ML20040G910

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IE Insp Repts 50-295/81-29 & 50-304/81-27 on 811201-820115. Noncompliance Noted:Unit 1 Operated W/Battery Charger Isolated from Bus 112
ML20040G910
Person / Time
Site: Zion  File:ZionSolutions icon.png
Issue date: 01/26/1982
From: Hayes D, Kohler J, Waters J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20040G904 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-2.B.4, TASK-2.F.1, TASK-2.F.2, TASK-2.K.3.09, TASK-TM 50-295-81-29, 50-304-81-27, NUDOCS 8202160607
Download: ML20040G910 (14)


See also: IR 05000295/1981029

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No.:

50-295/81-29; 50-304/81-27

Docket No.:

50-295; 50-304

License No.:

DPR-39, DPR-48

Licensee:

Commonwealth Edison Company

P. O. Box 767

Chicago, IL 60690

Facility Name:

Zion Nuclear Power Station, Units 1 & 2

Inspection At:

Zion, IL

Inspection Conducted: December 1, 1981 through January 15, 1982

J.5. Gtupw

[ - 2 0 ^8 2_

Inspector (s):

J. E. Kohler

. $. Y[

J. R. Waters

/ - 2.C - 8 2-

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Approved By:

I.

y s, Ch

Reactor Projects Section IB

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Inspection Summary

Inspection on December 1, 1981 through January 15, 1982 (Report No. 50-295/81-29;

50-304/81-27)

Areas Inspected: Routine unannounced resident inspection of licensee action on

previous inspection items, reactor trips, removal of battery and charger 112 from

service, Fischer Porter transmitters, inadvertent PORV opening, primary to secondary

leakage, auxiliary feedpump inoperability, 2B reactor trip breaker, ASCO valve

sticking, NUREG-0737 items, operational safety verification, monthly maintenance

observation, monthly surveillance observation and Licensee Event Reports. The

inspection involved a total of 286 hours0.00331 days <br />0.0794 hours <br />4.728836e-4 weeks <br />1.08823e-4 months <br /> onsite by two NRC inspectors including

33 hours3.819444e-4 days <br />0.00917 hours <br />5.456349e-5 weeks <br />1.25565e-5 months <br /> onsite during off shifts.

Results: Of the areas inspected one item of noncompliance (battery and charger

112 removed from service paragraph 4) was identified.

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8202160607 820127

PDR ADOCK 05000295

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1.

Persons Contacted

  • K.

Graesser, Station Superintendent

  • E.

Fuerst, Assistant Station Superintendent,0perations

  • G.

Plim1, Assistant Station Superintendent, Administrative

and Support Services

R. Budowle, Unit 1 Operating Engineer

J. Gilmore, Unit 2 Operating Engineer

L. Pruett, Assistant Technical Staff Supervisor

P. LeBlond, Assistant Technical Staff Supervisor

  • A. Miosi, Technical Staff Supervisor

B. Schramer, Station Chemist

F. Ost, Health Physics Engineer

C. Silich, Technical Staff Engineer,ISI

  • B.

Harl, Quality Assurance Engineer

T. Lukens, Quality Control Engineer

  • B. Kurth, Master Instrument Mechanic
  • Denotes those present at the exit of January 15, 1982

2.

Summary of Operations

Unit 1 operated at power levels up to 100% throughout the inspection interval.

No reactor trips were experienced.

Unit 2

The following reactor trips occurred during the inspection interval:

Date/ Time

Power Level

Occurrence

December 1, 1981

28%

Unit 2 was tied to the grid at 12:20

3:20 AM

AM December 1, 1981 for the first time

since commencing a refueling outage

September 11, 1981. At 3:20 AM the same

day the unit tripped from 28% power. The

trip resulted from the rupture of the 2D

feedwater regulating valve operating dia-

phragm. This caused a steam flow / feed

flow mismatch coincident with low level

in the Steam Generator. The valve was

repaired, the unit made critical and re-

stored to the grid at 1:25 PM December 1,

1981.

December 6, 1981

90%

The reactor tripped on low low stean gener-

3:55 AM

ator 2C level. The low low level condition

was initiated when a motor control center

that supplies power to the E.H.C. oil pump

tripped.

