05000315/LER-1983-030-03, /03L-0:on 830402,while on Tour,Security Guard Discovered Diesel Room AB Cardox Sys Isolated W/No One in Room.Caused by Personnel Error.Operator Instructed on Proper Procedures for Exiting Carbon Dioxide Protected Areas

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/03L-0:on 830402,while on Tour,Security Guard Discovered Diesel Room AB Cardox Sys Isolated W/No One in Room.Caused by Personnel Error.Operator Instructed on Proper Procedures for Exiting Carbon Dioxide Protected Areas
ML20023B819
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/29/1983
From: Don Krause
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20023B804 List:
References
LER-83-030-03L-01, LER-83-30-3L-1, NUDOCS 8305060414
Download: ML20023B819 (1)


LER-1983-030, /03L-0:on 830402,while on Tour,Security Guard Discovered Diesel Room AB Cardox Sys Isolated W/No One in Room.Caused by Personnel Error.Operator Instructed on Proper Procedures for Exiting Carbon Dioxide Protected Areas
Event date:
Report date:
3151983030R03 - NRC Website

text

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