ML20029A168

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Insp Repts 50-282/90-19 & 50-306/90-20 on 901120-910114. Violations Noted But Not Cited.Major Areas Inspected:Plant Operational Safety,Maint,Surveillance,Lers,Regional Initiatives & Cold Weather Preparations
ML20029A168
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 01/28/1991
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20029A167 List:
References
50-282-90-19, 50-306-90-20, NUDOCS 9102050002
Download: ML20029A168 (15)


See also: IR 05000282/1990019

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U. S. NUCLEAR REGULATORY COMMISSION'

REGION Ill

Reports No. 50-282/90019(DRP);50-306/90020(DRP)

Docket Nos. 50-282; 50-306

License Nos. OPR-42; DPR-60

Licensee: Northern States Power Company

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414 Nicollet Mall

Minneapolis, MN 55401

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Tacility Name:

Prairie Island Nuclear Generating Plant

Inspection At:

Prairie Island Site, Red Wing, MN

Inspection Conducted:

November 20, 1990 through January 14, 1991

Inspectors:

P. L. Hartmann

D. C. Kosloff

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Approved By:

B.'L. J rg sen, Chief

i/m/pt

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Reactor rojects Section 2A

Date

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Insp_ection Summary

Inspection on November 20, 1990 through January 14, 199_1

50-282/90019(DRP); 50-306/90020(DRP))

TheportsNo.

K'reas Inspected:- Routinh unannounced inspection by resident inspectors of

-Licensee Action-on Previous Items, Plant Operational Safety, Maintenance.

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Surveillance, Licensee Event Reports, Regional Initiatives,'and Cold Weather

-Preparations.-

=Results:

In the seven areas inspected, two non-cited violations of NRC

requirements were identified and are discussed below. One unresolved item

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identified in the security area is-also' discussed below.

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Operations

Unit 1 operated at- full power, interrupted by one reactor trip an'd a brief

power reduction for main condenser cleaning. Unit 2. operated at full power,

interrupted by one reactor trip. Each trip was from full power and recovery-

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The component failures which initiated each trip are-

was prompt in each case.

A non-cited

discussed below in the Engineering and Technical Support Section.

violation, involving f ailure to establish a continuous fire watch within one

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The event had minimal safety impact because an hourly.

hour, was identified. fire watch patrol was initially _ established (instead of a continu

9102050002 910128

PDR

ADOCK 05000282

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PDR

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and the one hour requirement was exceeded by only six minutes.

This event is

discussed in paragraph 6.c.

In addition, a shift supervisor found a valve open

in a 3/4-inch line penetrating containment. This event also had minimal safety

impact; there were other closed valves in the line.

Maintena_nce and Surveillanc_e

No deficiencies were noted by the inspectors' observation of work activities.

Engineering _and Te_chnical Support

Two reactor trips occurred which involved equipment failure and system design

wea knes ses . On November 21, 1990, the Unit I reactor tripped from a turbine

trip at 100 percent power.

The turbine trip was caused by a generator trip

on high bus duct temperature. A failed circuit breaker for one bus duct

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cooling fan led to the elevated bus duct temperature.

This event is discussed

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in paragraph 6.d.

On December 29, 1990, the Unit 2 reactor tripped from a high

negative flux rate caused by rod control system component failures.

This event

is discussed in paragraph 3.b.

In addition, engineers found that, due to an

inadequate understanding of the cooling water design, several cooling water

valves and chill water velves had not been included in the inservice test

program.

This event is discussed in paragraph 6.e.

Also, a non-cited

violation for exceeding a Technical Specification cooldown rate for the

Unit 1 pressurizer was identified.

This event is discussed in paragraph 6.a.

Security

A fitness-for-duty is.ue is discussed in paragraph 7.b.

An unresolved item is

assigned to an event involving unescorted access screening.

Safety Assessment / Quality Verification

The insoectors determined that there were several discrepancies between the

containnent penetration table in the Technical Specifications (TS) and the

contairnnent penetration table in the Updated Safety Analysis Report. This

combined with other deficiencies in the containment penetration TS text make

it difficult to understand the intent of the TS. This situation is discussed

in Paragraph 6.e.

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DETA_I L_S

1.