This caused the turbine governor

valves to drift closed causing a shrink

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condition in the steam generators. The

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redundant E. He C. oil pump

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Date/ Time

Power Level

Occurrence

December 6, 1981

did not auto-start and was started

(con;t)

manually. However, it failed to develop

sufficient E.H.C. oil pressure due to a

problem with the unloader valve setting.

After the trip was received, the 2B auxiliary

feedwater pump failed to start automatically

as designed.

Subsequent maintenance inves-

tigation found nothing that would indicate

the cause of the starting problems and the

pump successfully passed a surveillance test

to prove operability (See paragraph 9 for

details regarding auxiliary feedwater pump

starting problems).

December 11, 1981

90%

The unit returned to power on December 7,

1981. Reactor tripped due to a main genera-

tor trip-turbine trip. The generator tripped

on a ground fault which resulted from a tube

leak in a hydrogen cooler. The tube leak

introduced vs ter into the main generator

which caused a current path to ground to

develop in the T-1 bushing.

After the reactor trip was received, neither

the 2B or 2C motor driven auxiliary feedwater

pumps (AFW) started automatically as designed.

The 2A AFW pump was out of service at the time.

Both 2B and 2C pumps were able to be started

manually from the control room.

Because the failure of AFW pumps to start as

designed following a reactor trip was a re-

petitive occurrence (See Unit 2 reactor trip

of December 6, 1981), the NRC issued a con-

firmatory letterwhich required Unit 2 to re-

main shutdown until a definitive resolution

of the AFW pump starting problems could be

achieved (See paragraph 9 for details of AFW

pump starting problems).

The confirmatory shutdown letterwas lifted by

the NRC on December 21, 1981 after repairs

were made and the unit was on-line at 2:35 AM

on December 22, 1981.

December 22, 1981

50%

Reactor trip from low low Steam Generator C

2:35 AM

level. The low low level condition was caused

by a blown diaphragm in the 2C feedwater regu-

lating valve.

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Date/ Time

Power Level

Occurrence

After the trip was received, the AFW pumps

s tarted as designed af ter repairs were made

a s a result of the reactor trip on Decem-

bar 11, 1981.

Upon resetting safeguards following recovery

from the reactor trip, the 2B reactor trip

breaker opened for unknown reasons and would

not close immediately. The breaker was removed

and inspected but nothing was found and a

surveillance test to prove operability was

successfully passed.

The unit was returned to power at 6:25 PM on

December 22, 1981.

December 22, 1981

50%

Reactor trip from opening of train B reactor

8:33 PM

trip breaker at power. The opening of the

trip breaker was related to the reactor trip

of December 22, 1981 (See paragraph 10 for

details of reactor trip caused opening of 2B

reactor trip breaker).

The unit was placed back on line at 6:15 AM on

December 23, 1981.

January 4, 1982

22%

On January 1, 1982 a shutdown on Unit'2 was

1:30 AM

commenced to repair condenser tube leaks.

When the unit had been ramped down to zero

percent power as indicated by the EHC system the

generator was still producing 49 MW.

Tha

operators tripped the turbine knowing that a

turbine trip / reactor trip would result. On

January 3, 1982 the unit was taken to hot

standby in anticipation of the completion of

condenser repairs.

January 5, 1982

< 2%

On January 5, 1982 at 1:25 PM the reactor

1:25 PM

tripped from hot standby when instrument

mechanics tripped the P-13 bistable thus

enabling the at power trips. The trip signal

came from the reactor trip / turbine trip logic.

The reactor was made critical again at 4:45 PM

January 5, 1982.

January 6, 1982

< 2%

On January 6, 1982 at 12:39 AM, the reactor

12:39 M4

tripped on low inw level in the D Steam Gen-

erator. The MSIV's were being open in prepara-

tion for placing the unit on line. When the

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Date/ Time

Power Level

Occurrence

D MSIV was opened the downstream drain valve

failed to close automatically. The resultant

steam off dropped the Steam Generator level

below the trip point. The reactor was made

critical again at 4:05 January 6, 1982.

