ML20034F047

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Insp Rept 50-416/92-28 on 921220-930116.Violation Noted. Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Licensee self- Assessment Capability & Reportable Occurrences
ML20034F047
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 02/04/1993
From: Bernhard R, Cantrell F, Hughey C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20034F028 List:
References
50-416-92-28, NUDOCS 9303020224
Download: ML20034F047 (8)


See also: IR 05000416/1992028

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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rapart No.:

50-416/92-28

Licensee:

Entergy Operations, Inc.

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Jackson, MS 39205

Docket No.:

50-416

License No.: NPF-29

Facility Name:

Grand Gulf Nuclear Station

Inspection Conducted: December 20 1992 through January'16, 1993

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Inspectors:

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R. W.'Bernhard, SenioF Rjsider}t' Inspector

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C. A~.~H ghey, Resident"I(spector

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Reactor Projects Section IB

Division of Reactor Projects

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SUMMARY

Scope:

The resident inspectors conducted a routine inspection in the following areas:

operational- safety verification; maintenance observation; surveillance

observation; licensee self-assessment capability; and reportable occurrences.

The inspectors conducted backshift inspections on December 28, 1992, and

January 3 and 11, 1993.

Results:

A violation was identified for inadequate. control-room manning when an SR0

left the control room for a short period on January 11, 1993 (Paragraph 3a).

An additional violation was identified for failure to. complete a procedure

during a steam jet air removal rotation, which 'resulted in an unposted very

high radiation area (Paragraph 3b).

Inspections in the areas of maintenance

and surveillance activities did not identify any weaknesses.

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9303020224 930204

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

W. Cottle, Vice President, Nuclear Operations

  • L. Daughtery,. Superintendent, Plant Licensing

M. Dietrich, Manager, Training

  • J. Dimmette, Manager, Performance and System Engineering
  • C. Dugger, Manager, Plant Operations

C. Ellsaesser, Assistant 0perations Manager

  • C. Hayes, Director, Quality Assurance
  • C. Hicks, Operations Superintendent
  • C. Hutchinson, General Manager, Plant Operations
  • M. Krupa, System Engineering Superintendent

F. Mangan, Director, Plant Projects and Support

M. Meisner, Director, Nuclear Safety and Regulatory Aff airs

D. Pace, Director, liuclear Plant Engineering

  • J. Roberts, Manager, . Plant Maintenance
  • R. Ruffin, Plant Licensing Specialist
  • W. Shelly, Technical Coordinator, Training

Other licensee employees contacted included superintendents,

supervisors, technicians, operators, security force members, and

administrative personnel.

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  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

The plant operated in Mode 1, power operations, during the entire

reporting period. At the end of the reporting period, the unit had been

on-line for 163 consecutive days.

During the week of January 11, 1993, Region II, Division of Radiation

,

Safety and Safeguards, Safeguards Section personnel conducted a review

of Grand Gulf's security and safeguards program. The results of

inspection are contained in NRC Inspection Report No. 50-416/93-01.

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3.

Operational Safety (71707 and 93702)

Daily discussions were held with plant management and various members of

the plant operating staff. -The. inspectors made frequent. visits to the

control room to review the. status of equipment, alarms, effective LCOs,

temporary alterations, instrument readings, and staffing. Discussions

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were held as appropriate to understand the significance of conditions

observed. . Plant tours were routinely conducted and included ' portions. of.

the control building, turbine building, auxiliary building, radwaste.

building and outside areas.

These observations included safety related

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tagout verifications, shift turnovers, sampling programs, housekeeping

and general plant conditions. Additionally, the inspectors observed the

status of fire protection equipment, the control of activities in

prograss, the problem identification systems, and the readiness of the

onsite emergency response facilities.

No deficiencies were identified.

The inspectors reviewed the activities associated with the below listed

events:

a.

The inspectors reviewed the activities associated with an incident

in which the control room was not manned by an SRO. The incident

occurred after midnight on January 11, 1993.

Based on a review of operator and security guard written and oral

statements, interviews with involved personnel and their

supervisors, and security card access history printouts, the

inspectors determined the following represents the most likely

sequence of events:

On January 11, 1993, immediately prior to 0040 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />, the control-

room was manned with three SR0s (a shift superintendent, a shift

supervisor and a plant supervisor) and three R0s. At 0040 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />,

the shift superintendent turned over command function to the shift

supervisor and exited the control room' and the control building to

take a break. At 0043 hours4.976852e-4 days <br />0.0119 hours <br />7.109788e-5 weeks <br />1.63615e-5 months <br />, the shift supervisor turned over

command function to the plant supervisor and joined the shift

superintendent outside the control building.

