MI-04109

Source Range Functional Test

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DB-MI-09049

Test of the Incore to the liultiplexer.

DB-SC-03114

SFAS Integrated Time Response Test _

DB-SC-04024

13.8 KV Bus lockout Test

DB-SC-04052

4160 V System Transfer and Lockout

Test Busses D1 and D2

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DB-SC-04053

4160 V System Transfer and. Lockout Test

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Busses C1 and C2.

During the performance

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of this test, electrical-loads were shifted

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from Bus C1 to prevent them from losing power

during the test. One load was Y-3, one of

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four 120 VAC essential instrument busses.

The operator who was sent to transfer this

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load apparently used the wrong section of

the operating procedure, so:Y-3, although

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supplied via a different motor control

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center was still powered from C1. When the

test was performed,-Y-3 lost power. This

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deenergized Channel 3 of_ SFAS, providing

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a-trip signal.

Since liaintenance had

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previously inserted a. trip signal in

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Channel 1 of SFAS, the SFAS received

the two of four trip signals required'for

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an actuation even though there was no plant _.

condition requiring an SFAS actuation.

All

safety equipment functioned as required

resulting in an injection of approximately

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1000 gallons to the reactor coolant- system.-

The safety injection lasted for about

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6 minutes. After the event, the licensee

recognized that during the injection it was

in an Unusual Event and made'the appropriate

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notifications.

The inspectors are continuing

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their review of this item which will include-

revfew of.the relevant Licensee Event Report

when+ issued.

DB-SC-04109,

EDG Air Compressor 2 Charging Test-

DB-SP-04153

Auxiliary Feedwater Pump Turbine 1

Overspeed Trip Test

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Personnel performing = maintenance or surveillances used correct procedures

and proper work- control documents. Work authorization had been obtained

for the jobs performed.' _ Prerequisites for performing the job, such as

worker protection and tagging had been' performed.. Surveillance continues-

to be 'an area where only an: occasional problem arises.

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No other cited violations'or-deviations were identified.

8.

Emergency Preparedness (71707, 82701)

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An inspection of emergency preparedness activities was performed to

assess the licensee's implementation of'the. emergency )lan and

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implementing procedures.. The ~ inspection: included mont11y observation

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of emergency facilities and equipment, interviews with' licensee staff,

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and a review of selected emergency implementing procedures,

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No violations or deviations were identified.

9.

Security (71707, 81070,- 81052)

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The licensee's security activities-were observed by the inspectors during-

routine facility tours and during. the inspectors': site arrivals 'and:

departures. Observations included the security personnel's performance

associated with access control, security checks.:and surveillance

activities, and focused 'on the adequacy o_f security. staffing, the

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security response (compensatory measures), and the' security staff's

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attentiveness and thoroughness.

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Security personnel were observed to be alert at their posts.. . Appropriate

compensatory measures were established. in a timely manner. . Vehicles-

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entering the prot (cted area'were thoroughly searched.

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No violations or deviations were identified..

10.

Engineering and Technical Support (37828, 62703, 71707, 92701, 92720)

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An inspection of engineering:and technical support activities was

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performed to assess the adequacy of support functions associated

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with operations, maintenance / modifications, surveillance and testing

activities.

The. inspection. focused on' routine engineering-involvement-

in plant operations and response to plant problems. .The inspection

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included direct observation of engineering support activ'ities and

discussions with engineering, operations, and maintenance personnel..-

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The licensee determined that leakage existed on the reactor vessel head

vent at a flanged joint on steam generator (SG) 2.

An investigation

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revealed that the Flexatallic gasket installed was of the proper

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dimensions but of the wrong material and pressure rating.

In addition,

the joint had a smooth gasket seating surface instead of the vendor

recommended ' phonographic' finish.

The licensee has machined the flange

seating surface and has installed the proper Flexatallic gasket.

