05000296/LER-1981-043-03, /03L-0:on 810825,drywell 3-RM-90-256 Continuous Air Monitor Iodine Channel Failed Downscale.Caused by Condensation Plugging Unit Due to Loss of Sample Line Heat Trace from Loose Connection on Thermostat.Trace Repaired

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/03L-0:on 810825,drywell 3-RM-90-256 Continuous Air Monitor Iodine Channel Failed Downscale.Caused by Condensation Plugging Unit Due to Loss of Sample Line Heat Trace from Loose Connection on Thermostat.Trace Repaired
ML20010H279
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 09/18/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010H270 List:
References
LER-81-043-03L-01, LER-81-43-3L-1, NUDOCS 8109240294
Download: ML20010H279 (2)


LER-1981-043, /03L-0:on 810825,drywell 3-RM-90-256 Continuous Air Monitor Iodine Channel Failed Downscale.Caused by Condensation Plugging Unit Due to Loss of Sample Line Heat Trace from Loose Connection on Thermostat.Trace Repaired
Event date:
Report date:
2961981043R03 - NRC Website

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[ o l 2 l [During normal steady state operation, the drvwell 3-RM-90-256 continuous air monitor l

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". ritit ion e,f Occu rrence-During normal steady state operation, the drywell 3-101-90-2 >6 cont (nuous air monitor (CMf) iodine channel failed downscale at 1800 on 8/25/81.

( :. m.. !it io a : l'r ior h) Ci arrence Unit 1 in refueling outage.

Unit 2. 76%.

Unit 3 at 93%.

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The thermostat on the heat trace of the sample line had a loose connectton.

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i, There was no danger to the health or safety of the public, no release of activity, no damage to the plant or equipment, and no resulting significant chain of events.

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!ive Action - Water was purged f rom sample line and unit, sample line heat trace was repaired, and the model M1-331BF continuous air monitor was returned to service at 0510 on 8/21/81. During period of inoperability sampling program was initiated. This is considered a random event and no further recurrence control is required.

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