LER-1981-009, /03L-0:on 810708,while Attempting Start of Cooling Tower Pump 122,undervoltage Relay Operation Opened Breaker CT 11-1,closed Bus Tie CTBT-112 & Caused Trip of Bus CT-12. Caused by Improperly Set Undervoltage Relay Setpoint |
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e v NRC PORM 306 U. L. NUCLE AR C EGWLATORY COMMISSION 17 771 LICENSEE EVENT REPORT CONTROL BLOCK: l l
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8 tio 61 DOCI(ET NUf48En 68 69 EVENT DATE 14 75 REPORT OATE 80 EVENT DESCRIPTION AND PROBAflLE CONSEQUENCES h O a l During normal operation, an attempted start ot No. 122 Cooling Tower l
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Safeguards buses lef t l 10.]61 l with one source of offsite power for abour l's minntns.
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I August 7, 1981 Attachment NORTilERN STATES POWER COMPANY PRAIRIE ISLAND NUCLEAR GENERATING PLANT LER 81-009 Supplemental Report pait One Operation With One Of fsite Source of Power Detailed Description of Event 1.
Cooling tower pump 122 tripped. Later found to be due to high vibration reading on malfunctioning instrument channel.
2.
Operators attempted to restart 122 cooling tcwer pump.
3.
Cooling tower bus CT11 un<lervultage due to motor starting load.
Relay 27/CT11 drops out tripping open breaker CT11-1 and closing bustic CTBT-112.
4.
Cooling tower bus CT12 undervoltage occurs due to transfer of bus CT11 loads and continued starting of 122 cooling tower pump bus. Bus doss not trip due to undervoltage on both buses.
(27/CT11 and 27/CT12 both droped out).
5.
Cooling tower buses (still tied together through bustie) begin to recover from undervoltage.
Although volage is the same on both buses, relay 27/CT11 resets (picks up) first.
Since relay 27/CT12 is still dropped out, breaker CT12-7 trips open leaving the cooling tower buses (CT11 and CT12) tied together and without a source.
6.
Safeguards buses 16 and 26 sense the loss of source and initiate their voltcge restoration schemes.
Both diesel generators start and bus tie breakers 16-8 and 26-8 cloc' providing sources for the safeguards buses 16 and 26 from the siternate offsite source.
7.
Operators restore cocling tower buses to normal configuration and restart 123 and 124 cooling tower pummps.
8.
121 and 12 cooling tower pumps are restarted. Bus CT11 transfer is prevented by opening trip switch for undervcitage relay.
Designation of Appareat Cause of the Occurrence The undervoltage relay, a Westingl ouse type SV relay, was found with an incorrect set point.
The SV type alay is an overvoltage relay on which we use the dropout contact.
The setpoint card stated a pickup voltage of 110 V and a dropout voltage of 90% of pickup (99v). When the relay was calibrated (2/81) the pickup was set at 110V. The dropout is not adjustable separately. Due to bus trans fer problems this relay was recbecked (5/81) and the pickup was found to be correct.
In both cases the actual dropout voltage was not checked.
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On 7/9/81 the relay was rechecked and the dropout voltage was measured.
The actual setting turned out to be: pickup 110V, dropout 10SV or 98%. The pickup voltage was set at 99V.
This relay should not have tripped the second source b.caker.
This was dite to a slight difference in the pickup voltage for the two coils.
J is 3
difference is unavoidable in calibration of the relay and is unitportant as long as this relay is prever.ted from tripping the second source breaker,
Corrective Action
The cooling sources were restored to the safeguards buses and the undervoltage relay was recalibrated. Following this recalibration 122 Cooling Tower Pump was stopped and restarted to verify that the relay was properly calibrated and would function as designed.
If a fault condition occurred which caused an undervoltage on CT11 bus and was not cleared quickly the potential exists for this logic to trip both cooling tower source breakers.
The cooling tower transfer scheme will be revised to prevent this.
