LER-1981-060, /03L-0:on 810808,instrument Technician Misaligned Switch During Solid State Protection Testing,Resulting in Train B Safety Injection.Caused by Failure to Follow Written Procedures.Personnel Instructed to Adhere to Procedures |
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U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
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DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
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/ At 1640 on August 8, 1981, an instrument technician misaligned a switch during
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/ Unit 2 solid state protection testing causing a train B safety injection. The SI/
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER LH/ (18) [G/ (19) /Z/ (20) /Z/ (21) /0/0/0/0/ (22) [Y/ (23) [N/ (24) g/ (25) /Z/9/9/9/ (26)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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/ Failure to follow written procedures resulted in a switch misalignment. The
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8109110215 81096d~ " '")cDARER W. R. CARTWRIGHT PHONE (703) 894-5151 gDRADOCK 05000339 PDP
Virginia Electric and Power Company North Anna Power Station, Unit #2 Attachment: Page 1 of 3-Docket No. 50-339 Report No. LER 81-060/03L-0
Description of Event
On August 8, 1981, with Unit 2 in Hot Standby, during performance of train B reactor protection and ESF logic periodic test (2-PT-36.1),
the B train reactor trip breaker tripped. A procedure step initiated the *. rip by removing a low pressurizer pressure reactor. trip block and turb:. trip reactor trip block (P-7 reactor trip interlock).
Since the RCS p ussure (1500 psig) was below the low pressurizer pressure reactor trip setpoint (1870 psig) and the turbine was tripped, the.
B train reactor trip breaker trip was normal and should have been expected. The procedure did not warn the instrument technicians performing the test to expect the event described above when performing the test during shutdown conditions. Since the same instrument technicians had performed the same test on an operating unit previously and not observed the same event, they issued an emergency maintenance request and began investigating the event in accordance with an instrument maintenance procedure (IMP-C-SSP-04).
l While placing the train B solid state protection system (SSPS) in test pursuant to the instrament maintenance procedure, a SSPS output relay " Mode Selector" switch was returned to the operate position. This action allowed an existing low pressurizer pressure i
train B SI signal to actuate train B ECCS equipment at 1640 on August 8, 1981. Normally the low pressurizer ' pressure SI signal is blocked in Hot Standby if the RCS pressure is below 2000 psig; however, when the l
SSPS output relay " Mode Selector" switch is placed in the test position, I
for testing or maintenance, the low pressurizer pressure signal is removed from logic input causing an automatic drop of the low pressure i
SI block. Normally blocks are re-established by returning the SSPS output relay switch to the operate position and turning the manual block switches in the control room to the block position while inhibiting inputs to the SSPS train being tested. During performance of the maintenance procedure, the SSPS train B output relay " Mode Selector" switch was returned to the operate position without inhibiting SSPS train B inputs or re-establishing the SI low pressure block.
When the train B SI occurred, the reactor was shutdown with two shutdown banks withdrawn. Reactor trip breakers A and BYB (both train A operated) were closed; therefore, a reactor trip did net
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occur. The Shift Supervisor immediately ordered a manual reactor trip. Normally an automatic reactor trip would have occurred because train A and train B breakers are normally in series. One train of protection can be bypassed only for short. periods of time for sur-veillance testing pursuant to T.S. requirements. Maintenance testing as described above with one train bypassed required entry into the Action Statement of T.S. 3.3.1.1.
All train B emergency safety equipment responded as designed.
After determining that SI had-been caused by an instrument technician's error and was not required, SI flow to the RCS was secured at 1642.
RCS pressure and temperature were not significantly effected by the SI.
The safety injection event described above is reportable pur-suar.L to T.S. 6.9.1.9.c.
This report is also intended to meet the additional requirements of T.S. 6.9.2 and T.S. 3.5.2.h which require a report within 90 days describing the circumstances of the actuation-i_,-.-.--__..-.--
Attachment: Page 2 of 3 and the total accumulated cycles to date. This is the second ECCS actuation reportable pursuant to T.S. 6.9.2 and T.S. 3.5.2.b.
Removal of one train of protection for maintenance testing with the reactor trip system breakers in the closed position and the control rod drive system capable of rod withdrawal lead to oreration in a degraded mode. The Action statement of the LCO (T.S. 3.3.1.1) was met.
