ML20010G134

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Monthly Operating Rept for Aug 1981
ML20010G134
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 09/01/1981
From: Nicholson W
PORTLAND GENERAL ELECTRIC CO.
To:
Shared Package
ML20010G131 List:
References
NUDOCS 8109150371
Download: ML20010G134 (5)


Text

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e OPERATING DATA REPORT DOCKET NO. 50-344 DATE 9/1/81 COMPLETED BY W.O.

Nicholson TELEPHONE sna/ssA 1713 Ext. 293 DrERATING STATUS Troian Nucienr P1 nnt-Notes

1. Unit Name:

Correction to July 1981 Report August 1981

. 2. Reporting Period:

34I1 Yr-to-date Forced Outage

3. Licensed Thermal Power'(MWt):

1216 Rate = 7.8

4. Nameplate Rating (Gross MWe):

'T '" s 1110

5. Design Electrical Rating (Net MWe):

Cuinulative Forced Outage 1122

6. Maximum Dependable Capacity (Gross MWe):

Rate = 24.0 1080

7. Maximum Dependsbie Capacity (Net MWe):
8. If Changes Occur in Capacity' Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

'None None

' 9. Power Level To Which Restricted. If Any (Net MWe):

NA

10. Reasons For Restrictions,if Any:

' This Month Yr.-to-Date Cumulative 74&

sA11 41R71 II. Hours In Reporting Period 739.5 3801.8 26563.1

12. Nutuber Of Hours Reactor Was Critical 0

0 2171.8

13. Reactor Reserve Shutdown Hours 716.2 1Aas n 95A,A s
14. Hours Generator On-Line 0

0 1sog 7

15. Unit Reserve Shutdown Hours 2383041 11658396 80225078
16. Gross Thermal Energy Generated (MWH) 773690 1gnt7?n oA1773na
17. Gross Electrical Energy Genersted (MWH) 711010 1 son?75 94607014
18. Net Electrical Energy Generated (MWH) 99.0 62.5

' 58'. 5

19. Unit Service Factor 99.0 69.5 67 :n
20. Unit Availability Factor 01 1 s7 n s9 9
21. Unit Capacity Factor (Using MDC Net) 87 1 9A s Ao o
  • 22. Unit Capacity Factor (Using DER Net) 1.0 6.s 91.s
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date. sad Durstion of Each1:

s None.

NA

25. If Shut Down At End Of Report Period. Estimated Date of Startup.
26. Units In Ted Status (Prior to Commercial Operation):

Forecast Achieved W

"A INITIAL CRITICALITY NA NA INITIAL ELECTRICITY NA NA COMMERCIAL OPERATION 8109150371 sto9ap M'

DR ADOCK 05000344

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-344 UNIT Trojan 9/1/81 DATE COMPLETED 11Y W. O. Nicholson 503/556-3713 TELEPHONE

. Ext. 293 MONTH August 1981 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe. Net) g 846 g7 1026*

g 852 18 1045 1056 3

851 g9 1061 4

878 20 5

1046 21 924 1019

' 981 6

22 1053 7

975 33 8

870 24 1053 9

700 25 1052 1058 10 652

g 1059 11 1029 27 1049 1057 12 3

1062 13 1051 29 1048 g4 30 1060 1056 3g gg 16 1052 l

l INSTRUCTIONS On this format. list the average daily unit powu levelin MWe. Net for each day in the reporting inonth. Compute to the nearest whole megswatt.

l (9/77) 1 n

__ __, g& h

50-344 DOCKET NO.

UNI 1.iHUTDOWNS AND POWER REDUC 110NS UNIT N AME Troian DATE 9/1/81 REPORT MONT11 August 1981 COMPLETED BY W. O. Nicholson TELEPflONE 503/556-3713 Ext. 293 I

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Licensee Eg i

Cause & Corrective H[

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Event g'g 1

Action to I

No.