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| 05000282/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000282/LER-1981-001-03, /03L-0:on 810112,while Performing Mod Work,Workman Accidentally Bumped Overspeed Trip Mechanism of Auxiliary Feedwater Pump,Tripping Valve & Making Pump Inoperable. Caused by Personnel Error.Valve Operator Reset | /03L-0:on 810112,while Performing Mod Work,Workman Accidentally Bumped Overspeed Trip Mechanism of Auxiliary Feedwater Pump,Tripping Valve & Making Pump Inoperable. Caused by Personnel Error.Valve Operator Reset | | | 05000306/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | | | 05000306/LER-1981-002-01, /01T-0:on 810301,during Eddy Current Exam of Steam Generator Tubes,Tubes Found Degraded & Defective.Caused by Corrosion &/Or Fretting.Defective Tubes Plugged | /01T-0:on 810301,during Eddy Current Exam of Steam Generator Tubes,Tubes Found Degraded & Defective.Caused by Corrosion &/Or Fretting.Defective Tubes Plugged | | | 05000282/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000282/LER-1981-003-03, /03L-0:on 810316,during Surveillance Test,Steam Exclusion Damper Actuation Setpoint Exceeded Limit.Caused by Foxboro Model 63U-CC-OHDR-F 6 Bistable Drift.Instrument Recalibr & Tested Satisfactorily | /03L-0:on 810316,during Surveillance Test,Steam Exclusion Damper Actuation Setpoint Exceeded Limit.Caused by Foxboro Model 63U-CC-OHDR-F 6 Bistable Drift.Instrument Recalibr & Tested Satisfactorily | | | 05000306/LER-1981-004-03, /03L-0:on 810406,during testing,turbine-driven Auxiliary Feedwater Pump 22 Failed to Come Up to Rated Speed.Caused by Low Governor Setting.Governor Adjusted to Proper Speed | /03L-0:on 810406,during testing,turbine-driven Auxiliary Feedwater Pump 22 Failed to Come Up to Rated Speed.Caused by Low Governor Setting.Governor Adjusted to Proper Speed | | | 05000306/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000306/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000306/LER-1981-005-03, /03L-0:on 810423,containment Vacuum Breakers Test Sp 2130 Was Discovered to Not Have Been Performed.Caused by Personnel Oversight.Preheatup Surveillance Test Scheduling Will Be Changed | /03L-0:on 810423,containment Vacuum Breakers Test Sp 2130 Was Discovered to Not Have Been Performed.Caused by Personnel Oversight.Preheatup Surveillance Test Scheduling Will Be Changed | | | 05000306/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000306/LER-1981-006-03, /03L-0:on 810507,charging Pump 121 Drive Unit Failed.Caused by Bearing Failure in Varidrive Unit.Damaged Parts Replaced | /03L-0:on 810507,charging Pump 121 Drive Unit Failed.Caused by Bearing Failure in Varidrive Unit.Damaged Parts Replaced | | | 05000282/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000282/LER-1981-007-03, /03L-0:on 810622,both Doors in One Shield Bldg Airlock Found Open & Not Under Administrative Control.Caused by Const Personnel Opening Doors W/O Notifying Control Room. Training Program to Be Expanded to Emphasize Door Specs | /03L-0:on 810622,both Doors in One Shield Bldg Airlock Found Open & Not Under Administrative Control.Caused by Const Personnel Opening Doors W/O Notifying Control Room. Training Program to Be Expanded to Emphasize Door Specs | | | 05000306/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000306/LER-1981-008-01, /01T-0:on 810611,shaft Vibration on Reactor Coolant Pump 21 & Seal 1 Leakoff Flow Increased Beyond Normal Range.Pump Disassembled.On 810706,circumferential Crack Discovered.Cause Not Determined | /01T-0:on 810611,shaft Vibration on Reactor Coolant Pump 21 & Seal 1 Leakoff Flow Increased Beyond Normal Range.Pump Disassembled.On 810706,circumferential Crack Discovered.Cause Not Determined | | | 05000282/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000282/LER-1981-009-03, /03L-0:on 810708,while Attempting Start of Cooling Tower Pump 122,undervoltage Relay Operation Opened Breaker CT 11-1,closed Bus Tie CTBT-112 & Caused Trip of Bus CT-12. Caused by Improperly Set Undervoltage Relay Setpoint | /03L-0:on 810708,while Attempting Start of Cooling Tower Pump 122,undervoltage Relay Operation Opened Breaker CT 11-1,closed Bus Tie CTBT-112 & Caused Trip of Bus CT-12. Caused by Improperly Set Undervoltage Relay Setpoint | | | 05000306/LER-1981-010-03, /03L-0:on 810807,rod Position Indication Channel K7 Found Drifted Low & Declared Inoperable.Cause Undetermined But Probably in Reactor Vessel Head.Repairs Will Be Made at Shutdown | /03L-0:on 810807,rod Position Indication Channel K7 Found Drifted Low & Declared Inoperable.Cause Undetermined But Probably in Reactor Vessel Head.Repairs Will Be Made at Shutdown | | | 05000306/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000282/LER-1981-011-01, /01T-0:on 810812,D2 Diesel Generator Tripped & Locked Out During Operability Test.Caused by Generator Operating