ML20010H305
| ML20010H305 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 09/16/1981 |
| From: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Jackie Jones CAROLINA POWER & LIGHT CO. |
| Shared Package | |
| ML20010H306 | List: |
| References | |
| NUDOCS 8109240323 | |
| Download: ML20010H305 (2) | |
See also: IR 05000324/1981013
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Carolina Power anti Light Company
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ATTN: Mr. J. A. Jones, Senior Executive
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Vice President end Chief
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Gentlemen:
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50-324/81-13 and h 2 h
Subject:
Report Nos.
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This refers to your letter of August 24, 1981, infoming us of steps you have
taken to correct the violation concerning activities under NRC Operating Licenst
No. DPR-71 brought to your attention in our letter of July 24, 1981. We have
reevaluated our position in light of your response and find that no additional
infora tion was provided to change our finding.
Our position is based on the containment integrated leak rate test being an
important test to verify overall containment integrity and being conducted
Therefore, it is essential that
infrequently i.e. only three tests in ten years.
the test be performed correctly using the methods specified iri 10 CFR 50,
Appendix J and it is clearly your responsibility to insure that the procedure
addresses all requirements of Appendix J, regardless of the extent of NRC
Failure to properly perform this test has the
participar.f on in the test.
potential to permit reactor operation for an extended period without the requirei
On this basis, the violation was determined to be
containment integrity.
Your letter refers to internal NRC correspondence providing additional inter-
That letter of October 25, 1977, from Mr. V. Stello Jr.
pretation of Appendix J.
(NRR) to Mr. K. V. Seyfrit (01E), reiterates and seeks to clarify the require-
It is our
ments of Appendix J, bat does not change or extend the requirements.
understanding that the issue of a clarifying revision to Appendix J is imminent.
.
Additionally, we believe that you failed to recognize that Appendix J, paragraph
III.A.(d) specifies that certain systems shall be vented and drained during the
ILRT to simulate post-accident conditions. As described in the subject report,
Valve alignment during
your procedure failed to address venting and draining.
the test must also simulate post-accident conditions following an automatic
containment isolation. Your procedure contained valve lineups improper for this
purpose.
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8109240323 810916
PDR ADOCK 05000324
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SEP 161981
Caroli
Power and Light Company
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It is also our understanding that you Intend to revise your ILRT procedure to
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neet the requirements of Append 3x J, prior to the next 'lRT at Brunswick. This
corrective action appears adequate and W require no additional response from you
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at this time. We will examine your corrective actions and plans during sub-
sequent inspections.
We appreciate your cooperation with us.
Sincerely,
/s/
James P. O'Reilly
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Director
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C. R. Dietz, Plant Mir,ager
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NRC Resident Inspector
Document Management Branch
State of North Carolina
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