January 6, 1982

  • ( 2%

At 4:53 AM January 6, 1982 the unit tripped on

4:54 AM

steam flow / feed flow mismatch coincident with

low level in the A Steam Generator. The trip

resulted from an excessive rod pull which

caused Steam Generator relief valves to open

at the same time the operator was opening the

MSIV bypass valves. The condition was aggra-

vated by g steam flow set point which was high

by 0.4x10 pph and an initial Steam _enerator

level near the low level point. The reactor

was made critical again at 12:45 PM and tied

to the grid at 10:15 PM on January 6, 1982.

3.

Licensee Action on Previous Inspection Items

(closed) Unresolved Item (50-304/81-16-01) Slow Closure of Containment Isolation

Valves. The licensee submitted an updated LER which attributed the slow valve

closing time to an ASCO solenoid valve in the instrument line which failed to vent.

The failure to vent was attributed to oil in the instrument air lines (See paragraph

11 for details regarding containment isolation valves sticking due to oil in the

instrument air lines).

4.

Removal of Battery and Charger 112 from Service

On December 12, 1981 modification work on Unit i that required isolation of Battery

112 and Charger 112 from D.C. bus 112 was presented to shift management (shift

engineer S.E. and shift control room engineer S.C.R.E.).

Management reviewed

Technical Specification Section 3.15.2.E and 3.15.2.F and determined that the

battery and charger isolation were permitted by the above referenced Technical

Specification as long as the work was completed within twenty-four hours.

They

noted that the isolation should be acceptable since the temporary configuration

would be the same as that presently authorized procedurally to place a battery

on routine equalizing charge, whereby both battery and charger are also divorced

from the D.C. bus.

Management did not realize that such an isolation was in

violation of Technical Specification 3.15.2.H when performed on an operating unit.

As a final check prior to making the battery isolation, the Operating Engineer

(0.E.) was consulted, but he erroneously thought the work was being performed

on Unit 2 which was in hot shutdown, and agreed with the shift management's

conclusion to initiate the isolation. The work was authorized, bus 112 and 212

cross connected, and the 112 battery and charger isolated at about 10:20 AM

December 12, 1981.

The work was completed and the lineup returned to normal

about 6:30 PM December 12, 1981. The Operating Engineer realized the next day

that the work had been done on the operating unit in violation of Technical

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Specification 3.15.2.H and initf'ted a deviation report. The senior resident

inspector was notified about a

AM December 14, 1981 and a telegram sent to

Region III at 11:30 AM Decemb.

14, 1981.

The safety significance of the occurrence was that a_ degree of independence

112 remained energized from a power source that

between units was lost. *

was as reliable as its . zaal source.

Technical Specification Sections 3.15.2.E and 3.15.2.F describe operation with

an. inoperable battery and battery charger respectively. Technical Specification Section 3.15.2.H states:

If more than one of the conditions _specified in

3.15.2.A, 3.15.2.B, 3.15.2.C

3.15.2.D

3.15.2.E, 3.15.2.F and 3.15.2.G occur

concurrently, the reactor of the affected unit shall be brought to the hot

shutdown condition immediately.

Contrary to the above, from 10:20 ..M

to 6:30 PM December 12, 1981 Unit I was

operated with both the 112 battery and 112 battery charger isolated from bus

112 in violation of Technical Specification 3.15.2.H.

This violation was licensee

identified and is considered an item of noncompliance.

The resident inspectors consider the cause of this event to be personnel error

due to difficulties encountered in comprehending Technical Specification 3.25.2

and its eight subsection. The inspectors noted that the written structure-

of the specification is complex and has lead to items of noncompliance in the

past (NRC Inspection Report 295/79-01; 304/79-01 and 295/79-08; 304/79-09).

The licensee was requested to submit ~a revision to Technical Specification 3.15.2 which would clarify its meaning, particularly with respect to Technical Specification 3.15.2.H.

The change should include a provision to allow both

battery and charger to be isolated from a D.C. bus provided that bus was supplied

power from the opposite unit.

This item is open pending completion of corrective action and is designated

295/81-29-01 and 304/81-27-01.

