ML20040C941

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IE Insp Repts 50-317/81-27 & 50-318/81-25 on 811201-820105. Noncompliance Noted:Failure to Lock Svc Water Valves & Maintain High Concentration Boric Acid Piping Insulation
ML20040C941
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 01/12/1982
From: Architzel R, Mccabe E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20040C934 List:
References
50-317-81-27, 50-318-81-25, IEIC-81-13, NUDOCS 8201290393
Download: ML20040C941 (14)


See also: IR 05000317/1981027

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DCS Nos. 50317 811223

50318 811109

50318 811204

50317 811116

50318 811113

50320 790328

50317 811127

50318 811105

U. S. NUCLEAR REGULATORY COMMISSION

Region I

Report Nos. 50-317/81-27

50-318/81-25

Docket Nos.

50-317

50-318

Licenses

DPR-53

Category

C

DPR-69

Pricrity

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Licensee:

Baltimore Gas and Electric Company

P. O. Box 1475

Baltimore, Maryland 21203

Facility:

Calvert Cliffs Nuclear Power Plant, Units 1 and 2

In!pection at: Lusby, Maryland

Inspection Conducted: December 1,1981 - January 5,1982

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Inspectors:

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  1. I d.

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R. E. Architzel, Senior Resident Reactor

date signed.

Inspector

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iIi3.582.

Approved by:

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E. C. McCabe, Jr. , Chief, Reactor

date signed

Projects Section 2B

Inspection Summary:

December 1,1981 - January 5,1982 (Combined Report 50-317/81-27,

and 50-318/81-25)

Areas Inspected: Routine, onsite regular and backshift inspection by the resident

inspector (68 hours7.87037e-4 days <br />0.0189 hours <br />1.124339e-4 weeks <br />2.5874e-5 months <br />). Areas inspected included the control room and the accessible

portions of the auxiliary, turbine. service, and intake buildings; radiation' pro-

ter. tion;. physical security; fire protection; plant operating records; maintenance;

surveillance; plant operations; radioactive waste releases; open items; IE Circulars;

-TMI Action Plan Items; and reports to the NRC.

Noncompliances: Three: Failure to follow Radiation Control Procedures (detail

failure to lock Service Water Valves (detaii 3.d); and failure to maintain high

concentration boric acid ' piping insulation (detail 3.f).

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DETAILS

1.

Persons Contacted

The following technical and supervisory level personnel were contacted:

G. E. Brobst, General Supervisor, Chemistry

J. T. Carroll, General Supervisor, Operations

J. A. Crunkleton, Supervisor, Electrical Maintenance

C. L. Dunkerly, Shift Supervisor

W. S. Gibson, General Supervisor, Electrical & Controls

J. E. Gilbert, Shift Supervisor

J. R. Hill, Shift Supervisor

S. E. Jones, Supervisor, Training

J. F. Lohr,. Shift Supervisor

E. T. Reimer, Plant Health Physicist

J. E. Rivera, Shift Supervisor

P. G. Rizzo, Engineering Analyst

L. B. Eussell, Plant Superintendent

R. P. Sheranko, General Foreman, Production Maintenance

J. Shire, Instructor, Training

J. Sites, Supervisor, Instrument Maintenance Unit 1

R. L. Wenderlich, Engineer, Operations

D. Zyriek, Shift Supervisor

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2.

Licensee Action on Previous Inspection Findings

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(Closed) Unresolved Item (318/81-11-02), Diesel Generator Surveillance Test

Procedure. Surveillance Test Procedure STP 0-8-0 was revised (Rev.11) on

December 30, 1981 to reflect performance with the Diesel starting timer.

(Closed) Noncompliance (317/81-12-01; 318/81-12-01), Failure to Calibrate Gauges.

The inspector reviewed the following preventive maintenance procedures which the

licensee has developed to ensure calibration of gauges used in pump Inservice

Inspection testing for Units 1 and 2.