The maintenance testing as described above is reportable pursuant to T.S. 6.9.1.9.b.
The safety injection caused the Borca Injection Tank (BIT) boron concentration to fall below the concentration specified in T.S. 3.5.4.1.
The control room bottled air system actuated and dropped below the pressure specified in T.S. 3.7.7.1.
The refueling water storage tank (RWST) level dropped below the level specified in T.S. 3.5.5.
The BIT, control room bottled air system and RWST performed as designed.
After the Train B SI was reset, a failure of SI output relay K611 to unlatch prevented auxiliary feedwater pumps 2-FW-P-2 and 2-FW-P-3B from being secured. When this ocurred operation secured 2-FW-P-3B locally and isolated the discharge of 2-FW-P-2.
When the SI reset switches were tried a second time, relay K611 unlatched.
Probable Consequences of Occup ance The SI system with the exception of the SI reset problem described above performed as designed. An actual accident con-dition did not exist; therefore, the SI actuation was not required.
This event caused a thermal cycle stress load to be placed on the safety injection nozzles. Total cycles (two including this event) are well below design values. The action statements of applicabla LCO's wer2 met.
The public health and safety were not affected.
Cause of Event
Failure to follow procedure, failure to adhere to procedure precautions, and human error resulted in a switch misalignment.
The misaligned switch initiated a train B SI.
Immediate Corrective Action
The Shift Supervisor ordered the reactor trip breakers tripped.
The cause of the SI was determined. Verification that the SI was not required was made. The SI was secured.
Plant conditions and equipment were returned to normal..The BIT boron concentration was restored as required by the action statement of LCO (T.S. 3.5.4.1).
The control room bottled air system pressure was restored as re-quired by action statement of th2 LCO (T.S. 3.7.7.1).
The level of_the RWST was restored as required by the action statement of the LCO (T.S. 3.5.5).
The instrument technicians involved were instructed to closely adhere to procedures. Train B SSPS testing was completed satisfactorily and SSPS train B returned to servica.
Attachment: Page 3 of 3 Scheduled Corrective Action Us.it 1 and 2 reactor protection and ESF logic periodic tests 1-PT-36.1 and 2-PT-36.1 are being changed. Notes are being added to warn instrument technicians that when the test is performed during shutdown conditions,-the reactor trip breakers for the train under test will trip when placing the SSPS in the test mode. The procedures already contain precautions which if followed will prevent occurrence of the SI event.
SI output relay K611 will be tested and replaced.if necessary during the ne::t outage of sufficient duration.
Actions Taken to Prevent Recurrence Instrument technicians involved were instructed to adhere to procedures. Procedures are being changed as described in the scheduled corrective actions.
Westinghouse was notified of SI output relay unlatch.ng problems in November of 1980. Actions to prevent recurrenca will be taken when a satisfactory modification or design change is developed.
Generic Implications The failure of SI relay K611 to relatch has generic implications.
SI relay K611 was among several SI output relays which have unlatching failure histories (see LER 80-092/032-0). The latching mechanism is a Westinghouse ARLA type 4993D05606 and the relay is a Westinghouse type AR 440A relay.
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| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | | | 05000338/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003-03, /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | | | 05000338/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000338/LER-1981-004-03, /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | | | 05000339/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000339/LER-1981-004-03, /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | | | 05000338/LER-1981-005-03, /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | | | 05000338/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005-03, /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | | | 05000338/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000338/LER-1981-006-03, /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | | | 05000339/LER-1981-006-03, /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | | | 05000338/LER-1981-007-99, Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | | | 05000339/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000339/LER-1981-007-03, /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | | | 05000338/LER-1981-007, Forwards Updated LER 81-007/99X-1 | Forwards Updated LER 81-007/99X-1 | | | 05000339/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000338/LER-1981-008-03, /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | | | 05000338/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000339/LER-1981-008-03, /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | | | 05000339/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000339/LER-1981-009-03, /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | | | 05000338/LER-1981-009-03, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | | | 05000338/LER-1981-009, Forwards Updated LER 81-009/03X-1 | Forwards Updated LER 81-009/03X-1 | | | 05000338/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000338/LER-1981-010-03, /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | | | 05000339/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000339/LER-1981-010-03, /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | | | 05000338/LER-1981-011-03, /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | | | 05000338/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000339/LER-1981-011-03, /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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