5.

Investigation

The senior resident inspector interviewed licensed personnel regarding Commonwealth

Edison Management Director 1-0-17 as part of a separate NRC investigation.

No items of noncompliance were identified.

6.

Zero Shift of Fischer Porter Transmitters

LER 304/81-26 identifies a repetitive problem involving zero shift on Fischer-

Porter transmitters resulting in nonconservative safety settings. The licensee

has undertaken a program to improve transmitter setpoint stability by replacing

transmitters used in environmentally qualified applications with transmitters

of another manufacturer. The replacement program will be ongoing.

For transmitters that do not require environmental qualification, a setpoint

change study has been prepared with the intent of introducing a conservative

bias into the setpoint to offset any drift. The setpoint change study is under

review.

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No items of noncompliance were identified.

7.

Inadvertant PORV's Opening

The resident inspector was requested by NRC Headquarters to reinspect NUREG 0737 requirement II.K.3.9 regarding the P.I.D. controller for the power operated

relief valves (PORV's). The re-inspection only concerned plants using Foxboro

type controllers for the PORV's.

The inspector determined that Zion Station

does not use Foxboro type equipment in the P.I.D. application.

No items of noncompliance were identified.

8.

Unit 1 Primary to Secondary Leakage

The licensee has continued to monitor the unit primary to secondary leakage.

Previous leak test results are documented in Inspection Reports 50-295/81-09,

-14, -20 and -26.

The lesk test results for this inspection period are as

follows:

Date

Leak Rate in GPD

1B S/G

1 C S/G

December 1, 1981

374

56.1

December 4, 1981

218

10.3

December 11, 1981

300

7.97

December 17, 1981

264

25.5

Decamber 23, 1981

367

37.7

December 30, 1981

375

54.0

January 7, 1982

387

27.5

January 14, 1982

431

12.5

FortheDecember4,1981angsubsequentleakratesthelicenseeusedare-

calculated value of 4.65x10 cc for the volume of water in the steam generator.

Previous leak rates were based on a steam generator volume of 6.13x10

cc.

The calculated leak rates were thus reduced by a factor of 0.74 using the new

value.

The inc reasing activity in the steam generator has increased the activity of the

air ejet*or exhaust. The set point of the air ejector rad monitor has been

raised from 600 cpm to 14,000 cpm.

Several areas'in the turbine building

including the Unit I high pressure turbine enclosure, the Unit 1 steam tunnel,

the area around the Unit 1 air ejectors, the secondary sample room and the

auxiliary boiler room have been roped off due to radioactive contamination.

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On December 3, 1981 the licensee held a meeting to discuss the past history,

current status and anticipated actions reParding the Unit 1 primary to secondary

leakage. The following major conclusions were reached by the licensee:

a.

The probable locations of the leaking tube (s) are row 1 and row 2,

and those adjacent to anti-vibration bars,

b.

An early shutdown for refueling is not feasible due to excess reactivity

remaining in the undischarged assemblies.

c.

The reduction in leak rate achieved by a load reduction would be small.

d.

Industry data for series 51 Westinghouse steam generators would predict-

the leakage to be from several faults rather than one large one.

c.

Unit I will continue to operate until the 500 gal / day Technical Specification

limit is reached or the February 1982 scheduled refueling outage commences.

f.

Leak rate calculations will continue on a weekly basis.

No items of noncompliance were identified.

9.

Auxiliary Feed Pumps Inoperability

In recent months the auxiliary feedwater pumps have been subject to three different

problems which resulted in their failure to respond to automatic initiation

signals.

On September 14, 1981 during a normal cooldown on Unit 2, Steam Generator level

was allowed to fall below the 10% low low level resulting in an auto start signal

to the auxiliary feedpumps. The operators placed the auxiliary feedpump control

switches in the pull-to-lock position as allowed by procedure, to avoid excessive

cooldown. The pumps tripped as required. Subsequently the operators were unable

to restart either motor driven auxiliary feedpump. After racking out the breaker

and then returning it to service, one pump was successfully started. The failure

of the motor driven pumps to start was later found to be caused by a " sneak path"

resulting from an earlier modification to the Westinghouse W-2 control switches.