1+2-ll-I-Q-14, Rev. 0, Service Water Pumps Suction and Discharge

Pressure Gauges

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1+2-12-I-Q-6, Rev. O, Salt Water Pumps Discharge Pressure Gauges

1+2-15-I-Q-15, Rev.1, Component Cooling Pumps Suction and Discharge

Pressure Gauges

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1+2-36-I-Q-8, Rev. O, Auxiliary Feed Pumps Suction and Discharge

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Pressure' Gauges

1+2-40-I-Q-15, Rev. O, Boric Acid Pumps Suction and Discharge

Pressure Gauges

1+2-52-I-Q-51, Rev. O, LPSI and HPSI Pumps Suction Pressure Gauges

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1+2-61-I-Q-8, Rev. O, Containment Spray Pumps Suction Pressure Gauges.

(0 pen) Noncompliance (317/79-23-02), Failure to Correct a Grounded Condition

in the 21 DC Battery Bus. The licensee responded to this item in a letter

dated May 3, 1980. Requirements were added to the Control Room Operator's

logs to check for grounds once per shift, require the writing of MR's for any

ground less than 50 K ohms,and close coordination between the Shift Supervisor

and Electrical Foreman regarding which DC loads could be deenergized. The

letter stated that further plans included using the reserve battery as a

parallel power supply while attempting to identify grounds. During review

of logs and observations in the Control Room and Cable Spreading Rooms, the

inspector has noted implementation of the stated actions.

Use of the reserve

battery has been approved by the NRC (Amendments 58 and 40 dated November 2,

1981) during normal operations. The licensee questioned the inspector about

use of the reserve battery during corrective maintenance while locating

grounds.

(The reserve battery's charger is not class 1E, and the licensee

is required to use the regular IE chargers when the reserve battery is being

used as a replacement on a battery bus.) The inspector discussed the

corrective maintenance procedure with the Operating Reactors Project Manager

The proposed procedure was for corrective maintenance and involved powering

distribution panels (versus buses) with the reserve battery. Such a line

up would allow use of the installed charger's gmund detector and reduce,

by a factor of six, the individual circuits which must be deenergbed to

locate a ground. The inspector noted that the proposed proccdure did not

contain a specific precaution to limit the amount of time the reserve

battery is used to power a distribution panel. The licensee stated that

such a precaution would be added to the proposed procedure and that the

intent was to limit the time to that necessary to locate which panel had

a ground.

The inspector concluded that the proposed procedure was a

significant improvement in the licensee's ground troubleshooting methods

and did not violate Technical Specifications. Concerns about cab!c

attachments to the panels, transient currents during the paralleling, and

a complete set of precautions should be resolved prior to implementation.

This item will remain open pending inspector review of the approved

Battery Ground Isolation procedure.

(Previously Closed) Noncompliance and Unresolved Items (317/79-24-01 through-

04), Unmonitored Discharge of Caustic to Chesapeake Bay.

The licensee has

reorganized several water treatraent functions which were oerformed by the

Operations organization and transferred them to a new Chemistry (Water

Treatment) group.

During the current inspection, the licensee questioned

the inspector concerning the reed to continue performing certain commit-

ments which had been made to the NRC in light of the reorganization. The

referenced commitments were made at a Management Meeting to prevent

recurrence of a long history of unmonitored releases of caustic and acid.

The licensee had researched past commitments in Licensee Event Reports and

discussed provisions of a draft procedure with the inspector. All previous

commitments had not been thoroughly compared to the proposed shift in

controls by the licensee. For example, current procedures require hourly

logging of tank levels by the Control Room Operator (received from an out-

side operator), approval of the Senior Control Room Operator prior to a

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release, and review of valving checklists by the Senior Control Room Operator.

In addition, specific training for Operations personnel had been conducted

an/ orocedure audits performed by the Quality Assurance organization. The

invector concluded that the proposed revisions to commitments were significant

and did have some advantages (for example, the limited job scope of the Water

Treatment personnel would result in increased familiarity with the operation

of the Waste Neutralizing System), however, the overall impact was a reduction

in the administrative controls. The licensee was informed that any changes

in operation of the Waste Neutralizing from previous commitments should be

addressed in formal ccerespondence with the NRC.

