ML20042C352
| ML20042C352 | |
| Person / Time | |
|---|---|
| Site: | Kewaunee |
| Issue date: | 04/01/1981 |
| From: | Ruiter G WISCONSIN PUBLIC SERVICE CORP. |
| To: | |
| Shared Package | |
| ML20042C346 | List: |
| References | |
| NUDOCS 8203310269 | |
| Download: ML20042C352 (4) | |
Text
v UNIT SEUTD0V NS A 5D POV EP RED UCTIONS I
- 2 1111 DOCKET No: 50-305 DM UNIT NAME: Kevaunea-d D AT E: April 1,
1981 DU COMPLETED BY:
C.
H.
Puiter U$
TELEPHONE: 814-380-25G0 x225 Rn lEl>
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PEFORT MONTH - MARCH, 1981 Om 82 lDERATION'IBE ASON' METHCDI LEh NUMBER iS15 i COMPONENT l COMMENTS I
8 NO. 5 DATE ITYPE I
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1 3/21/811 F I 24.5 i A I 3 i
N/A I RE ] CR CRV E I
- 3. During perf orcance of scheduled bi-veckly CitDM i i
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exercising, CRDM power supply fuses blev i 1
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resulting in a
reactor / turbine trip.
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n d-o f-li f e cond it io ns delayed restart until i I
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the post-trip xenon transient was passed.
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,I TYPE SEASON EETHOD SYSTEM C COMPONENT CODES Y
F: Forced 7-Equipment Fallure (Explain) 1-M an u al From NUREG-0161 S: Scheduled B-raintenance er Test 2-Manual Scram s
C-Refueling 3-Automatic Scras E-Regula tory Restriction 4-Continuations E-Cperater Training C License Examination 5-Lead Reductions F-Adm in Lntrat ive 9-Other G-Operational Error (Explain) n-Other (Explain)
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OPEDAT ISG C ATA R EPOPT COCNET NO-50-305 e
COMPLETED BI-G.
B.
RUITER OPER AIINC STATUS TELEPHONE-414-383-2560 I225 1 UdIT N%ME KEWAUNEE e
2 REFOBTING P E BIO C MARCH, 1981
- NOTES With the exception of a 1-day outage, the unit operated at full power s
3 LICENSED THERHAL FCVER (M WT) 1650 for the entire reporting period.
4 NAMEILATE RATING (CROSS MWE) 560 5 CESIGN ELECTRICAL BAIING (N ET E W E) 535 6 NAIIEUM DEPENCAELE CAPACITY (GRCSS FWE) 545 7 MAXIrUn'CEPERCABLE CAPACITY (N ET MU E) 522 O IF Cf!ANGES OCCUR IN CAPACITY EATINGS (ITEMS MUMBER 3 THROUGH 7) SINCE LAST BEPOBT, CIVE REASONS Nome 9 POWER LEVEL TO WHICit BES1PICTEE IF ANT (NET MWE) None g
10 REASC;iS FOR DESTRICTIONS,oIP ART THIS MCNTH TR-TC-CATE CUMULATIVE 11 HOURS IN REPORTING PERICD 144 2160 59545 12 NUMDER CF HotRS R f ACTOR WAS CRITICAL 727.5 2141.7 50464.3 13 RE ACTOP BESERVE SHUTDOWN HOURS
- 0. 0 0.0 2330.5 w
14 HOURS GENER ATOR 05-LINE 719.5 2132.3 49341.2 15 UNIT RESERVE SUIDCWN !!OURS 0.0
- 0. 0 10.0 16 CROSS TI!EPMAL E)EPGY CENEP ATED (MWH) 1136912 343E294 76125518
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17 GROSS ELECTRICAL INERGY GENERATED ( RWH) 373600 1129500 25123700 s
18 NTT ELECTRICAL F"EPCY GENERATED (MWH) 355650 1077598 239085G8 19 UNIT SEPTICE FACTCR
'96.7 98.7 82.9 L
20 UNIT AV AIL AEILIT Y ! ACTOR 96.7 98.7 82.9 21 UNIT CAPACITY FACTCR (USING MCC NET)
- 91. E 95.6 76.6 22 UNIT CAPACITY FACTOR (USING DEF NET) 89.4 93.3 75.1 6
23 UNIT FOTCED OUTAGE RATE 3.3
- 1. 3
- 5. 3 v
24 SHUICOWNS SCFIDUIED CVED NEIT 6 MONTRS (TYPF, CATE, AND DifRATION OF EACU)
A refueling shutdown of 6-week duration is scheduled to start en April J1, 1981.
s.
25 IF.Snut DOWN AT END OF REPORT PERIOD, ESTIMATED D ATE OF STARTUP - N/A l
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EOCKET 50-305 KEW A'JNEE NUCLEAR PONER P LA NT SUNNARY OF OPED ATING EXP ERIENCE Ma rc h, 1981 a
OP ER ATIO NS:
On Ma rch 2, the unit was returned to full load a f ter a trip in February.
On March 12, load was reduced to 490 MW for heater drain pump naintenance. The unit was returned to full load on the same day.
g On March 21, during performance of scheduled bi-weekly CRDM exercising, CRDM pcwer supply fuses blev resu lt ing in a reactor / turbine trip. The unit was returned to full 1 cad on March 23.
MAINTENANCE:
Replaced a transistor in a feedwater flow square roct ccaverter.
3eplaced a relay in a service wa ter pump brea ker.
Re pla ced a sample punp for a containment radiation DCaitor.
Replaced bolts on Safety Injection valves.
Peplaced an oil pump on an auxiliary feedwater pump.
Replaced plungers and C-rings in a charging pump.
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A VER AG E DA IL Y
' U. Il IT F0W E B L EV E L.
DOCKET 11 0 305 Uti1T-KEW All!!EE COMPLETED BY-G.
11. RUITER TELEPH0!1E-414-388-2560 X225 REPORT M C '1T l!
MABCH, 1981 AVERAGE DAILY DAY POWER LEVEL (MW E-N ET) 1 2 10 2
434 3
512 4
511 5
517 6
5 18 7
522 8
517 9
5 16 10 5 16 11 521 12 512 13 517 14 517 15 516 16 520 17 512 IE 521 19 517 20 517 21 127 22 132 23 491 24 516' 25 515 26 5 16 I
27 516 i
28 516 29 516 30 516 31
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