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stock' code and design drawing properly identified the gasket dimensions,

but failed to correctly identify the pressure rating, material, and the

intended application of the gasket. These failures were the root cause

which resulted.in the installation of the incorrect gasket. The stock

code and the design drawing have both been modified. The licensee's

research reveals that no other joint was assembled using a gasket of a

lower pressure rating than specified.

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On January 22, 1990,. the licensee reduced reactor power and removed

reactor coolant pump (RCP) 2-2 from service due to high vibrations. A

failed motor bearing was identified as the cause of the high vibrations.

The licensee believes that the lower motor bearing failed due to-rotor

imbalance, pump / motor misalignment, poor bearing shoe fit up, non-

concentricity of the shaft journal and/or circulating electrical

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-currents between the shaft stator via the lower bearing shoes.

RCP 2-2

was repaired during the refueling outage and an inspection plan for the

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other RCPs has been developed.

Prior to the performance of DB-PF-10100, " Hydrostatic Test of SG 1-1",

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erformance engineering was concerned that venting the steam generator

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p(SG) during the filling evolution would possibly cause airborne

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contamination to be released and issued a change to the procedure to

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vent the SG to the gaseous rad waste system.

While filling these on

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May 23, 1990, the-gaseous rad waste vent line became congested and

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develo)ed a back pressure.

In addition, the. gaseous radiological waste

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tanks 1ad a 3.5 psi cover gas which also provided a back pressure to

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the vent line. The operators were monitoring flow into the SG and SG

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water level. They were filling the SG with the motor _ driven feedwater

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pump and controlling level increase by opening a valve which allowed

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water to flow back to the main condenser.

Procedurally-SG' water level

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was to be maintained at approximately 610 inches. When indicated level

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stopped increasing below the desired level, the operators thought this

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was due to the volume of water flowing back to the main condenser.

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However, actual SG water level was greater than the indicated level

(the SG was full).

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This faulty level indication was caused by the SG level sensor also being

vented for the plugged vent line. As a result, water flowed from a SG

atmospheric vent valve (AVV) into the Main Steam Line Room.

The Main

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Steam Line room floor drains had been taped over by radiological controls

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personnel to prevent any SG effluent from entering the storm drain

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sys tem. At least 4000 gallons of water issued from an AVV to the Main

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Steam Line room before the evolution was stopped. At least 2000 gallons

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of this water leaked from the Main Steam Line room and flowed into the-

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electrical and mechanical penetration rooms below. The shift supervisor

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uncovered a taped floor drain to prevent the' water from flowing into the

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electrical penetration room. He thought that the floor drain discharged

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to the auxiliary. building drain system where it could'be collected and -

treated before discharge. He was unaware that these drains.went to the

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storm drain system.-_A minimum of 2000 gallons _of water entered the storm

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drain'which discharged to the COB _po_nd.

Trace amounts of. radioactivity

were detected in the effluent and at.the storm drain radiation monitor.

Operators closed the outlet valve from the COB ~ pond to prevent a release

outside the owner controlled area. The pond was sampled for radioactivity.-

No radioactive contamination was detected in tne' pond.

The root cause

of this event is a failure of performance engineering to properly vent

the SG and to assess its affects on the SG level indicating system.

Review by the inspectors indicates that the licensee's review of the

procedure was inadequate because the effect of the containment vent

header pressure was not identified and-the-absence of a quantitative

value for drain capacity was not corrected. The procedure was also

deficient because there was'no requirement to use redundant level

-indication and there was no requirement to monitor the MS line vents-

during the fill.

This is an apparent violation of 10 CFR 50, Appendix B, Criterion V

which requires that activities affecting quality shall be prescribed

by documented instructions or procedures of a type appropriate to the

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circumstances (346/90009-06). Procedure DP-PF-10100, " Steam Generator 1

Rydrostatic Test," was not appropriate to the circumstances in that it

did not evaluate the effects of connecting.the steam generator level-tap'-

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to the containment vent line, nor did it require diverse level indicators-

or the monitoring of open vents.