Per_s_o_ns_ Contacted

_No_rthern States Power Company _(NS_P)

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  • L. Eliason, Vice President Nuclear Generation
  • C

Blair, Executive Vice Precident ' Power Supply

  • E. Watzl, General Manager, Prairie Island Site
    • H. Sellman, Plant Manager
  1. M. Wadley, General Superintendent, Operations
    • D. Mendele, General Superintendent, Engineering
  1. G. Lenertz, General Superintendent, Maintenance

A. Snith, General Superintendent, Planning and Services

  1. R. Lindsey, Assistant to the Plant Manager
  1. D. Schuelke, General Superintendent, Radiaticn Protection
  1. G. Miller, Superintendent, Operations Engineering
  1. K. Beadell, Superintendent, Technical Engineering

T. Breene, Superintendent, Technical Engineering

  1. M. Klee, Superintendent, Quality Engineering
  • D

Musolf, General Manager, Nuclear Support

  • B. Stephens, Superintendent, Design Standard Engineering NPD
  • G. Goering, Manager, Nuclear Projects Department
  1. A. Hunstad, Staff-Engineer

R. Conklin, Supervisor, Security.and Services

J. Leveille, Nuclear Support Services

'*E. Eckholt, Plant Licensing Engineer

U._._S. Nuclear Regulatory Commission (U.S. NRC)

  • C, Paperiello, Deputy Regional Administrator
  • H. Miller, Director, Division of Reactor Projects
  • T. Martin, Director, Division of Reactor Safety
  • M. R'ng, Chief, Engineering Branch
    • H Clayton, Chief, Projects Branch 2
  • M. Phillips, Chief, Operational Programs Section
    • B. Jorgensen, Chief, Projects Section 2A
  • I

Yin, Senior Mechanical Engineer

  1. P. Hartmann, Senior Resident Inspector
  • E. Schweibinz, Senior Project Engineer
    • R. Bywater, Reactor Engineer
  • N. Choules, Reactor Engineer
  • R. Langstaff, Reactor Inspector
    • D. Kosloff, Resident Inspector
  • C

Brown, Reactor Engineer-

  1. Denotes those present at the exit interview of January 15, 1991.

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  • Denotes those present at the Management Meeting in Region III on

December 6, 1990.

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'2.

Li_cen_s_ee_ Action on_P_revious Inspection Findings (92701, 92702)

-a.

(Closed) Violation __(50_-282/88012-02(DRP)): Failure to Stoke Time

Test" Pressurizer Power Operated Relief Valves (PORVs)

The inspector identified that the h

urizer PORVs had never been

stoke time tested prior to January of 1988.

Because the-licensee had

not classified these valves as ASME Code Classes 1, 2, or 3 valves,

it had not included-them in its ASME Section XI testing program.

The

licensee had developed testing requirements and added the pressurizer

PORVs to'the testing program prior to the issuance of the violation.

Surveillance Procedures (SP) 1291 and 2291, " Pressurizer PORV Stoke

Timing'l, were also implemented prior to the issuance of the violation.

The inspector verified _the surveillances-have been performed at the

frequency required since the violation was issued.

This matter is

closed.

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Failure to Perform

lClosed) Violation (50_-282/88019-01(DRP)):

b.

ersonnel Airlock Door Seal Test

Technical-Specification,-4.4.A.2 Containment Leakage Tests, requires

thatthecontainmentpersonnelalrlockdoorsealsbeseal-tested-by

SP 1132 (2132) within three days of opening the personnel-airlock. A

violation was issued following a second example of not performing

this surveillance when required.

In response, the licensee performed

the test and emphasized testing'requireuents to involved personnel.

The inspector identified several recent containment entries and

reviewed the' tests completed following the entries.

No anomalies

were noted.

Licensee performance related to this surveillance

requirement appears adequate. This matter is closed.

c.

(Closed) Unresolved Item (282/89024-01(DRP); 306/89024-01(DRP)):

-Ti1Tegral Welded Attachments (IWA) with Increased Loads Were not

Evaluated for Acceptability

A Region III inspector reviewed Calculation No. 0910-242-001,

" Prairie Island IWA Criteria / Evaluation", Revision 0, February 1990.

This calculation, generated by the licensee to address this issue,

evaluated 159 IWAs with load increases. These loadt were derived

from IE Bulletin 79-14 reanalyses or later modification calculations.

All of the welds associated with the IWAs were shown to be acceptable.