3.

Review cf Plant Operations

a.

Daily Inspection

The inspector toured tha facility to verify proper manning and access

control, and observed adherence to approved procedures and LCOs.

Instrumentation and recorder traces were observed. Status of contrc'.

room annunciators were reviewed. Nuclear instrument panels and other

reactor protective systems were examined. Control rod insertion limits

were verified.

Containment temperature and pressure indications were

checked against Technical Specifications. Stack monitor recorder

traces were reviewed for indications of releases.

Panel indications

for onsite/offsite emergency power sources were examined for automatic

operability.

Control room, shift supervisor, and tagout log books,

and operating orders were reviewed for operating trends and activities.

During egress from the protected area, the inspector verified operability

of radiological monitoring equipmene and that radioactivity monitoring

was done before release of equipment and materials to unrestricted use.

These checks were performed on the following dates:

12/2, 12/7, 12/8,

12/11,12/14,12/15,12/21,12/22,12/23,12/29,12/30,12/31,and

1/04/82.

No unacceptable conditions were identified.

b.

Weekly System Alignment InspectJon

Operating confinnation was made of selected piping system trains.

Accessible valve positions in the flow path were verified correct.

Proper power supply and breaker alignment was veria ied. Visual

inspections of major components were cerformed. Operability of

instruments essential to system performance was verified. The fol-

lowing systens were checked:

-- Unit 2 CVCS ;ystem - Boric Acid Flow Paths in BAST Room, checked

on 12/11/81.

-- Unit 1 and Unit 2 Service Water System Line Up in Auxiliary Building,

5' elevation (service to Diesel Generators and to Containment

Coolers) on 12/21/81.

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Unit 2 CVCS System - Charging Line Up in Charging Pump Room

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checked cn 12/30/81.

Findings are addressed in paragraphs e and f below.

c.

Biweekly Inspection

Verification of the following tagouts indicated the action was properly

conducted.

No.12673, Unit 2 Boric Acid Basket Strainer, verified 12/11/81.

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No. 94685, Unit 1, Removal of No. 11 Beric Acid Pump, verified 12/21/81.

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Boric acid tank samples were compared to the Technical Specifications. Tank

levels were also confimed.

d.

Other Checks

During plant tours, the inspector observed shift turnovers, security

practices at vital area barriers, completion and use of radiation

work permits, protective clothing and respirators. The use and operational

status of personnel monitoring practices, and area radiation and air

monitors were reviewed.

Equipment tagouts were sampled for conformance

with TS LCOs.

Plant housekeeping and cicanliness was evaluated. Other TS

LCOs, including RCS Chemistry and Activity, Secondary Chemistry and Activity,

watertight doors, and remote instrumentation were checked.

A large amount of Boric Acid residue was observed in the Ur.it 2 BAST Room

and underneath the mixing tee in the 5 foot Auxiliary Building hallway,

apparently from valve packing leaks. The licensee acknowledged the

inspectors comments. This area is unresolved and will be reexamined to

ensure action has been taken by the licensee to improve the housekeeping

and minimize leakage (318/81-25-01).

e.

On December 21, 1981, during the check of the Service Water (SRW) Sistem

line up to the Diesel Generators (E' elevation, Auxiliary Building) the

following valves were observed to be in the correct position but not locked:

2SRW 174, Diesels to 21 SRW Subsystem Discharge Header Stop (Locked Open).

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2SRW 171,21 Diesel Generator Discharge to 22 SRW (Locked Open).

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2SRW 169,22 SRW Subsystem Supply to 21 EDG (Locked Open).

The General Supervisor - Operations was informed of the unlocked valves and

issued instructions to have the valves locked the same day. Failure to lock

valves as required violates the OI 15, Rey, 11, dated December 16,1980

requirement that those valves be locked and the TS 6.8.1 requirement for ad-

herence to the Service Water System procedures recommended in Appendix A, R_egu-

latory Guide 1.33(318/81-25-02).

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-f.

