ML20027A998

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Corrected Notice of Violation from Insp on 820526-0621, Submitted W/Corrected IE Insp Repts 50-321/82-20 & 50-366/82-20
ML20027A998
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 07/30/1982
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20027A989 List:
References
50-321-82-20, 50-366-82-20, NUDOCS 8209160250
Download: ML20027A998 (2)


See also: IR 05000321/1982020

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APPENDIX A

NOTICE OF VIOLATION

Georgia Power Company

Docket Nos. 50-321, & 50-366

Hatch 1 and 2

License Nos. OPR-57 & NPF-5

As a result of the inspection conducted on May 26 - June 21, 1982, and in

accordance with the NRC Enforcement Policy, 47 FR 9987 (March 9,1982), the

following violation was identified.

A.

Technical Specification 6.8.1 requires that procedures controlling the

operation of safety-related systems be implemented.

Plant procedure

HNP-1-1200, Plant Service Water, Data Package 1, requires that PSW pump

cooling water isolation valves be locked open and other status be double

verified.

Contrary to the above, on June 18, 1982, the Unit 1 cooling water isolation

valve for ID Plant Service Water (PSW) pump was found by the inspector not

locked open and properly verified in that position as required by the

HNP-1-1200 procedure. The valve was later determined to be partially open.

This is a Severity Level IV Violation (Supplement I). This is a repeat

item. A similar occurrance was brought to your attention in our letter of

April 8,1982.

B.

Technical Specification 3.9.12.a requires that operations involving an

increase in reactor decay heat load or a positive reactivity change be

suspended when the Residual Heat Removal (RHR) system is inoperable.

Contrary to the above, on April 19, 1982, the licensee failed to declare the

Unit 2 "A" loop RHR system inoperable and halt refueling operations when

maintenance personnel de-energized the vertical portion of the 601 panel

(RHR section) in the control room. The vertical portion of the RHR rection

of the 601 panel had been de-energized for approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> prior to

being identified to the licensee by the inspector.

This is a Severity Level IV Violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, you are hereby required to submit to

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this office within thirty days of the date of this Notice, a written statement or

explanation in reply, including:

(1) admission or denial of the alleged viola-

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tion; (2) the reasons for the violation if admitted; (3) the corrective steps

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which have been taken and the results achieved; (4) corrective steps which will

be taken to avoid further violations; and (5) the date when full compliance will

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8209160250 020907

PDR ADOCK 05000321

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Georgia Power Company

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Docket Nos. 50-321, & 50-366

Notice of Violation

License Nos. DPR-57 & NPF-5

be achieved. Consideration may be given to extending your response time for good

cause shown.

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Date:

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