ML20058A175

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SALP Repts 50-348/93-14 & 50-364/93-14 for Period 920531- 930925
ML20058A175
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 11/12/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20058A177 List:
References
50-348-93-14, 50-364-93-14, NUDOCS 9311300141
Download: ML20058A175 (6)


See also: IR 05000348/1993014

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SALP REPORT - FARLEY NUCLEAR PLANT

50-348/93-14 & 50-364/93-14

I.

BACXGROUND

The SALP Board convened on October 13, 1993, to assess the nuclear safety

performance of Farley Nuclear Plant (FNP) Units 1 and 2 for the period May 31,

1992 to September 25, 1993. The Borrd was conducted pursuant to NRC

Management Directive (MD) 8.6 (see NiC Administrative Letter 93-02).

Board

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members were Albert F. Gibson (Board Chairman), Director, Division of Reactor

Safety, NRC Region II (RII); J. Philip Stohr, Director, Division of Radiation

Safety and Safeguards, NRC RII; Jon R. Johnson, Deputy Director, Division of

Reactor Projects, NRC RII; and S. Singh Bajwa, Acting Project Directorate II-

1, NRC Office of Nuclear Reactor Regulation.

The performance category ratings and the assessment functional areas used

below are defined and described in RC MD 8.6, " Systematic Assessment of

Licensee Perfcrmance (SALP)."

II. PERFORMANCE ANALYSIS - OPERATIONS

During the previous assessment period a decline in performance was noted in

the operations area. A significant number of personnel errors and equipment

malfunctions had resulted in challenges for operators to respond to reactor

plant transients. Management challenges were noted with reducing the number

of plant transients, personnel errors, and improving log keeping.

Configuration control was weak both at power and during plant shutdown

conditions.

During this assessment period the licensee corporate and station management,

as well as the operations staff, increased attention to these areas.

Management remained knowledgeable of emerging issues and participated in key

decisions. Periodic meetings were held among plant management and also with

station staff.

Plant management continued to disseminate plant and industry

event information to station employees. Control room professionalism was

maintained at a high level; the control room was quiet and the number of

operating parameters in alarm (lit annunciators) was small

(usually less than

five). New procedures were implemented late in the period to further improve

control room formality and communications. Computerized plant equipment

parameter logkeeping was initiated allowing more effective trending of

equipment. Overall operational performance of the two units improved this

period as indicated by a marked reduction in the number of reactor protection.

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system actuations: two this period (one manual and one automatic) compared to

15 last period (four manual and 11 automatic).

The Operations staff remained stable and well qualified. .0perations training

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programs were re-accredited, and licensed operator requalification program

implementation was excellent.

Licensee management provided support for

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operations group team building training to improve overall performance.

Operators were sent on visits to other power plants to observe control room

operations. Trip reports summarizing new ideas for control room conduct were

9311300141 931112

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distributed as part of a weekly operation % euartment newsletter.

In

addition, overtime was significantly reduced from a past practice of up to

12-hour days, seven days a week during outages, to a 1992 average of about

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> / week and in 1993 an average of about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> / week.

This showed direct

involvement by operations management to improve working conditions and

operational performance.

During this period, self identification of operational errors was excellent.

Most procedural violations were identified by the licensee, or were self

disclosing and for which corrective actions were prempt.

Plant management

became directly involved with discussions regarding the root cause of

personnel errors. The licensee audited the effectiveness of control room

attentiveness and logkeeping, two areas discussed in the previous assessment

report. Comprehensive troubleshooting was performed in response to an anomaly

with the turbine driven auxiliary feedwater pump suction pressure, and good

self-identification of questionable traceability of lubricating greases was

noted by plant operators.

Plant equipment configuration control and personal errors continued to be a

challenge. .During a forced outage of Unit 2 in February 1993, there were two

instances of unplanned safety injection: one due to improper valve

sequencing, and the other due to improper testing. Although wrong-unit,

wrong-train events continued during this period, their number and safety

significance (including duration) decreased. An incorrect auxiliary feedwater

remote control switch was operated during testing but promptly corrected; and

the wrong diesel generator circuit breaker was opened but annunciated in the

control room and was promptly corrected. An improper lineup for the Unit 2

containment component cooling water system in September 1993, (and a recent

event outside the SALP period involving interruption of component cooling to

the spent fuel pool) indicated a continuing weakness in the area of

configuration control.