The effects of localized stresses on the piping components were also

shown to meet the original design code. The IWA evaluation

methodology will be proceduralized to prevent future questions

and to assure consistent application of acceptance criteria.

No discrepancies or inconsistencies were noted in the calculation by

the inspector.

In all cases the methodology appeared to be

conservative. Since no modifications were required to any of the

pipe supports with IWAs, the licensee concluded that the original

design criteria was sufficiently conservative.

Based on the above

discussion, this item is closed.

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d._

(Closed) Violation (282/880201-01; 306/880201-01):

Inadequate

evaluations f or use of commercial ~~g'FWe items BTal's) in

safety-related systems

By letter dated November 29, 1990, the licensee committed to improve

the CGI evaluaticn process.

Based on a review of these proposed

actions, the inspector determined that the process-described is

adequate and this item is closed.

No violations, deviations, unresolved, or open items were identified.

3.

Operational _ Saf_e_ty Verificatf o_n (7_1707, 93702)

a.

Routine Inspection

The inspector observed control room operations, reviewed applicable

logs, conducted discussions with control room optrators and observed

shif t turnovers.

The inspector verified operability of selected

emergency systems, reviewed equipment control records, and verified

the proper return to service of affected components, conducted tours

of the auxiliary building, turbine building and external areas of

the plant to observe plant equipment conditions, including potential

fire hazards, and to verify that maintenance work requests had been

initiated for the equipment in need of maintenance. The inspectors

reviewed a third party audit of plant performance for a two-year

period which revealed no significant safety issues.

-b ,

Event Followup.

On November 21, 1990, at 3:45 p.m., the Unit I reactor tripped from

a main turbine trip while the unit was at full power.

The cause of

the turbine trip was determined to be a breaker tripping open for

the in-service main transformer bus duct cooling fan without the

-standby bus-duct fan starting.

The intent of the circuit design was

for the standby bus duct fan to be energized and prevent a generator

lockout (and generator trip) from high bus duct temperature.

However, the circuit design did not achieve the intended design

function.

Followino replacement of an intermediate range detector

ana-other minor repairs in the secondary plant, the unit was

restarted at 10:29 a s , and was placed on-line at 3:41 p.m.

on November 22, 1990. This event is discussed further in

paragraph 6.d.

At approximately 3:45 a.m. on December 10, 1990, a shift supervisor

(SS) found valve 2S1-20-16, Test Line Flow Instrument inlet

Isolation, open.

By procedure the valve should have been closed.

The SS immediately closed the valve.

Initially, the licensee

considered the valve to be a containment isolation valve.

Therefore, since the valve was found open and not administratively

controlled, this was considered to be contrary to Technical Specification 3.6.C.1.

However, upon further review, the licensee

concluded that the Technical Specifications did not require the

valve to be closed. After discussing the event with the inspectors,

the licensee stated that it would report the event and its

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evaluation in a'su?plement to LER 50-282/90018 (discussed in

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complete their evaluation of this event during their review of the

LER supplement.

On December 29,1990, at 10:34 p.m., the Unit 2 reactor tripped from

a negative flux rate trip while the unit was at full power.

All

safety systems functioned as designed. The cause of the negative

flux rate trip was determined to be a failure of the stationary coil

group B regulator circuit card in the rod control system.

The

reference voltage (v-ref) provided by this card fell to zero, which

removed current to the stationary coils for the four control bank 0

rods. _These rods fell into the reactor, causing the negative flux-

rate trip. The intent of the rod control circuit design is for the

alarm card to detect a loss of v-ref and generate an " urgent failure"

condition. This 3revents-the affected rods from dropping by applying

hold current to t1e moveable coils.

However, due to a simultaneous

or previous alarm card failure, this intended design function was not

achieved.

Following replacement and testing of the alarm and

regulator cards, the unit was restarted at 10:34 a.m. and-placed

on-line at 1:32 p.m. on December 30, 1990.

The licensee has experienced previous reactor trips on Unit 2 due to

similar rod control component failures (December 21 and 26, 1989).

In response, the licensee conducted rod control circuitry

refurbishment during the winter 1990 Unit I refueling outage and the

fall 1990 Unit 2 outage. The licensee is evaluating the merits of

that activity, which is conducted by a vendor. The inspectors will

review the licensee corrective actions within LER 50-306/90013.