During the inspection of the CVCS Systems on December 11 and 30,1981,

the inspector noted the following deficiencies (all piping sections

are high concentration Boric Acid).

There was no insulation on the suction elbow in the supply to

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21 Boric Acid Pump.

There was no insulation on the suction line from 21 Boric Acid

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Tank.-

A section about 12 inches long in the 22 Boric Acid Pump minimum

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flow line was not insulated.

-- One of the (two) heat trace circuits in the discharge of 22 Boric

Acid Pump appeared broken and there was no insulation.

-- Additional sections of high concentration piping were covered with

a black paste.

An approximately 10 foot length of Gravity Feed Piping to the Unit 2

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CHV Pumps was not insulated.

The insulation cover was not closed on 12 Boric Acid Pump and there

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was no insulation covering the box.

The inspector reviewed the licensee's Safety Related Q list in this area

and noted that both the heat trace circuit and piping in question were

safety related. The inspector also reviewed the FSAR,which states that

high concentration boric acid lines are heat traced and insulated, and

P&ID 6750-E-39-36-5, Unit 2 Boric Acid System, Electric Heat Tracing

Revision 3.

This P&ID requires the system to be covered with 1.5

inches of calcium silicate insulation.

In addition, the black paste is

a heat distribution compound which is required to be covered with

insulation. The inspector stated that failure to properly maintain the

insulation of the Boric Acid System was an item of noncompliance

(317/81-27-01; 318/El-25 ^3),

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4.

Review of Events Requiring One Hour Notification to the NRC

The circumstances surrounding the following events requiring prompt NRC (one

hour) notification via the dedicated telephone (ENS-line) were reviewed.

Acout 1:20 p.m. on December 23, 1981, an inadvertant actuation of the

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Unit 1 Recirculation Actunhn System (RAS) occurred. Although

surveillance testing w s in progress to test individual channels no

cause was found for the actuation. The RAS opens the Containment Sump

Valves and trips the LPSi Pumps if running. No other equipment was

affected. The inspector discussed the everit with I&C technicians and

the Control Room Operator on shift. The: UMt 1 Alarm Typewriter was

also reviewed. This device only printed verification of the actuation

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at 1321 hours0.0153 days <br />0.367 hours <br />0.00218 weeks <br />5.026405e-4 months <br /> for both RAS A and RAS B.

The technicians stated that

the surveillance test procedure had been followed and could give no

reason for the actuation.

(The RAS actuates on a low level in the

Refueling Water Storage Tank, with a 2 out of 4 level switch logic.

The STP requires testing of one switch at a time with a reset of alarms

prior to preceding.) The Control Room Operator stated that when the

actuation occurred (RAS A and B alarms) three alarms for the actuation

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cabinets ZF, ZD AND ZE were present. The RAS was immediately reset in

the Cable Spreading Room by the I&C technicians. Troubleshooting later

that day and the next (portions observed by the inspector) did not

iaentify any problems with the ESFAS system sad the problem did not

recur. The inspector concluded that either the problem was spurious

or the test conditions were otherwise not being duplicated.

5.

Plant Maintenance

The inspector observed and reviewed maintenance and problem investigation

activities to verify compliance with regulations, administrative and

maintenance procedures, and codes and standards.

Proper QA/QC involvement,

safety tags use, equipment alignment, jumpers use, personnel qualifications,

radiological controls for worker protection, fire protection, retest

requirements, and reportability per Technical Specifications. The following

activities were included.

I-81-130, Unit 1, ESFAS RAS Channel ZF, ZD, or ZE Hanging, observed 12/24/81.

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PMS-2-36-M-M-1, Change Oil in Turbine Bearings, take samples, 21 AFP,

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observed on 12/31/81.

The inspector observed portions of the testing to determine the cause of the

RAS actuation. This included activities in the Control Room, Cable Spreading

Room and Unit 1 Refueling Water Tank Room. About 9:00 a.m., the inspector went

to sign in on a Radiation Work Permit for access to the Unit 1 RWT Room.