The Operations area is rated Category 1.

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III. PERFORMANCE ANALYSIS - MAINTENANCE

In the previous SALP,. maintenance was rated Category 2.

While generally good

performance was demonstrated, there were instances of inadequate supervisory

oversight, declining equipment material conditioas, and weaknesses in

procedural adherence.

During this SALP assessment period, NRC staff observed that performance

generally improved in the maintenance area. The licensee took initiatives to

improve plant lighting, reduce leaks, and improve plant material conditions,

all of which contributed to an improved maintenance program and a reduction in

the backlog of maintenance work orders.

In addition, strong maintenance

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support contributed to improved equipment performance, as evidenced by

significantly fewer reactor trips and forced shutdowns.

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There were a number of examples of improved management attention which

contributed to a high level of safety performance.

Following the lightning

strike on July 1, 1993, the prompt identification and repair of the

circulating water pump motor damage showed the capability of the maintenance

team to perform a difficult task under tight schedular restrictions with a

minimal adverse affect on the plant. Management implemented several positive

initiatives to enhance maintenance performance.

Examples included a reduction

in overtime during outages, the pre-release work control process, continued

use of the maintenance support engineering group, sending maintenance

personnel to team building sessions, the stop, think, act, review (STAR)

program, and maintaining a 24-hour presence of a maintenance shift supervisor

on site.

Improved steam generator eddy current surveillance and analysis

techniques were strengths. The licensee also significantly improved the

avaflability of the emergency diesel generators during the assessment period.

Individual events detracted from the generally improving good performance.

Several events were attributed to personnel errors and lack of procedural

adherence.

Examples included improper disassembly and assembly of the

component cooling water pump motor bearings, improper installation of valves

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in the emergency diesel generator air compressors, improper use of electrical

jumpers during surveillance testing that resulted in two engineered safety

feature actuations, use of the wrong data table during performance of a

nuclear instrumentation calibration, and erroneous removal of the output

breaker from the wrong unit emergency diesel generator. Most of these events

occurred during the first portion of the assessment period and the licensee's

measures to improve communication, teamwork, and self-verification had a

beneficial impact on reducing the frequency of these events. However, at the

end of the assessment period, two more events occurred (inadvertent breaching

of tiie control room pressure boundary and operation of the wrong motor-

operated valve during MOVATS testing) that indicated this challenge remained.

Root-cause evaluations and corrective actions were generally good.

However,

during the assessment period, the licensee failed to identify the root cause

of continuing instrumentation calibration problems and to take timely

corrective action.

For example, the licensee failed to identify the cause of,

and take timely corrective action for, emergency diesel generator load

sequencer timing relays that were out of calibration and failed to require

evaluations for as-found out-of-tolerance readings as part of the calibration

check program for service water instrumentation.

Maintenance performance improved during this period. The qualification and

skill level of craft personnel contributed significantly to the overall

excellent plant material condition and equipment reliability.

However,

challenges remain to reduce personnel errors and provide more attention to

detailed planning before performing maintenance work.

The Maintenance area is rated Category 2.

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IV. PERFORMANCE ANALYSIS - ENGINEERING

In the previous SALP period engineering was rated Category 2 with an improving

trend,

Strengths during that period included a well qualified staff,

effective self-initiated assessments of safety systems, and improved support

to operations and maintenance staffs. Challenges included a design control

problem associated with the RTD bypass loop modification and inadequate

incorporation of setpoint tolerances in associated drawings.

The qualifications of the engineering staff remained a strength during this

SALP period.

Excellent knowledge of regulatory requirements and plant design

bases was evident in licensing submittals and during inspections conducted by

the NRC.

Knowledgeable site and corporate engineering staffs aided in the

resolution of problems and in the completion of several design changes to

inprove the station electrical distribution system.

Management emphasized improvements in plant safety and risk reduction during

operation and outages.

Steps to reduce risks identified by probability risk

assessment were included in operating procedures, and a program to ensure

reliable decay heat removal during outages was implemented.

The fuel was

removed from the reactor in order to reduce the duration of mid-loop

operations which reduced risk. Outage activities were prioritized and

scheduled to reduce risk.

Strong design control was applied to safety related equipment.

Drawings were

legible and accurate; the design bases of service water and electrical

distribution systems were well documented; safety evaluations performed

pursuant to 10 CFR 50.59 were adequate, and plant modifications were properly

designed.