No violations, deviations, unresolved or open items were

identified.

4.

MaintenanceObservation(71707,37700,62703)

Routine, preventive,_and corrective maintenance activities were observed

to ascertain that they were conducted in accordance with approved

procedures, regulatory guides, industry codes or standards, and in

conformance with Technical Specifications. The following items were

considered during this review: adherence to limiting conditions for

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operation while components or systems were removed from service,

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approvals were obtained prior to initiating the work, activities were

accomplished using approved procedures and were inspected as applicable,

functional testing and/or calibrations were performed prior to returning

components or systems to service, quality control records were

maintained, activities were accomplished by qualified personnel,

radiological controls were implemented, and fire prevention controls were

implemented.

Portions of the following maintenance activities were observed during the

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inspection period:

Troubleshooting and Repair of Unit 2 Rod Control Power Cabinet 2BD

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Troubleshooting and Repair of Unit 1 Rod Position Indication

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Preventive Maintenance of No. 12 Diesel Cooling Water Pump

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Troubleshooting of Unit 1 Intermediate Range Nuclear Instrumentation

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Pouring of Concrete Wall for New Emergency Diesel Generator (EDG)

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Building. While a contractor was pouring concrete for the north

wall of the new EDG building, the forms allowed concrete to escape

into the space between the new EDG building and the existing metal

wall of the turbine building.

The licensee's initial evaluation of

this condition concluded that the structural integrity of the wall

was not adversely affected. The inspectors discussed the condition

with a Region III specialist, who has discussed the condition

further with the licensee. The Region-III inspector will review the

licensee's documentation and verification activities related to this

condition in a future inspection.

No violations, deviations, unresolved, or open items were identified.

5.

Surveillance (6_1726,_71707)

The inspector witnessed portions of surveillance testing of

safety-related systems and components. The inspection included

verifying that the tests were scheduled and performed within

Technical Specification requirements, observing that procedures

were being followed by qualified operators, that Limiting Conditions

for Operation (LCOs) were not violated, that system and equipment

restoration was completed, and that test results were acceptable to

Technical Specification and procedural requirements.

Portions of the following activities were observed:

SP 1093

D1 Diesel Generator Slow Start and Train A Auto Load

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Sequencer Test

SP 1091'

Containment Fan Coil Units Surveillance Test

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While testing the operation of the Fan Coil Units' motors,

the licensee found that one of the associated ventilation

dampers appeared to have failed in its safety position.

Licensee personnel entered containment and verified that

the damper was in its safety position.

Later, the

licensee determined that the failure resulted from a

fuse losing continuity with its fuse holder. This is an

example of a plant aging issue which has been previously

identified on other plant systems. The licensee is

continuing with its plant-wide program to eliminate this

problem. The inspectors will continue to monitor the

licensee's progress with this program.

SP 1158

Cooling Water Valve Test (Unit 1)

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The inspectors observed testing of valves which had

mistakenly been excluded from the test. The test was

used to establish a base line operating time and was

controlled as a maintenance activity so the test

procedure was not used.

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SP 2158

Cooling Water Valve Test (Unit 2)

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This test was performed in the same manner as SP 1158.

No violations, deviations, unresolved, or open items were identified.

6.

LER Fol_lowup (92700)

a.

(Closed) LER_ 50_-282/9000_2_-LL :

Excessive Pressurizer Cooldown Rate

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and Excessive Spray / Pressurizer Temperature Difference

This LER described a Technical Specification (TS) violation in which

the cooldown rate limit of 200 degrees F/ hour for the pressurizer and

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the limiting temperature difference of 320 degrees F between the

pressurizer auxiliary spray and the pressurizer had been exceeded.

In this case, the licensee violated TS 3.1.B.2.

Specifically, the

maximum cooldown rate for the pressurizer was 265 degrees F/ hour

measured by the pressurizer water space temperature.

During the

cooldown, the operators verified the temperature difference between

the pressurizer and the pressurizer auxiliary spray as being less

than 320 degrees F by using the control board indication.

Later, a

more precise determination was obtained by using the Emergency

Response Computer System (ERCS) which indicated an actual temperature

difference of 349 degrees F.

The ERCS was used on the cooldown to

gather surge line thermal stress information.