This occurrence was the subject of a special I.E. Report No. 50-295/81-22, 50-304/81-18

in which one item of noncompliance was issued to the licensee.

On November 26.-1981 the Unit 2 motor driven feedpumps failed to start in response

to operator action while the unit was in hot standby. The operators found that by

throttling shut the discharge valves, the pumps could be started. Once the pumps

were running, the discharge valves could be re-opened to their normal positions

and the pump would continue to operate.

It was later determined that the pumps

were tripping off on low suction pressure. This was the result of an improper

set point modification on the suction pressure instrument. The modification had

been performed on the 2A, 2B and 2C auxiliary feedpump instruments during the

Unit 2 refueling outage of September 11-November 24, 1981. The modification had

also been completed on the 1C auxiliary feedpump instrument April 10, 1981. All

four instrument aet points were returned to their previous setting.

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On December 6, 1981 Unit 2 tripped from power Operation. Auxiliary feedpump_

2B_ failed to start in response to an automatic initiation signal. The pump was

checked out. mechanically and electrically but no cause for the failure to start

was found. An operational test was performed satisfactorily on the pump and

Unit 2 was returned'to operation.

On December 11, 1981 Unit 2 again tripped from power-operation. The 2A auxiliary

feedpump was already out of service and the 2B and 2C auxiliary feedpumps failed

to start. The operator was able to start the 2B pump manually on the first attempt

but the 2C pump required two tries before it started. A Confirmatory letter was

issued by NRC Region III confirming that Unit 2 uould not be restarted until the

cause of the auxiliary feedpumps failure to operate was found and corrected.

Subsequent investigation determined that the pumps were tripping on momentary

low suction pressure which occurred during simultaneous start with each pump-

lined up to a separate discharge header. This split header arrangement is used

whenever the steam driven auxiliary feedpump is out of service. This mode of

operation was instituted in September of 1979 in response to an NRC request

resulting from the accident at Three Mile Island and required that two separate

auxiliary feed flow paths to the steam generators be maintained.

The licensee installed time delays that block the low suction pressure trip for a

short time after the pump starts to allow the momentary low suction pressure to

clear. This modification has been cempleted on Unit 2.

For Unit 1, a standing

order has been issued to alert the operators that the motor driven auxiliary

feedpumps may trip during a simultaneous pump start with the discharge headers

split. The order instructs them to manually restart the pumps if this occurs.

This order will remain in effect until the time delay modification _can be completed

on Unit 1.

The_ difficulty experienced when starting the 2C auxiliary feedwater

pump manually during the event was found to be caused by a problem in the pump

switch. That switch was replaced.

Unit 2 tripped from power December 22 and 23, 1981. On both occasions both motor

driven auxiliary feedpumps started and operated satisfactorily even though the

discharge headers were split. This demonstrated the adequacy of the time delay

modification.

The improper setting of the suction pressure trips and the inoperability of the

pumps in the split header mode are being inspected by the NRC Region III Division

of Engineering and Technical Inspection. A separate report will be issued on

these subjects.

This item is open pending completion of the special NRC inspection and is designated

Open Item 295/81-29-02; 304/81-27-02.

10.

Opening of the 2B Reactor Trip Breaker

Zion Un'2 2 was placed on the line at 6:25 PM on December 22, 1981 following

startup from a reactor trip of December 21, 1981 due to a blown diaphragm in a

feedwater regulating valve. At 8:35 PM on December 22, 1981 Unit 2 tripped from

approximately 40% power.

fhe cause of the trip was the opening of train B

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reactor trip breaker. All safety systems operated as designed and the unit was

placed back on the line at 6:15 AM on December 23, 1981.

The cause of the train B safeguards actuation was a power loss to the undervoltage

coil associated with the Westinghouse DB-50 reactor trip breaker.

After recovery from the trip, the 2B reactor trip breaker would not close upon

resetting safeguards. This was similar to that experienced after recovery from

the reactor trip on December 22, 1981. Upon investigation it was determined that

the two parallel reactor trip relays associated with the 2B steam generator low

low level trip had failed in the safe direction by opening which resulted in

opening train B reactor trip breaker and a subsequent reactor trip.