No other violations or deviations was identified.

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Safety Assessment / Quality Verification-(35502, 92701', '92720, 30703,

35702, 92720, 35701, 92700, 90712)

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An inspection of the licensee's' quality programs was performed to assess

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the implementation and effectiveness of programs associated with management

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control, verification, and: oversight activities. The inspectors considered

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areas indicative of overall management involvement in quality matters,

self-improvement programs, response.to regulatory and industry initiatives,

the frequency of management plant tours and control room observations,. and

management personnel's participation in technical and planning meetings,

The inspectors reviewed Potential Condition Adverse to Quality Reports

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(PCAQR), Station Review Board (SRB) and Company Nuclear-Review Board

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meeting minutes, event critiques, and related documents; focusing on

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the licensee's root cause determinations and corrective actions.

The

inspection also included a review-of quality records and selected quality-

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assurance audit and surveillance activities.

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On April 26, 1990, Cresap, Inc. issued its report on'the results of

its management review of the Centerior Energy Corporation.

Cresap

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recommended that Centerior be restructured into three groups; Power -

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Generation, Customer Operations, and Finance and~ Administration.

The

recommended changes for Davis-Besse were minimal.

The inspectors will

continue to monitor actions related to the. proposed changes and their

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effects.

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12.

Enforcement Conference (30702)

On June 1, 1990, an enforcement conference was held in Region III to

discuss the events surrounding the April 25, 1990, core support assembly

(CSA) lift and the draining of the refueling canal on May 1,1990.- These

events are described in Inspection Report No. 50-346/90012(DRSS).

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licensee also described subsequent events (described in Sections 4 and 11

of this report) and-their overall corrective action program. A

supplemental enforcement conference was held by telephone on July 17,

1990, to discuss potential escalated enforcement for apparent violations

described in Sections 4 and 11 of this report and other violations

-described in Inspection Report No. 50 -346/90013(DRP).

The enforcement

conference will be documented in Inspection ~ Report No. 50-346/90014(DRP).

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13. Commissioner Visit

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On May 7.-1990, Commissioner Rogers and.the Director of the Division of

Reactor Projects Region III met with the inspectors and senior licensee

management and members of their staff and toured the facility,

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Violations for Which a " Notice of Violation" Will Not Se Issued

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The NRC uses the Notice of Violation (NOV) as a standard method for

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formalizing the existence of a violation of a legally binding requirement.

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However, because the NRC wants to encourage-and support licensees'

initiatives for self-identification and correction of problems, the NRC

will not generally issue a Notice of Violation _ for an issue that meets

the tests of 10 CFR 2, Appendix C, Section V.G.I.

These tests are:

(1) the issue was identified by the licensee;_ (2) the issue would be

categorized as Sev_erity Level -IV or V violation; (3) the issue was reported

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to the NRC, if required;.(4) the issue will be' corrected,' including-

measures to_ prevent recurrence, within a reasonable time period;-and

(5) it was not an issue that could reasonably be expected to have been

prevented by the licensee's. corrective action for a previous violation.

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In addition, in accordance with Section V.A. of the enforcement policy,

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for isolated Severity Level V violations, a . Notice of Violation normally

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will not be issued regardless of who.idertifies the violation provided-

that the licensee has initiated appropriate corrective action before'

the inspection ends.

Issues. involving the failure to meet regulatory

requirements,' identified during the inspection, for which a Notice of

Violation was not issued are discussed in Paragraphs 3 and 7.

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ExitInterview(30703)

The inspectors met with licensee representatives (denoted in Paragraph 1)

throughout the inspection period and at the conclusion of the inspection

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and summarized the scope and findings of the inspection activities.

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addition, a conference call was, held on July 17, 1990 to discuss the

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apparent violations identified during this inspection period.

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licensee acknowledged the findings. After discussions with the licensee,

the inspectors have determined there is no proprietary data contained in-

this inspection report.

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