Upon discovery of

these anomalies, the licensee modified the cooldown procedure (C.1.)

so that the pressurizer water space temperature is used in computing

the cooldown rate and the ERCS is used to determine the temperature

difference between the pressurizer and the pressurizer auxiliary

spray.

In addition, the licensee contracted Westinghouse Electric

Corporation to determine whether the repetitive pressurizer cooldowns

and heatups had any effect on the vessel protection against brittle

failure and on the approach to fatigue limits for transients of-this

type.

By letter dated May 23, 1990, Westinghouse Electric Corporation

issued a report titled, " Rapid Pressurizer Cooldown and Heatup

Evaluation for Northern States Power Company, Prairie Icland Unit 1"

(MT-SMDT-167 Rev. 1). This report, which was reviewed by NRR staff,

assesses the structural stability of the pressurizer vessel when

subjected to the cooldown and heatup transients described in the LER.

The report covers fracture mechanics and fatigue analyses at the

critical locations of the pressure vessel when subjected to 50

thermal transients. The analysis considered the possibility of

vessel failure by an abrupt and brittle fracture mechanism which is

conservative relative to other failn ~ modes. The effects on the

fatigue limit-being approached were aise considered. The report

concludes that transients have not compronMed the structural

integrity of the pressurizer.

NRR agreed witi the conclusions o'ren

in the report based on review of the analyses.

In additic.,, NRR

found the corrective action, revising the plant cooldov;, procedure,

would ensure that the fatigue limits would not be c.npromised in the

future.

The inspector verified the cooldown procedure was revised.

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This licensee-identified violation (50-282/90019-01(DRP)) of TS is

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not being cited because the criteria specified in 10 CFR 2, Appendix

C, Section'V.G. of the NRC Enforcement Policy were satisfied.

This

exercise of discretion is being given because the NRC wants to

encourage and support licensee. initiative for self-identification and

-correction of problems. A non-cited violation must meet all of the-

following_ criteria: _(:) It was identified by the licensee; (b) It is

normally classified as a Severity Level IV or V; (c) It was reported,

if required; (d) It was or will be corrected, including measures to

prevent recurrence, within a reasonable time; and (e) It was not a

willful violation or a violation that could reasonably be expected to

have been prevented by the licensee's corrective action for a

previous violation,

b.

(Closed) LER 50-306/90009-LL:

Unit 2 Reactor Trip from Zero Power

Wen Fuses Were Removed From the Wrong Nuclear Instrumentation

Channel Drawer

On October 7, 1990, Unit 2 was critical at zero power following a

refueling outage.

Zero power physics testing had just been completed.

The reactivity computer used for physics testing was to be

disconnected from Nuclear Instrumentation Power Range Channel N41.

An instrument and control (I&C) technicier, when assigned to do_the

work,. reviewed the controlling procedure and the logic diagrams to

determine required actions. With procedure in hand, he removed the

control power and instrument power fuses from the front panel of NIS

Intermediate Range Channel N35 instead of Power Range Channel N41.

This caused a unit trip signal, because the intermediate range

nuclear instruments utilize a one of two logic verses the two of four

logic utilized by the power range instruments.

Cause of the event was personnel error in removing fuses from the

wrong NIS channel drawer.--Channel N35 $s immediately above Channel

N41 on the NIS rack which led to the error.

The technician failed to

use self-checking when removing the fuses.

The licensee corrective action included counseling the I&C-technician

regarding the self-checking-plant policy and revising the controlling

procedure D-30, " Post Refueling Start-Up Testing". - The inspector

verified the procedure was changed (Rev. 20) to utilize power range

channel N44, since an intermediate range channel is not above this

power range d-awer.

The licensee also improved labeling of the

nuclear instrument panel covers and the inspector verified the

change.

This matter is closed.

c.

(Closed)-LER 50-282/90016-LL:

Failure to Establish a Continuous Fire

Nitch When Removing a Sprinkler System from Service Caused by

Inadequate Procedure

On November 6,1990, both units were at 100 percent power.

Surveillance procedure SP 1196, " Fire Protection Safety-related

Sprinkler System Test," was in progress. This 18 month surveillance

checks operation of deluge valves, so fire suppression supply water

must be isolated to prevent actual system actuation.