Based on interviews, the remaining SRO.and the three R0s heard a

very loud disturbance outside the east door (0C503) of the control

room at approximately 0050 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />. The disturbance was interpreted

to be the sounds of a female under extreme duress.. The SRO and

two of the three R0s responded by proceeding to and opening door

0C503. This door is functional but is very rarely used and exits -

into the_RCA of the plant. The operators called from the doorway.

up a stairwell to the source ofl the disturbance and received no

response. The plant supervisor stated that at this time he was

still concerned that a woman was being beaten and exited through

the control room door to be in a better position to look up the

stairs. The plant supervisor also stated that he was the only

person present with the proper dosimetry to enter the RCA.

He

then gained the attention of two security guards positioned.in the

stairwell. They told him that everything was fine and that they

had trouble with a door (OC619) while performing a routine weekly

security door surveillance. The plant supervisor stated that he

then realized that the R0s had closed door 0C503. At that time he

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proceeded through the turbine building and through the routine

exit point of the RCA instead of reentering the control room.

through door 0C503.

(Reentry of the control room from the RCA

would have also been a violation of plant procedures.) He entered

the control building elevator to return to the control room. The

elevator stopped at the ground elevation, and the shift

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superintendent and the shift supervisor, who were returning from

their break, entered the elevator. All returned to the control

room.

Security Card access histories indicated that all three SR0s

reentered the control room at 0055 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />.

The control room was

not manned by an SR0 for approximately five minutes. During this

period the plant was in Mode 1, at 100% power, with no significant

activities occurring in the plant.

Written and oral statements by the two security guards involved

indicated that while performing a weekly security door check on

OC619, the female officer was trapped inside the room and could-

not exit because of mechanical problems with the door. This door.

allows entry to the control room envelope in the ceiling spaces

above the control. room and contains a small concrete landing and

some electrical cable trays.- The false ceiling of the control

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room can be seen from this landing. There is no lighting in'this

room.

In order to gain the attention of her co-worker on the

other side of the very heavy door, the officer called very loudly,

banged on the door palm switch and manipulated the door handle.

These noises and the noises from the officer's radio, were

transmitted through the false ceiling and were interpreted by the

control room operators as a female in distress. After several

minutes, her co-worker opened the door from the outside and freed

her. This corresponds to the time when the plant supervisor ~

gained their attention by calling up the stairs after'he had

exited the control room.

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10 CFR Part 50.54(m)(2)(iii), requires, in part, that when a

nuclear power unit is in an operational mode other than cold

shutdown or' refueling, as defined by the unit's technical

specifications, each licensee'shall have a person holding a Senior

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Operator License for the nuclear power unit-in the control room at

all times.

In addition, Technical Specification 6.2.2.b requires,

in part, that while the reactor is in operational condition 1, 2

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or 3, at least one licensed shall be in the control room.

This matter was identified as violation 50-416/92-28-01, Failure

to properly man the control room with an SRO.

b.

The inspectors revs?wed an event that could have resulted in

inadvertent exposur to plant personnel. Health Physics, while

conducting surveys of the_'A' SJAE room on December 27, 1992,~

discovered higher than normally expected radiation levels. The

room was posted as a Radiation Area following surveys taken after

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a SJAE swap over on December 22, 1992, but remained under the

control of a locked door as if it were still a-Very-High _ Radiation

Area.

Radiation levels surveyed on December 27, 1992, would have

required a Very High Radiation Level posting.

Records _ indicated

that no one entered the' room between the two surveys.

Investigation into the cause of the higher than normal _ radiation

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readings showed a valve not properly positioned.

Valve N64 F201A

had not been repositioned as required by step 5.1.2.11 in

procedure S0104-1-01-N62-1, Condenser Air Removal, Revision 37,

dated February 24, 1992. Upon discovery, operations reestablished ~

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the air purge on the ' A' SJAE, allowed the room radiation levels

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to return to normal, and closed the valve. This failure to

perform a procedure step was identified as violation 50-416/92-28-

02.

Operation's failure to perform this step could have resulted

in unnecessary exposure to an individual entering the area posted

at lower radiation level than actually existed.

c.

On January 14, 1993, the inspectors directly observed control room

activities during a power reduction from 100% to 60%.

Power was-

reduced to facilitate the repair of some steam leaks associated

with the main turbine moisture separator / reheaters. The inspector

verified that the applicable steps of Integrated Operating

Instruction (101) 03-1-01-2, Power Operations, Revision 33, were

followed during the downpower.

Effective command and control

along with good communications and annunciator response was

observed during this plant manipulation.

d.