While discussing entry requirements with Control Point pernonnel, the inspector

stated that an RM-14 (survey instrument) would not be neccssary as he would

use the one issued to the technician working in the room.

The Radiation

Control personnel were not aware of any work in the RWT Rooms nor that any

technician had checked out a survey instrument. The inspector told the licensee

he was sure a technician had entered the room because he had observed portions

of the testing in the Cable Spreading Room which required actions in the RWT

Room. A Radiation Control technician accompanied the inspector to the RWT Room

with an instrument. The I&C technician had been contacted by his supdrvisor and

had left the room without surveying. He was located and frisked by the

Radiation Control technician and found not to be contaminated. The inspector

noted that the technician had not signed in on any Radiation Work Permit, had

not checked in with the Radiation Control Point, and had not obtained a survey

instrument for access to this controlled area. This violates the TS 6.8.1 imposed

CCI400B~requirementsforreadingandinitiallingRWP's'(tocertifyunderstanding)

and for self-monitoring upon exiting a radiation controlled area (317/81-27-02).

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6.

Surveillance Testing

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The inspector observed parts of tests to verify: Performance in acccrdance

with approved procedures; LC0's were satisfied; test results (if completed)

were satisfactory; removal and restoration of equipment were properly

accomplished;:and that deficiencies were properly reviewed and resolved.

The following tests were reviewed:

-- STP-0-8-0,11 Diesel Generator Weekly Test, observed 12/22/81.

-- STP-M-220-1, ESFAS Functional Test, observed on 12/23/81. (Note.1)

During-the observation of this test, the inspector noted that the procedure

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still called for the use of a stopwatch to verify start times. As noted

during Inspection Report 318/81-11, the licensee actually uses a test device

for timing the diesels such that a stopwatch is not necessary. The inspector

expressed concern that this procedural deficiency had existed so long after

being highlighted by the NRC (May, 1981). The licensee stated that the change

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had apparently been overlooked and issued a change to STP-0-8-0-on December 30,

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1981 to correct the. procedure.

7.

Radioactive Waste Releases

Records and sample results of the following liquid and/or gaseous radioactive

waste releases were reviewed to verify conformance with regulatory requirements

prior to release.

R-099-81, 11 RCWMT released 12/12/81, est. curies 0.148 (excluding Tritium

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and Noble Gasses).

R-100-81, 12 RCWMT released 12/20/81, est. curies 1.44 E-2 (excluding

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Tritium and Noble Gasses).

G-066-81,11 WGDT,1solated 11/28, released 12/15/81. Release Rate

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GpI 3.18 E+2 m3/sec.; GpII 1.23 E+2 m3 sec.

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G-067-81, Vent Unit 1 Containment via ECCS Pymp Room on 12/17/81.

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Release Rate GpI 6.7 E+4 m3/sec.; GpII 0.6 m3/sec.

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No items of noncompliance were identified.

Note 1 - As discussed in paragraph 4 an inadvertant actuation of the RAS occurred

' during this surveillance. The licensee was unsuccessful at finding the cause and

has left the thintenance Action (I-81-130) open pending the next retest.

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8.

Observation of Physical Security

The inspector. checked, during regular and off-shift hours, on whether selected

aspects of security met regulatory requirements, physical security plans, and '

approved procedures.

a.

Security Staffing

Observations and personnel interviews indicated that a full time

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member of the security organization with authority to direct physical

security actions was present, as required.

Manning of all three shifts on various days was abserved to be as

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required.

b.

Physical Barriers

Selected barriers in the protected area (PA) and the vital areas (VA) were

observed. Random monitoring of isolation zones was performed. Observations

of truck and car searches were made.

c.

Access Control

Observations of the following were made:

Identification, authorization, and badging.

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Access control searches.

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Escorting.

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Communications.

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C0mpensatory measures when required.

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No unacceptable conditions were identified.

9.

Review of Licensee Event Reports (LERs)

LERs submitted to NRC:RI were reviewed to verify that the details were clearly

reported, including accuracy of the description of cause and adequacy of

corrective action. The inspector determined whether further information was

required from the licensee, whether generic implicstions were indicated, and

whether the event warranted onsite followup. The following LERs were reviewed.