Since the

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procedure would require the sprinkler system in the emergency diesel

generator rooms to be isolated, aersonnel performing the test asked

the Shift Supervisor _to establisi a continuous fire watch in the

rooms. The Shift Supervisor reviewed Technical Specification 3.14.C.2,

and at 9:14 a.m. he ordered the isolation of the zone.and started an

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hourly fire watch.

B;ckup fire suppression equipment had also been

made available to compensate for isolation of the sprinkler system.

When the personnel performing the test entered the zone at 10:20 a.m.

and realized no continuous fire watch was present, they called the

Shift Supervisor to discuss the matter.

The Shif t Supervisor made a

further review of Technical Saecification 3.14.C.2, realized his error,

and at 10:25 a.m. he establis1ed a continuous fire watch.

The licensee identified the cause of-the event as an inadequate

procedure. The surveillance procedure references Technical Specification 3.14, Fire Detection and Prctection Systems, but does

not specifically require establishment of a continuous fire watch

with backup fire suppression equipment.

The procedure contains only

a note that warns that a continuous fire watch is required if the

sprinkler system is out of service for more than an hour.

The Shift

Supervisor misread the fire watch requirement and instead of

establishing _a continuous fire watch within one hour, he established

an hourly fire watc_h.

Technical Specification 3.14.C.2 requires a continuous fire watch

with backup fire suppression equipment to be established within one

- hour whenever the spray and sprinkler system is inoperable.

Backup

fire suppression equipment had been established, but a continuous

fire watch was not established for one hour and six minutes, although-

an hourly firewatch was established.

The inspector discussed the event with licensee management following

the event.

The inspector verified the surveillance procedure was

revised as described in the LER.

Thislicensee-identifiedviolation-(50-282/90019-02(DRP))of

Technical Specification 3.14.C.2 is not being cited because the

criteria specified in 10 tpfs 2, Appendix C,Section V.G. of the NRC

Enforcement Policy were satisfied. This exercise of discretion is

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being given because the_NRC-wants to encourage and support licensee

initiative for self-identification and correction of_ problems.

A

non-cited violation must meet all of the following criteria:

(a)It

was identified by'the licensee; (b) i+ is normally classified as a

Severity Level IV or V;-(c) It was r; parted, if required; (d) It was

or will be corrected,-including measures to prevent recurrence,

within a reasonable time; and (e) It was not a willful violation or a

violation that could reasonably be expected to have been prevented by

the licensee's corrective action for a previous violation,

_C_losed) LER 50-282/900_ _7_-LL:

Reactor Trip Caused by Inadequate

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d.

Design of Main Generator Bus Duct Cooling System

On November 21, 1990, while Unit I was at full power, a non-licensed

operator noticed that there was no indication that either Unit 1 Bus

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Duct Cooling Fan was operating.

Normally one fan is operating and

-one is in standby.

Af ter finding the breaker tripped for No.11 Bus

Duct Cooling Fan, the operator discussed the condition with the

control room and was instructed to start the No.12 Bus Duct Cooling

Fan. 'There were no alarms in the control room and the bus duct

temperature indication in the control room was not abnormally high.

The unit tripped shortly af ter the fan was started.

The inspector

responded to the control room and observed trip recovery activities.

One rod-at-bottom light was not lit immediately after the trip but it

did light a short time later.

The licensee concluded that this

problem was due to dirty electrical contacts on a signal conditioning

circuit card. The contacts were cleaned and the system was restored

to normal. An intermediate range flux detector also failed and was

replaced. All of the manufacturer's recommended diagnostic tests on

the detector had normal results and the failure mechanism is unknown.

Minor balance-of-plant problems occurred and were repaired prior to

restart or shortly thereaf ter.

The licensee determined that the trip was caused by high bus duct air

temperature.

The main generator bus is normally cooled by a bus duct

cooling fan that circulates hot air from the bus duct through a

cooling coil.

The bus duct cooling system is not a safety-related

system. At about 10:45 a.m. on November 21, 1990, Qe circuit

breaker for the operating fan tripped open.

No direct indication of

this condition was provided in the control room.

The bus duct air

resistance temperature detectors (RTDs) are located in the fan

suction duct. When the fan stopped, heated bus duct air was no

longer drawn past the RTDs and the temperature at the RTDs was no

longer representative of the temperature in the bus ducts. The

temperature at the RTDs began to drop (to ambient) as the temperature

in the bus duct began to rise.

