05000327/LER-1981-089-03, /03L-0:on 810719,operator Observed Rod Position Indication for Shutdown Rods G13 & B12 Indicated Full Insertion Although Rods Were Withdrawn.No Dropped Rod Alarm Received.Caused by Power Supply Failure Due to Short

From kanterella
(Redirected from ML20010C559)
Jump to navigation Jump to search
/03L-0:on 810719,operator Observed Rod Position Indication for Shutdown Rods G13 & B12 Indicated Full Insertion Although Rods Were Withdrawn.No Dropped Rod Alarm Received.Caused by Power Supply Failure Due to Short
ML20010C559
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 08/12/1981
From: Harding M, Wilkey A
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010C557 List:
References
LER-81-089-03L, LER-81-89-3L, NUDOCS 8108200189
Download: ML20010C559 (2)


LER-1981-089, /03L-0:on 810719,operator Observed Rod Position Indication for Shutdown Rods G13 & B12 Indicated Full Insertion Although Rods Were Withdrawn.No Dropped Rod Alarm Received.Caused by Power Supply Failure Due to Short
Event date:
Report date:
3271981089R03 - NRC Website

text

~

(7 J t.

LICENSEE EVENT REPORT

,c.

coNTRot. stoCx: l l

l l

l l

l@

(PLEASE PR NT OR TYPE alt REQUIRED INFG4MATION)

~

3 6

@ l T l N l S l N l P'l 1 l@l0 l0 l-l O! O! 0 l 0 l 0 l - 10 l 0 l@l 4 l1 l1 l1 l1 l@l l

l@

i 8 9 LICENs(E coot 14

,15 LICENSE NUMBER 25 26

_ LICENSE TYPE 40 57 car w CON'T l0l l

,"7,,y l L l@l 0 l 5 10 l 0 10 l3 l2 l7 Ml 0 l 7 l 1 l 9 l 8 l 1 @[,g,{_9 j.1.1. 2 I 8 l 1 l@

I, S

60 68 oOCKETNUM01H 68 69 EVENT oATE 34 75 F,LPORT OAT E 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES O'o o.

i l-i2l l At 1016(c) on 7/21/81 with Unit 1 in Mode 3 (544 F & 2235 psig), the'Un' t Operator I observed that rod positi6n in'dication for shutdown rods G13 and B12 indicated fully o a lt i4l l inserted although the rods had been fully withdrawn. The operator verified the absence,

~

[olsl l of a dropped rod aiarm, then tripped the shutdown banks to comply with the action lo is ] l statement of LCO 3.1.3.3..

There'wati no effect on public health or safety. No previous, lol2] I occurrences.

l-

[TT31 I I

  • EoEo"
  • ^ "o'r' -susCoSt sue $o's sENs Co Cou oNENTCoos

['oTs"l l R lB l@ y@ W@ l.Il Nl Sl T l R l-U l@ lp l@ 'y g 7

8 9

to 13 12 13 18 19 20 sEOUE NTI AL OCCunhENCE-At* ORT REvtsfoN g gf ag EVENT YE AR R EPonT No.

4aDE TYPE No.

O,a(gg i 81 11 L _.I I o 1819 I l-1 Iol3I l LJ l--J

~lo I

~

_ 21 22 23 24 26 27 28 29 30

. 31 J2 TAK t A T o't o PLANT MET Hours 22 s8 8T O Fon [US.

sUPPLIE

  • MAN ACTURER Wgl34Zl@

lZ [@

l0l@

l 0 l0 l0 lu l U@

W@

[j@

lW l1 l2 l0 l JJ JS 36 31 40 41 42 43 44 4p CAUSE DESCRIPTION AND CORRECTIVE ACTIONS IiloIl Durine maintenance on the rod position indication system, a +13VDC-to-grourd short re g

~

i i l sulted in the failure of the main and auxiliary power supplies. The system was ice ! rc{

li 121 l declared inoperable until the power supplies were restored. Adjustments to a module fi l 3I l were also made to prevent recurrence.

11 iIl s

si so

's*rliiI[

oinEn sTAfus h biSCSNN h

sPowtR oiscoveny otsCRiPTioN lTT~l d@ l 0 l 0 l 0 l@l NA l

W @ l Operator Observation j

40TiviTY Co' Teuf 80 AMoVNT of ACTiv1TY @ l LOCATION oF AntASE @

RELEA%Eo oF nELFW Q l Z l @ l Z lgl l

NA l

NA 7

8 9 10 11 44 45 So PERSONNEL EXPOSURES NUMBER TYPt oEsCRIPfloN l i l 71 l 0 l 0 l 0 l@l Z l@l NA l

,t Aso~Ni L,~,Un'i.s oesCmeTioN@

Novet R It 18Il0l0l0l@l NA l

11 12

.o Lois of oR oAMAGE To FACILITY TV't otsCRipfioN lll9'l W @l NA l

PuntiETv 8108200189 810812

@ tssuto@otsCRiPTioN@

NRC ME W PDR ADOCK 05000327 W

l NA S

PDR l

lllllllll1lll 8

a e to es as

.Name of PrenRrer: A. M. Wilkey/M.R. Harding

. Phone. (61 % 842-R'll7 4

.e

r enn~ ~ee V.llity Auth;rity Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION SQRO-50-327/81089 At 1016 CDT on 7/21/81 with Unit 1 in Mode 3 (544 F & 2235 psig), the Unit Operator observed that rod position indication for shutdown rods G13 and B13 indicated that they were fully inserted although the rods had been fully withdrawn. After verifying that no dropped rod alarm had been received, the operator tripped the shutdown banks to comply with the action statement of LCO 3.1.3.3.

During maintenance on a signal conditioning module in the system, an extender board had been positioned at an angle which caused the +13VDC supply to short to ground. This resulted in the loss of regulation on the +26VDC main supply as well as the loss of the t13VDC alternate supply, When the indicators fell to zero due to the associated operational ampli-fiers being supplied by the +13VDC, the fault was diagnosed and the system was declared inoperable and the power supply fuses were pulled to prevent further damage to the equipment.

Subsequent investiga+ 'on determined that an alignment spacer normally installed in one pin of the module connector had been pulled out when the module had been removed. In addition, the module's side guides were also discovered to be loose. These two factors contribu'.ed to the electtical short which caused the event.

The signal conditioning module's side guides were tightened to prevent a recurrence of the short, the main and auxiliary power supplies were replaced, and the rod position indication system was declared operable at 1838 CDI.