LER-1981-043, /03L-0:on 810825,drywell 3-RM-90-256 Continuous Air Monitor Iodine Channel Failed Downscale.Caused by Condensation Plugging Unit Due to Loss of Sample Line Heat Trace from Loose Connection on Thermostat.Trace Repaired |
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| 2961981043R03 - NRC Website |
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NRC FOfp1366 U. S. NUCLEAR REGULA10RY COMMIS$ ION T777) y,'
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[ o l 2 l [During normal steady state operation, the drvwell 3-RM-90-256 continuous air monitor l
lo l3 j l(CAM) iodine channel failed downscale at 1800 on 8/25/81. (T.S. 3.6.C.2)
There was l
Io la i [no danger to the health or safety of the public. There.ere no redundant systems l
[ o l t, l land no previous similar events.
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40 43 42 43 44 47 CAUSE DESCHiPTION AND CORRECTIVE ACilONS h I i l o l l The thermostat on the heat trace of the sample line had a loose connection. With-l
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liI,ilservice at 0510 on 8/27/81. This is considered a random event and no further l
[ i I.t i lrecurrence control is required.
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- ". ritit ion e,f Occu rrence-During normal steady state operation, the drywell 3-101-90-2 >6 cont (nuous air monitor (CMf) iodine channel failed downscale at 1800 on 8/25/81.
( :. m.. !it io a : l'r ior h) Ci arrence Unit 1 in refueling outage.
Unit 2. 76%.
Unit 3 at 93%.
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The thermostat on the heat trace of the sample line had a loose connectton.
Without heat trace, condensation collected and plugged the unit.
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i, There was no danger to the health or safety of the public, no release of activity, no damage to the plant or equipment, and no resulting significant chain of events.
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!ive Action - Water was purged f rom sample line and unit, sample line heat trace was repaired, and the model M1-331BF continuous air monitor was returned to service at 0510 on 8/21/81. During period of inoperability sampling program was initiated. This is considered a random event and no further recurrence control is required.
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| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. 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