LER t.o.

Date of Event

Date of Report

Subject

Unit 1

81-80/3L

11/16/81

12/16/81

CRACKED WELD ON 12 SPENT FUEL

COOLING PUMP DISCHARGE VENT LINE.

81-83/3L

11/27/81

12/24/81

HYDROGEN ANALYZER INOPERABLE.-

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LER No.

Date of Event

Date of Report

Subject

Unit 2

81-51/3L

11/09/81

12/09/81

22-A RCP MIDDLF SEAL PRESSURE

TRANSMITTER SENSING LINE LEAKED.

81-52/3L

11/13/81

12/11/81

REACTOR PROTECTIVE SYSTEM

CHANNEL B TRIP UNITS FOR HIGH

POWER, THERMAL MARGIN / LOWS

PRESSURE & AXIAL SHAPE INDEX

BYPASSED FOR MAINTENANCE.

81-53/3L

11/05/81

12/04/81

CLOSURE OF SALTWATER OUTLET

ARTICULATED VALVE CAUSED HIGH

DISCHARGE PRESSURE ON 22 SW PUMP.

81-55/3L

12/04/81

12/31/81

22 CHARGING PUMP OUT OF SERVICE.

No unacceptable conditions were identified.

10.

IE Circular Review

The following IE Circulars were reviewed on site to determine that the circular

was received by licensee management, that a review for applicability was

perfonned, and that further action taken or planned was appropriate.

-- Circular 81-13, Torque Switch Electrical Bypass Circuit for Safeguard Service

Valve Motors. This circular addressed a coninon wiring error discovered

in the motor control circuitry for Limitorque Motor Operated Valves at two

operating Boiling Water Reactors. The error involved failure to install a

bypass circuit to override the valve open or valve close torque switch under

emergency conditions to eliminate the chance of the valve stalling before

it had completed its travel. The licensee reviewed the circular and

determined that their design did not incorporate bypass circuits as described.

The licensee uses Limitorque Valves, however, by design, the bypass func' ion

is only activated during the initini travel of the valve (in either the

close or open direction). The purrow of this bypass is to allow the motor

to apply sufficient torque to brea!. the valve off its seat.

During the

rest of the valve travel the torque switches are in the circuit and will

stop the motor if actuated. Once actuated a torque switch can only be

reset at the motor operator after removing its cover. The licensee stated

that installation of the bypass switches had been verified during scheme

checks in t.1e start-up program. The licensee also noted that their design

will allow closing of a valve with an open torque switch by manually holding

the motor starter closed without resetting the torque switch.

In addition,

all starters are located outside containment and would, therefore, be

accessible.

The inspector reviewed selected schematics for the licensee's motor operated

valves, several Limitorque Motor Operator Technical Manuals, Regulatory

Guide 1.106. Thermal Overload Protection for Electric Motors on Motor

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Operated Valves, and discussed various aspects of this circular with

the licensee. The inspector concluded that the licensee's design did

not incorporate bypass circuits as described in Circular 81-13. Such

circuits are apparently installed in conformance with Regulatory Guide 1.106 for newer plants.

(This Regulatory Guide addresses bypassing of

Thermal Overloads during emergency conditions, or as an alternative

conservatively setting (in favor of the safety function) overloads and

periodic testing of the settings.) The inspector discussed the pro-

visions of the Regulatory Guide with the licensee and recommended that

they evaluate the present design in light of the NRC guidance in this

area.

11.

Licensee Action on NUREG 0660, NRC Act, ion Plan Developed as a Result of the

TMI-2 Accident

The NRC's Office of Inspection and Enforcement has inspection responsibility

for selected action plan items. These items have been broken down into

nunbered descriptions (enclosure 1 to NUREG 0737, Clarification of TMI

Action Plan Items). Licensee letters containing comitments to the NRC

were used as the basis for acceptability, along with NRC clarification

letters and inspector judgment. The following items were reviewed.