The relays that failed open are BFD type 22S relays, which are similar to relays

identified in previous NRC Bulletins on BFD relays (type 48S, 84S). The licensee

inspected Unit 1 and found one failed relay. The failed relays in both units

were replaced with spare BFD type 22S relays.

As a long range program to improve BFD relay reliability,.new relays, type NBFD

have been ordered, in addition to improved coils to modify type 22S relays.

No items of noncompliance were identified.

11.

ASCO Solenoid Air Valves Sticking Due to Oil-in the Instrument Air System.

Zion Station has had a history of air operated valves failing to stroke because

the solenoid valve which releases the operating air has stuck. The licensee

has determined that oil in the instrument air system interacts with the Buna N

seals in the solenoid valve at elevated temperature and causes the valve stem

to stick. The source of the oil appears to be the service air system via the

cross connect to instrument air. Cross connection of the two systems is necessary

when less than two instrument' air compressors are operable. The instrument air

system is not sampled for oil on a routine basis.

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The licensee has taken the following actions in response. to the sticking solenoid

problem:

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a.

A third air compressor has been installed in the instrument air system-

in order to increase the instrument air system reliability and reduce

the frequency of cross tie's to the service air system.

b.

A modification has nearly been completed to replace the Buna N seals

in the ASCO solenoids with Viton seals. Approximately 99% of the Unit I

and 95% of the Unit 2 ASCO's have undergone this modification. The modi-

fication has been halted in anticipation of a new modification to replace

the installed ASCO's with a new environmentally qualified model,

c.

Surveillance of containment isolation valve operability has been increased

by instituting Procedure TT-300.

This procedure verifies the operability

of all (53 per unit) ASCO controlled containment isolation valves monthly.

Prior to implementing TT-300 these valves would be tested no more frequently

than quarterly.

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The -licensee has' implemented a program ~ to. improve the L reliability of-

d.

the instrument air compressors. The program-includes application of a

vibration analyser and balancing of the compressors. Detailed records

are not available, but the licensee. believes.the instrument-service air

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cross connect time has been reduced from several days to a few hours per

year.

The effectiveness of the licensee's action is illustrated by the reduction

in reportable containment isolation valve malfunctions:

Year

No. of Occurrences

1977

7

1978

7

1979

2

1980

1

1981

2

In view of the results achieved by the licensee's actions and the redundancy

of the isolation valves, the licensee's response to the sticking ASCO problem

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appears to be adequate.

No items of noncompliance were identified.

12.

NUREG 0737 Items

The following NUREG 0737 Action Items were complated by the licensee for both

Unit i and Unit 2.

Item

Title

II.B.4

Training for Mitigating Core Damage

II.F.1-4

Containment Pressure

II.F.1-5

Containment Water Level

II.F.2.-3B

Reactor Vessel Level

No items of noncompliance were identific3.

13.

Operational Safety Verification

The. inspector observed control room operations, reviewed applicable logs and

conducted discussions with control room operators during the months of

December and January. The inspector verified the operability of selected

emergency systems, reviewed tagout records and verified proper return to service

of affected components. Tours of the auxiliary building and turbine building

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were conducted to observe plant equipment conditions, including potential

fire hazards, fluid leaks, and excessive vibrations and to verify that main-

tenance requests had been initiated for equipment in need of maintenance. The

inspector by observation and direct interview verified that the physical security

plan was being implemented in accordance with the station security plan.

The inspector observed plant housekeeping / cleanliness conditions and verified

implementation of radiation protection controls

During the month of December,

the inspector walked down the accessible portions of the auxiliary systems to

verify operability.

These reviews and observations were conducted to verify that facility operations

were in conformance with the requirenents established under Technical Specifications,

10 CFR, and administrative procedures.

No items of noncompliance were identified.

14.

Monthly Maintenance Observation

Station maintenance activities of safety related systems and components listed

below were observed / reviewed to ascertain that they were conducted in accordance

with approved procedures, regulatory guides and industry codes or standards

and in conformance with Technical Specifications.