The RTDs were inputs for a high

temperature alarm and a computer temperature indication in the

control room.

When the standby fan was started at about 3:45 p.m.,

it blew the hot air from the bus duct past the RTDs and the indicated

temperature quickly exceeded the control room high temperature alarm

setpoint and the main generator trip setpoint. The main turbine

tripped, providing the trip signal which tripped the reactor.

The

licensee's system description (B22B, Rev.1, July 14,1989) for the

main generator incorrectly states that."The standby fan starts

automatically if the primary fan trips . . ." Neither B22B nor the

operatingprocedureforbusductcooling(C22.5, August 1,1975)

describes the location of the temperature detector.

Had these

procedures been more detailed, the operators might have restored the

plant to normal operating conditions without a plant trip.

The licensee concluded that the cause of the event was inadequate

design of the bus duct cooling control system. The inspectors

concluded that the root causes of the event were design weaknesses

in the bus duct cooling control system and alarms, and a lack of

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trainino and procedural guidance to compensate for the design

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weaknesses.

Although th.s LER was more thorough than some past LERF, the

inspectors observed several deficiencies in the LER.

These

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deficiencies were discussed with licensee personnel. The most

significant deficiency was that the LER did not completely describe

the event from the perspective of the operator.

The inspectors verified that the licensee disabled the high bus duct

temperature generator trip, improved procedure C22.5, and initiated a

modification to provide en annunciator alarm to indicate when both

bus duct fans are not operating.

This LER:is closed.

e.

(0 )en) LER__ _5_0 _282/_90018-LL: Discovery That Certair Valves Should Be

Su) ject to AS74E Section XI Testing Found through Design Basis

Reconstruction

The licensee found that several valves in the ;ooling water and

chilled water systems should have been includei in its ASME Section

XI inservice testing program, but they were not

The l_icensee

discussed the findings with the inspectors and A scribed its plans

for verifying the operability of the valves.

The inspector observed

valve operability verification testing and discussed the results with

licensee engineers.

The valves are considered operable.

The

licensee is continuing its evaluation and has committed to submission

of a supplement to this LER.

During the review of this event, the

inspectors discovered errors in the containment penetration table in

_the Technical Specifications and discrepancies between the containment

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penetration table in the TS and the containment penetration table in

the Updated Safety Analysis Report.

These errors and discrepancies

make the intent of the TS unclear.

The inspectors discussed these

errors and discrepancies with the licensee.

The licensee is

developing a method to correct these errors which will be

discussed in the supplement to_the LER. The licensee also stated

that the mispositioning of valve 2SI-20-16 would be discussed in the

supplementtotheLER(seeparagraph3.b.).

The inspectors will

continue to inspect the licensee's efforts in this area fn future

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inspection.

This LER will remain open until the inspectors review

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the licensee's LER supplement.

Two violations (not cited) and no deviations, unresolved, or open items

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were identified.

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7.

_ Regional Initiative _(92701,'TI2515/106)

a.

NRC Region III management has reviewed the existing open items for

the Prairie Island Station and determined that the following open

items will be closed administratively due to their safety

significance relative to emerging priority issues and to the age of

the item. The licensee is reminded that commitments directly

relating to these open items are the responsibility of Lthe licensee

,

and should be met as committed.

NRC Region III will review licensee

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actions by periodically sampling administratively closed items.

(Closed) Bulletin 85003: Motor Oper:ted Valve Common Mode Failures

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During Plant Transients Due to Improper Switch Settings

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(50-282/85003-BB(DRS);50-306/85003-BB(DRS))

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(Closed) Bulletin 79002, Rev. 1_ Supplement ___1:

Pipe Support Base

PTaWDesigns Using concrete Expansion Anchnr Bolts

(50-306/79002-BB(DRS))

b.

Fitness For Duty _(TI2515/106): One unresolved item was identified

regarding the apparent tailure to conduct a management and medical

determination of fitness for duty for an individual who had received

treatment for alcohol abuse.

During an audit conducted on October 24, 1990, a representative of

the licensee's Corporate Security Department discovered information

that appeared to indicate that a guard at Prairie Island should not

have been granted unescorted access to the site. The licensee

conducted an extensive investigation of the contractors who were

responsible for conducting the background investigation and

evaluating the information.