II.B.4 - Training for Mitigating Core Damage. The inspector attended

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two days of requalification training lectures. The area covered was the

mitigation of core damage. The course outline included Incore Instru-

mentation, Excore Instrumentation, instrument failure modes, chemistry,

and radiation monitoring, including sources of radioactivity. The

inspector did not complete review of this item (lesson plans and

attendees) during the current inspection. These aspects will be

reviewed by the NRC during a future inspection prior to closing out

TAP Item II.B.4

II.E.4.2(5) - Containment Pressure Setpoint. As previously noted in

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Combined Inspection Report 317/81-18; 318/81-17, this item had been

scheduled for completion by July 1,1981 but had not been implemented

pending NRC review of the proposed setpoint change. The NRC approved

the licensee's proposed action (lowering the setpoint to 2.8 psig) in

a letter dated October 20,1981. Because a reduction in setpoint was

approved, Technical Specification changes were requested to be submitted.

The letter alsa included a Safety Evaluation Report and a Technical

Evaluation by EG&G Energy Measurements Group. The Technical Evaluation

stated that the staff had (generically) accepted a total loop error of

3.0 psi for isolation setpoint margin over the nonnal containment pressure.

The licensee reviewed this letter and noted that the existing setpoints

were within the staff guidance.

In a letter dated December 7,1981,

they noted that the existing pressure setpoint (less than 4.0 psig) was

conservative with respect to the Technical Evaluation, thus retracting

the commitment to lower the Containment Isolation setpoint. The inspector

expressed concern that the licensee had used the NRC's approval of the

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proposed change as a basis for not making the change. The inspector

questioned the licensee's technical basis for not lowering the

isolation setpoint to 2.8 psig. The licensee stated that the loop

error was 1.0 psi, and the inspector noted that the instruments

measure gauge pressure of the Containnient with respect to the

Auxiliary Building such that atmospheric changes are sensed by

the instruments. The licensee stated that reduction of the Contain-

ment Pressure setpoints would result in Reactor Protective System

Containment High Pressure pre-trip alarms being sensed under normal

conditions.

The inspector noted that II.E.4.2.(5) only addressed

lowering the Containment Isolation setpoints, consequently only the

Containment Isolation and Safety Injection Actuation System setpoints

needed to be changed. The licensee stated that the technical basis

for not reducing the setpoint to 2.8 psig as originally committed

would be reviewed.

The inspector also noted, in discussions with the

Operating Reactors Project Manager, that the licensee's revised

response was undergoing further NRC review for acceptability.

Item

II.E.4.2(5) will remain open pending completion of these reviews and

any indicated licensee action.

12. Meeting with Calvert County Commissioners

The Resident Inspector accompanied Region I Administrator Ronald Haynes for

a meeting on December 8,1981 with Calvert County Comissioners and Public

Safety Officials.

The purpose of the meeting was to introduce Mr. Haynes to the Commissioners

and explain the NRC's roles and responsibilities as a regulatory agency as

they relate to Calvert County. A tour of the County's Emergency Operations

Center (located in the basement of the Court House) was also conducted.

13. Review of Periodic and Special Reports

,

Upon receipt, periodic and special reports submitted pursuant to Technical Specification 6.9.1 and 6.9.2 were reviewed. That review included the

following:

Inclusion of information required by the NRC; test results and/

cr supporting information consistency with design predictions and performance

specifications; planned corrective action adequacy for resolution of problems;

determination whether any information should be classified as an abnomal

occurrence; aad validity of reported information. The following periodic

report was reviewed:

November,1981 Operations Status Reports for Calvert Cliffs No.1 Unit

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and Calvert Cliffs No. 2 Unit, dated December 14, 1981.

14.

Unresolved Items

Unresolved items are matters about which more information is required to

detemine whether they are accep+.able. An unresolved item is discussed

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in paragraph 3.d of this report.

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15. ' Exit Interview

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' Meetings were-held with senior facility management periodically during the

course of this inspection to discuss the inspection scope and findings.

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summary of findings was also provided to the licensee at the conclusion of

. he report period.

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