Dwe yU aE r2 j if, g

.Repori*

've u Prevent Recurrence 6

81-13 810809 F

4.5 A

3 NA IIF PUMPXX The Reactor tripped from a Turbine trip when vacuum was lost due to trip of

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west circulating water pump. The pump tripped on low lube oil pressure. The pressure setpoint was found 2.5 psig i

high 'and was recalibrateil.

l 81-14 810810 F

3.3 G

3 NA HF PUMPXX The Reactor tripped from a Turbine trip

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l when vacuum was lost.due to a trip of the west circulating water pump. The, pump tripped as a result of troubic-shooting that wa's in p,rogress.

I 2

3 4-F: Forced Reason:

Method:

Exhibit G -Instructions S: Scheduled A Equipment Falture(Explain) 1-Manual for Preparation of Data B. Mali.tenance of Test 2 Manual Scram.

Entry Sheets for Licensee 1

C Refueling J-Automatic Sc.am.

Event ReporI(LER) File (NUREG-D Regulatory Restriction 4 01her(Explain) 0161)

E-Operator Training & Ucense Exu.dnation F-Administrative 5

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G Operational Error (Explain)

Exhibit 1 - Same Source (9/77)

(1 Other (Explain)

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DOCKETT NO:

50-344 DATE:

9/1/81 COMPLETED BY:

W. O. Nicholson TELEPHONE:

503/556-3713 Ext. 293 SUtOfARY OF OPERATING EXPERIENCE OPERATION:

The plant began the montn operating at approximately 80% power at the request of the load dispatcher.

Full power operation was achieved on August 4, 1981.

On August 9, 1981, a circulating water pump trip resulted in a Turbine trip /

l Reactor trip. The unit was back on-line within five hours. On August 10, 1981,

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an identical plant trip occurred when the same circulating water pump tripped while croubleshooting-The unit was back on-line ir three hours.

Power was reduced to approximatery 64% on August 9).,

1931, to replacc the coupling end bearing on the notth main feedwater pamp turbine. The work was completed and power eased co 100% on August 22, 1981.

For the remainder of the month, the plant operated at or near full power.

Occasional small power reductions due to high condenser back pressure were required on seven days during the month due to hot weather.

The Reactor Coolant System gross gamma activity increased from about 5 uC/ml to about 10 pC/ml in the first half of August.

Since this time, RCS activity has remained essentially constant.

Radiochemistry analysis shoue suspected fue2 failure in 8 to 12 rods in the twice burned fuel region.

MAJOR SAFETY RELATED MAINTENANCE:

The work was completed on structural modification of the Control and Auxiliary Building walls to improve seismic integrity.

The work was completed on the revision of the Auxfliary Feedwater turbine steam admission valves from AC motor-operated to air-operated.

Fire hydrant #4 was relocated and tested satisfactorily.

The work continued on the Reactor Vessel Level Indicating System outside of Containment.

The work was completed on the Containment Water Level Monitoring System and tested satisfactorily.

MISCELLANEOUS MAINTENANCE:

Annual preventativa maintenance was comp) i on the east emergency dieael generator.

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SUMMARY

OF OPERATING EXPERIENCE (Cont.)

f LICENSE CHANGES:

Amendment 65 - Revises the program for periodic inspection of the Control Building connection bolts.

Amendment 66 - Makes administrative changas related to off-site and on-site functional organizational charts, minimum shift crew composition, correction j

of a typographical error, membership of.the off-site review committee, and i

clarifies responsibilities of the on-site review committee.

Amendment 67 - Deletes licensa conditions related to interim operation of the facility and to the Control Building modification program. Updates the design features section of the Technical Specifications to describe the modified structure.

i MI'SCELLANEOUS :

'The work is continuing on the Technical Support Center.

i.

The electric Auxi' ury Feedwater Pump discharge was cross-connected with the discharge of both tho turbine driven and diesel driven Auxiliary Feedwater 2

Pumps.

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