05000334/LER-1982-031-03, /03L-0:on 820826,main Feed Regulating Valve FCV-FW-498 for C Steam Generator Found Leaking Excessively When Shut.Caused by Improper Seating of Seat Assembly Into Valve Body.Maint Procedure Revised

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/03L-0:on 820826,main Feed Regulating Valve FCV-FW-498 for C Steam Generator Found Leaking Excessively When Shut.Caused by Improper Seating of Seat Assembly Into Valve Body.Maint Procedure Revised
ML20027B752
Person / Time
Site: Beaver Valley
Issue date: 09/17/1982
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20027B751 List:
References
LER-82-031-03L, LER-82-31-3L, NUDOCS 8209300063
Download: ML20027B752 (2)


LER-1982-031, /03L-0:on 820826,main Feed Regulating Valve FCV-FW-498 for C Steam Generator Found Leaking Excessively When Shut.Caused by Improper Seating of Seat Assembly Into Valve Body.Maint Procedure Revised
Event date:
Report date:
3341982031R03 - NRC Website

text

U.S. NUCLEAR REGULATORY COMMISSION NRC PORM.3Eg g7. m LICENSEE EVENT REPORT CONTROL BLOCX: l l

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80 61 OOCKET NuadSER 68 SS EVENT QATE 74 78 REPORT DATE 80 EVENT DESCRIPTION AND PROSA8LE CONSEQUENCES h l o 121 i During a plant startup FCV-W-498 (main feed regulatine valve for C I

ITTTlI steam generator) was identified as having excessive leakane. when shut.

I lo141l A load reduction was inade and FCV-W498 was inninead _ vin Mov-1:U-l uc.

I IO Is! I Piant operation continued via the bypass valve FCV-N-499.

There were no 1

1016 l l nafety imn11cnefons duri n a ehi n incidane dua en eha nnavnh 414 ev nf tha l

l0l7l l header isolation MOV-N-156C, which would have provided containment I

ITTTII isolation if reautred.

7 8 9 CODE COO 9

COMPONENT CODE Sue E

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9 to 11 12 13 18 19 SSOUENTIAL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR REPORT NO.

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23 38 30 37 40 43 43 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIOP.S 27 1 101 l Investication into Fev-1% AqR internals revenind rhne ebn a nn e no e:nmb l y 1

It i1l l (Cneo) hnd not bonn senrod ( th re nde d) enmninen1v inen eh n knar o f th e j

gI valve.

Future maintenance will require both torque limitn and feeler i

Iil3l l gnge measurements to insure proper seatinn of the <' ace assembly.

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% POWER OTHER STATUS 1 OV R DISCOVERY DESCRIPTION Ii 15_I (,J.j@ l 0 l 210 l@l N/A l

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as so PERSONNEL EXPOSURE 5 NUMSER TvPE QESCRIPTTON I 1 l 7 l l 01 O l 0 lhl Z lhl N/A l

PERSONNEL iN;Udits NUMGER OESCRIPTION 11 lall0l0l0l@l N/A l

  • 00ss OP OR OSacES PactuTv 8209300063 820916 43 PDR ADOCK 05000334 rvPE 0:sCRimON S

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. S. Lacey PHONE:

NAME OF PREPARER i

.o Attachment to LER 82-031/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is available or needed to satisfy the reporting requirement.

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