Effective self-assessments continued during this SALP period.

Strengths noted

included overview and audits of site engineering by the Corporate Nuclear

Operations Review Board; and reviews of design outputs by the Technical

Adequacy Review Board and the Design Adequacy Review Committee.

Engineering

reviews identified design deficiencies in service water and electrical

distribution systems; and, except as noted below,-engineering support for

resolution of these deficiencies was effective.

Strong support was generally provided for the maintenance of plant equipment,

but this support was not fully effective in addressing failures in the areas

of instrumentation and controls.

Strengths included:

Use of thermography,

vibration analysis and time domain reflectometry on emergency diesel

generators; development and implementation of an effective, conservative

program for eddy current inspection of steam generator tubes; and,

strengthening of the program for maintenance and surveillance of motor

operated valves.

However, problems occurred in the area of instrumentation

and controls because of the failure to identify and correct the causes of

these problems.

In summary, overall performance in the area of Engineering continued to

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improve this period.

Strengths were noted in staff qualifications, risk

management, design control, and self-assessments.

Support to maintenance

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remained strong except for evaluation and correction of failures in the

instrumentation and control area.

The Engineering area is rated Category 1.

V.

PERFORMANCE ANALYSIS - PLANT SUPPORT

This new functional area consolidates assessments of plant support activities

that were previously provided in several different functional areas. The new

area includes assessments of radiological controls and chemistry (rated

category 1 in the previous SALP), emergency preparedness (previously category

2), security (previously category 1) and fire protection and housekeeping (not

individually rated in the past).

Radiological exposures, both external and internal have been effectively

controlled this period. A comprehensive program for maintaining radiation

exposures as low as reasonably achievable resulted in a reduced source term

and has been a significant factor in the effectiveness of internal and

external exposure control programs.

Examples included reducing the rate of

plant shutdown to reduce the spread of activation products throughout the

reactor coolant system (soft shutdown), teledosimetry and submicron

filtration.

The 1992 collective dose of 805 persan-rem was largely associated

with outage work and considered consistent with outage activities.

Radiological effluents were well controlled during this period, and

radioactive waste was well managed.

Effluent release concentrations were well

within Technical Specification limits, and offsite doses were only a fraction

of a percentage of regulatory limits.

The environmental monitoring program

confirmed the low concentration of radioactivity in effluent from the site.

The licensee has been proactive with respect to management of solid

radioactive wastes and has significantly reduced waste volumes by safely

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packaging and shipping them to an authorized disposal facility.

In general,

root cause evaluations and corrective actions for problems improved this

period, however there were problems concerning evaluation of batch liquid

releases and adherence to Radiation Control procedures.

The facility's emergency re:ponse capability was maintained in a good state of

readiness this period.

Performance improvements were noted in the emergency

preparedness area. The licensee maintained good working relations with;

offsite emergency preparedness authorities.

The annual exercise was

successful, and no exercise weaknesses were observed.

The licensee used a

series of drills, a number of which were above regulatory requirements, to

enhance the level of preparedness. These drills demonstrated that the program

was well supported by licensee management. Additionally, emergency response

management demonstrated a wide ranging familiarity with emergency response

methodology which contributed positively to the level of performance. During

the period, the licensee made significant progress toward meeting NRC criteria

relative to addressing the previously NRC identified issue concerning timely

staffing and activation of the E0F. To achieve this the licensee revised the

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response concept, implementing procedures, made necessary E0F modifications,

and provided additional training to the staff.

The security program continued to be effectively implemented this period.

Performance was improved as a result of a noteworthy training program which

included realistic drills and a thorough critique process. A high level of

management support was evidenced this period by improved weaponry and response

equipment and other programmatic improvements. During the later portion of

this assessment period, the NRC identified problems with the recently required

access authorization program.

The fire protection program was effectively implemented this period.

Ignition

sources and combustible material were well controlled, and the installation of

a new jockey pump in the fire main system resulted in an improved stable fire -

main system operating pressure.

A major contributor to the superior level of safety performance in the plant

support area was a strong level of management support and effective, well

administered training programs in the areas of emergency preparedness,

security, fire protection, and radiation protection.

Housekeeping has been improved during this period.

Maintenance has reduced

the number of small leaks, and the repainting program progressed.

The Plant Support area is rated Category 1.

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