ML20055A626

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Monthly Operating Rept for June 1982
ML20055A626
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 07/12/1982
From: Bogart D, Culver M
FLORIDA POWER CORP.
To:
Shared Package
ML20055A625 List:
References
NUDOCS 8207190262
Download: ML20055A626 (4)


Text

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OPERA 11NG DATA REPORT DOCKET NO.

50-302 DATE 7/1/82 C051PLETED BY D.

Bonart TELEP110NE (904) 795-6486 OPERATING STAT 1JS

1. Unit Name:

Crystal River Unit #1 Notes

2. iteporting Period:

6/1/82 - 6/30/82

3. Licensed Thennal Power (51Wt):

2544

4. Nameplate Rating (Gross alWe):

890

5. Design Electrical Rating (Net SIWE): _825
6. Slaximum Dependable Capacity (Gross 31We):

845

7. Staximum Dependable Capacity (Net 31We):

806

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

N/A

9. Power Lesel To Which Restricted,if Any (Net 51We):

Approximately 2300 MW thermal.

10. Reasons For Restrictions,1f Any:

Restricted to 2300 MW thermal due to RC Pump Power Monitors being bypassed. Net MWe corresponding to this varies with cycle efficiency.

This Slonth Yr.-to-Date Cumulative f

i1. Ilours In Reporting Period 720 4344 46464

12. Number Of Ilours Reactor Was Critical 703.7 3379.5 28828.89
13. Reactor Reserve Shutdown flours 4.2 19.9 1229.12
14. Ilours Generator On Line 698.1 3339.6 28151.78
15. Unit Reserve Shutdown flours 0

0 0

16. Gross Thermal Energy Generated (SIWil) 1451344 7539000 62905941
17. Gross Electrical Energy Generated (51WII) 489790 2563074 21362665
18. Net Electrical Energy Generated (SIWil) 463686 2437844 20267142
19. Unit Service factor 97.0%

76.9%

60.6%

20. Unit Availability Factor 97.0%

76.9%

60.6%

21. Unit Capacity Factor (Using 51DC Net) 79.9%

69.6%

55.6%

22. Unit Capacity Factor (Using DER Net) 78.1%

68.0%

52.9%

21 Unit Forced Outage Rate 3.0%

23.1%

26.2%

24. Shutdowns Scheduled Oser Next 6 Slonths(Type. Date.and Duration of Each):

None

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

7/1/82

26. Units in Test Status (Prior to Commercial Operationi:

Forecast Achiesed INill \\ L CRITICA LITY 1/14/77 INIIIAL ELECTRICITY 1/30/77 CO\\lNIERCIAL OPER AIION 3/13/77 8207190262 820712 (9/77)

PDR ADOCK 05000302 R

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO, 50-302 UNIT FLCRP-3 DATE 7/1/82 COMPLETED BY D. Bogart TELEP110NE (904) 795-6486 MONTil June 1982 DAY

AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (Mbe-Net)

(ywe.ye,

1 744 17 619 2

703 224 gg 3

723 524 39 4

710 20 436 5

750 21 571 739 6

579 22 7

753 579 23 8

748 24 565 765 9

25 565 745 10 572 26 11 751 27 561 12 742 28 565 751 13 570 29 I4 30 524 13 740 3,

3 16 INSTRUCTIONS On :his format, list the average daily unit power lesel in MWe-Net for each day in the reporimg month. Compute to the nearest whole megawatt.

(9 /77 )

~ - -.., - -,. - - - -

d UNIT SilUTDOWNS AND POWER REDUC 110NS DOCKET NO.

50-302 UNIT NAME _FT rup_,

D ATE 7/7/82 COMPLETED BY M.W. Culver REPORT MONTil 6/82 TELEPflONE (904) 705-64R6 C

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=a O

.5 ?

s 4iX Licensee

[-r, E%

Cause & Corrective R"f Attiini to No.

D.it e g

3g g

,3 g 5 Event

=?

$5 5

j5g Report

  • N0 Prescia Recurrence 6

82-13 820617 F

17.57 A

3 N/A IA RELAYX Roof joint leak caused a ' ground fault on RC pump 'B' resulting in a reactor /

turbine RPS trip.

j 1

82-14 820618 F

A 4

N/A Hli MECFUN Power reduced to 70% to 80% power due to the loss of condensate pump IB.

1 L

82-15 820620 F

4.2 G

3 N/A CD ZZZZZZ Operator accidentally closed the Main i

Steam Isolation Valves causing reactor /

turbine trip on high pressure.

82-16 820630 F

0.13 D

1 Not written SF HANGER Discovered that conduits carrying g

yet, see next some 11PI controls were not seismically month.

qualified. Declared HPI inoperable, entered I hour action statement, manually shutdown the reactor.

I 2

3 4

F: Forced Reason:

Method:

Exhibit G - Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Piepaution of Data B-Maintenance of Test 2 Manual Scram.

Ent > Sheets for Licensee C Refueling 3-Automatic Scram.

Esent Report (LER) File INURI G-D Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Training & License Examination F Administrative 5

G-Operational Error (Explain)

Exhibit I-Same Source

)

P)/77).

Il-Other ( Explain) 4

MONTiiLY CPERATIONAL SUIStARY STATEMENT

(..'c =

DOCKET NO. 50-302 UNIT FLCRP-3 DATE 7/7/82 COMPLETED BY M.W. Culver TELEPIIONE(904) 795-6486 MONTil.. Tune 19A?

SIDS!ARY STATD!ENT:

The plant experienced three (3) forced shutdowns and one (1) major power reduction this month.

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