The following items were considered during this review: The limiting conditions

for operation were met while components or systems were removed from service;

approvals were obtained prior to initiating the work; activities were accomplished

using approved procedures and were inspected as applicable; functional testing

and/or calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities were accomplished

by qualified personnel; parts and materials used were properly certified;

radiological. controls were implemented; and, fire prevention controls were

implemented.

Work requests were reviewed to determine status of outstanding jobs and to assure

that priority is assigned to safety related equipment maintenance which may affect

system performance.

The following maintenance activities were observed / reviewed:

a.

Modification of auxiliary feedpump suction pressure instruments

b,

Following completion of maintenance on the O diesel generator, the

inspector verified that these systems had been returned to service

properly.

No items of noncompliance were identified.

15.

Monthly Surveillance Observation

The inspector observed Technical Specifications required loop functional

surveillance testing and verified that testing was performed in accordance

with adequate procedures, that test instrurentation was calibrated, that

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limiting conditions for operation were met, that removal and restoration of

the affected components were accomplished, that test results conformed with

Technical Specifications and procedure requirements and were reviewed by

personnel other than the individual directing the test, and that any deficiencies

identified during the testing were properly reviewed and resolved by appropriate

management personnel.

No items of noncompliance were identified.

16.

Licensee Event Reports Followup

Through direct observations, discussions with licensee personnel, and review

of records, the following event reports were reviewed to determine that re-

portability requirements were fulfilled, immediate corrective action was

accomplished, and corrective action to prevent recurrence had been accomplished

in accordance with Technical ( 'cifications:

Unit 1

LER NO.

DESCRIPTION

81-46

Non-representative Sample From Off Gas Monitor

81-47

Failure of ORT-PR-10C

81-48

Failure of IRE-0011 and IRE-0012

81-49

Failure of Power Range Channel N-42

81-50

Battery and Charger 112 Taken Out of Service

Unit 2

LER NO.

DESCRIPTION

81-25

Missed Shiftly Grab Samples

81-26

2A S/G Feedwater Flow Loop High

81-27

Vessel Level Leak in Containment

81-28

Blower Tripped for Rad Monitors

81-29

2C S/G Channel Failed liigh

81-16 Update

Failure of 2A0V-SS9356B to Close

Regarding LER 304/81-25, this will be designated a licensee identified item of

noncompliance in which no citation will be issued.

Regarding LER 304/81-26, the zero shift of Fischer Porter transmitters is

described in paragraph 6 of this report.

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Regarding LER 50-304/81-16 (Failure of 2A0V-SS9356B to close), the subject valve

did not operate because the ASCO solenoid failed to vent the air off the

operator of the A0V. The licensee believes this was due to the ASCO valve

sticking caused by residual oil in the instrument air system interacting with

the Buna N seals. This problem has existed with sol'enoid air valves at least

as far back as 1976 and has been well documented via LER's.

A further discussion

of this problem is contained in paragraph 11.

17. Meetings, Offsite Functions

The inspectors attended the following meetings and offsite functions during

the inspection period:

J. R. Waters

December 10, 1981

Zion Probalistic Risk Seminar NRC Headquarters

Bethesda, Maryland

December 16-18, 1981 Resident Inspector Seminar

NRC Region III

Headquarters

Glen Ellyn, Illinois

J. E. Kohler

November 30-

December 18, 1981 American Nuclear Society

Meeting

San Francisco, California

December 17, 1981

Commonwealth Edison

Corporate Office

Chicago, Illinois

December 18, 1981

Resident Inspector's Seminar

NRC Region III

Headquarters

Glen Ellyn, Illinois

18.

Unresolved Items

Unresolved items are matters about which more information is required in order

to ascertain whether they are acceptable items, items of noncompliance or

deviations. Two unresolved items (paragraphs 4 and 9) were disclosed during

this inspection.

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19.

Exit Interview

The inspector met with licensee representatives (denoted in paragraph 1)

throughout the month and at the conclusion of the inspection on January 15,

1981 and summarized the scope and findings of the inspection activities.

The licensee acknowledged the inspector's comments.

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