On January 3,1993, the inspectors observed control room and plant

activities associated with adjustment of the Plant Service Water

system flows and pressures.

Prior to performance of system

adjustments, briefings were given to the plant operators to insure

personnel understood the possible effects of the adjustments.

Good command and control was exercised by the operations staff.

The inspectors identified' procedural weaknesses, which have been

corrected.

4.

Maintenance Observation (62703)

During the report period, the inspectors observed portions of the

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maintenance activity listed below.

The observations included a review

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of the MWO and other related documents for adequacy; adherence to

procedure, proper tagouts, technical specifications, quality controls,

and radiological controls; observation of work and/or retesting; and

specified retest requirements.

MWO

DESCRIPTION

079712

Reset open limit switch to stop valve stroke for

lE5-F013.

No violations or deviations were identified.

The results of the

inspections in this area indicated that maintenance activities were

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effective.

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5.

Surveillance Observation (61726)

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The inspectors observed the performance of portions of the surveillance

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listed below.

The observation included a review of the procedures for

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technical adequacy, conformance to technical specifications and LCOs;

verification of test instrument calibration; observation of all or part

of the actual surveillance; removal and return to service of the system

or component; and review of the data for acceptability based upon the

acceptance criteria.

06-RE-lC51-0-0001, Rev 31.

Local Power Range Monitor

Calibration.

No violations or deviations were identified.

The observed surveillance

test was performed in a satisfactory manner and met the requirements of

the Technical Specifications.

6.

Reportable Occurrences (90712 and 92700)

The event report listed below was reviewed to determine if the

information provided met the NRC reporting requirements. The

determination included adequacy of event description, the corrective

actions taken or planned, the existence of potential generic problems

and the relative safety significance of each event. The inspectors used

the NRC enforcement guidance to determine if the event met the criterion

for licensee identified violations.

On January 8,1993, the licensee notified the Environmental Protection

Agency and the State of Mississippi of an oil spill from a spare

transformer stored onsite within the owner controlled area. 'The

transformer oil contained polychlorinated biphenyl compounds (PCBs).

The resident inspector was notified and a four hour notification was

made by the licensee to the NRC Operations Center per 10 CFR 50.72

(b)(2)(vi).

No violations or deviations were identified.

7.

Exit Interview (30703)

The inspection scope and findings were summarized on January 19, 1993,

with those persons indicated in paragraph 1 above.

The licensee did not

identify as proprietary any of the materials provided to or reviewed-by

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the inspectors during this inspection.

The licensee had no comment on.

the following inspection findings:

Item Number

Description and Reference

50-416/92-28-01

Failure to properly man the control

room with an SR0

50-416/92-28-02

Failure to complete procedure for -

SJAE swap over

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Acronyms and Initialisms

ADHRS -

Alternate Decay Heat Removal System

ADS

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Automatic Depressurization System

APRM -

Average Power Range Monitor

ATWS -

Anticipated Transient Without Scram

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BWR

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Boiling Water Reactor

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CRD

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Control Rod Drive

DCP

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Design Change Package

DG

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Diesel Generator

ECCS -

Emergency Core Cooling System

ESF

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Engineering Safety Feature

FCV

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Flow Control Valve

HPCS -

High Pressure Core Spray

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HPU

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Hydraulic Power Unit

I&C

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Instrumentation and Control

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IFI

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Inspector Followup Item

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LC0

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Limiting Condition for Operation

LER

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Licensee Event Report

LLRT -

Local Leak Rate Test

LPCI

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Low Pressure Core Injection

LPCS -

. Low Pressure Core Spray

MNCR -

Material Nonconformance Report

MSIV -

Main Steam Isolation Valve

MWO

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Maintenance Work Order

NPE

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Nuclear Plant Engineering

NRC

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Nuclear Regulatory Commission

PCB

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Polychlorinated Biphenyls

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PDS

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Pressure Differential Switch

P&ID -

Piping and Instrument Diagram

PSW

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Plant Service Water

QDR

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Quality Deficiency Report -

RCIC -

Reactor Core Isolation Cooling

RCA

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Radiologically Controlled Area

RHR

Residual Heat Removal

R0

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Reactor Operator

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RPS

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Reactor Protection System

RWCU. -

Reactor Water Cleanup

RWP

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Radiation Work Permit

Standby Liquid Control

SBLC

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SJAE

Steam Jet Air Ejector

S0I

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System Operating Instruction

Senior Reactor Operator

SR0

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SRV

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Safety Relief Valve

- SSW

Standby Service Water

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Temporary Change Notice

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TS

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Technical Specification

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