The investigation disclosed that the

individual's background screening records appeared to indicate that

about two years prior to being hired, the individual had

unsuccessfully participated in an alcohol rehabilitation program

and was, as a result, terminated from his employment.

The records

contained no information to show that those facts were evaluated, as

required by 10 CFR 26.27, prior to the guard being granted unescorted

access.

When this situation was identified, the licensee suspended the

individual's site access. A management and medical evaluation was

conducted and the licensee determined that the individual must

enroll in an alcohol treatment program.

The guard began the program

and unescorted access was temporarily reinstated. The individual is

to perform duties as an unarmed watchman pending successful

completion of the treatment program.

Thisisconsideredanunresolveditem(50-282/90019-03(DRSS);

50-306/90020-03(DRSS)). An unresolved item is a matter about which

additional information is required in order to determine whether it

is acceptable, a violation, or a deviation. Currently, no

additional information or written response is needed from the

licensee. The resolution of this issue will be addressed by

separate correspondence.

No violations, deviations, or open items were identified. One unresolved

item was identified.

8.

M_anagement Meeting (30702)

_

A management meeting was held at the Region III office on

December 6, 1990, between the NRC represented by Dr. C. J. Paperiello,

and Northern States Power, represented by Mr. C. J. Blair. Others in

attendance are indicated in Paragrapn 1 above.

Mr. E. L. Watzl provided a briefing on the development of the Site

Organization structure at Prairie Island.

The management reorganization,

including creation of the Site General Manager position, places more

responsibility, accountability, and authority at the site.

The

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reorganization also consolidates redundant activities and removes

activities from the plant- staff that may not directly contribute to the

safe and reliable operation and maintenance of the plant.

Mr. G. Goering-and Mr. B. Stephens provided an update of the

Configuration Management (CM) program. The Design Basis Document (DBD)

element of the CM program was discussed. All safety-related plant

systems and structures and key topical areas are scheduled to be

addressed by December 31, 1994

Discrepancies and open items identified

by DBD development and verification are evaluated, prioritized, and

resolved in a Follow-on Item program.

Mr. M. Sellman and Mr. D. llendele provided an update on " attention to

detail" issues.

Improper work practices and inadequate written

communications were found to be root causes for personnel errors at

prairie Island during the previous 12 months.

Several specific steps

have been undertaken to improve these areas, including:

development of

awareness programs, quality teams, and a video tape presentation to all

employees including management emphasis on the need to self-check work;

revision of maintenance procedures, development of procedure writing

guides, and training in procedure writing; and enhancement of technical

support through the recent plant reorganization.

9.

C_old Weather _ Preparatio_ns1(71714_)

In conjunction with the requirements of HRC Inspection Procedure 71714,

Cold Weather Preparations, the inspectors reviewed-the licensee's

surveillance procedure, SP-1637, " Winter Plant Operation," Revision 9.

Additionally, the inspectors performed tours during cold weather (-22

degrees F) to determine the adequacy of the licensee's program.

Tours

of the turbine building, auxiliary building, radioactive waste buildings,

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and screenhouse revealed temperatures well above freezing with

safety-related fluid systems appearing properly heat-traced or contained

within heated structures.

Some minor operational problems occurred during cold weather during this

inspection period. A level indicator for the 121 Diesel (0-1) Fuel Oil

Storage Tank operated sporadically during diesel generator operation.

The rapid turnover of air within the diesel room during operation cooled

the 3/8-inch sensing line for this level transmitter to a point where an

inline air regulator did not function adequately.

The licensee put a

portable heater in the area, which restored normal indication.

The

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licensee plans to begin routine preventive maintenance on the four air

regulators for Diesel Fuel Oil Tank indicators to prevent recurrence of

the problem. The licensee also plans to blow down the air supply to the

Emergency Diesel Generator air start control valves each month.

No violations, deviations, unresolved, or open items were identified.

10. Management _ Interview

The inspectors met with the licensee representatives denoted in aaragraph

1 at the conclusion of the report period on January 15, 1991.

T ;e

inspectors discussed the purpose and scope of the inspection and the

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findings. The inspectors also discussed the likely information content

- of the-inspection report with regard to documents-or processes reviewed

by the inspectors during the inspection.

The licensee did not identify

any documents or processes as proprietary.

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