in Unfamiliar Mode & Var & Watt Meters Being Confused by Operator | /01T-0:on 810812,D2 Diesel Generator Tripped & Locked Out During Operability Test.Caused by Generator Operating in Unfamiliar Mode & Var & Watt Meters Being Confused by Operator | | | 05000282/LER-1981-011, Forwards LER 81-011/01T-0 | Forwards LER 81-011/01T-0 | | | 05000282/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000282/LER-1981-012-03, /03L-0:on 810909,during Surveillance Test,One Low Pressurizer Pressure Reactor Trip Bistable Failed to Trip. Caused by Failure of Foxboro Model 63U-AC-OBHA-F Single Low Alarm Unit.Unit Replaced | /03L-0:on 810909,during Surveillance Test,One Low Pressurizer Pressure Reactor Trip Bistable Failed to Trip. Caused by Failure of Foxboro Model 63U-AC-OBHA-F Single Low Alarm Unit.Unit Replaced | | | 05000282/LER-1981-013-03, /03L-0:on 810912,during Coastdown Operation,Minor Xenon Oscillation Caused Flux Difference to Go Slightly Outside Target Band.Caused by Personnel Error | /03L-0:on 810912,during Coastdown Operation,Minor Xenon Oscillation Caused Flux Difference to Go Slightly Outside Target Band.Caused by Personnel Error | | | 05000282/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000282/LER-1981-015-03, /03L-0:on 810920,one Steam Generator Safety Valve Failed to Lift at Set Pressure During Refueling Tests.Cause Unknown.Valve to Be Hot Tested Before Reactor Taken to Power | /03L-0:on 810920,one Steam Generator Safety Valve Failed to Lift at Set Pressure During Refueling Tests.Cause Unknown.Valve to Be Hot Tested Before Reactor Taken to Power | | | 05000282/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000306/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000306/LER-1981-016-03, /03L-0:on 810925,diesel Cooling Water Pump Indicator Light Revealed Loss of Power to Pump.Probably Caused by Personnel Error in Not Adequately Reattaching Lifted Wire.Wire Reattached | /03L-0:on 810925,diesel Cooling Water Pump Indicator Light Revealed Loss of Power to Pump.Probably Caused by Personnel Error in Not Adequately Reattaching Lifted Wire.Wire Reattached | | | 05000306/LER-1981-017-03, /03L-0:on 810925,one Steam Pressure Safeguards Actuation Logic Trip Setpoint Was Found to Trip Out of Specs.Caused by Zero Shift in Foxboro Duplex Alarm Unit. Bistable Replaced | /03L-0:on 810925,one Steam Pressure Safeguards Actuation Logic Trip Setpoint Was Found to Trip Out of Specs.Caused by Zero Shift in Foxboro Duplex Alarm Unit. Bistable Replaced | | | 05000282/LER-1981-018, Forwards LER 81-018/01T-0 | Forwards LER 81-018/01T-0 | | | 05000282/LER-1981-018-01, /01T-0:on 810928,during Eddy Current Testing of Steam Generators at Refueling,Tube Degeneration Observed. Caused by Corrosion &/Or Fretting.Defective Tubes Plugged | /01T-0:on 810928,during Eddy Current Testing of Steam Generators at Refueling,Tube Degeneration Observed. Caused by Corrosion &/Or Fretting.Defective Tubes Plugged | | | 05000282/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000282/LER-1981-019-03, /03L-0:on 810927,w/122 Fire Pump Out of Svc,Daily Operability Test of 121 Pump Was Done on Schedule.Caused by Personnel Error on Turnover Sheet.Personnel Counseled | /03L-0:on 810927,w/122 Fire Pump Out of Svc,Daily Operability Test of 121 Pump Was Done on Schedule.Caused by Personnel Error on Turnover Sheet.Personnel Counseled | | | 05000282/LER-1981-020, Forwards LER 81-020/01T-0 | Forwards LER 81-020/01T-0 | | | 05000282/LER-1981-020-01, /01T-0:on 811011,Westinghouse Nbfd Relays in Reactor Protection Sys for Units 1 & 2 Found to Have Failed Relay Coils.Caused by Failure of Solder Joint Pigtail Connection Coil to Lead Wire | /01T-0:on 811011,Westinghouse Nbfd Relays in Reactor Protection Sys for Units 1 & 2 Found to Have Failed Relay Coils.Caused by Failure of Solder Joint Pigtail Connection Coil to Lead Wire | | | 05000282/LER-1981-022-03, /03L-0:on 811029,during Startup Operations, Pressure Transmitter Observed Reading Lower than Redundant Channels Used for High Pressure Reactor Trip Function.Caused by Zero Shift Made During Previous Recalibr | /03L-0:on 811029,during Startup Operations, Pressure Transmitter Observed Reading Lower than Redundant Channels Used for High Pressure Reactor Trip Function.Caused by Zero Shift Made During Previous Recalibr | | | 05000282/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000282/LER-1981-023-03, /03L-0:on 810921,during Surveillance Test,One Cooling Water Header Isolation Valve Did Not Close Fully. Caused by Wet Motor Leads in Junction Box.Wiring Renewed | /03L-0:on 810921,during Surveillance Test,One Cooling Water Header Isolation Valve Did Not Close Fully. Caused by Wet Motor Leads in Junction Box.Wiring Renewed | | | 05000282/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000282/LER-1981-024-03, /03L-0:on 811014,status Light Found Off & Breaker for Boric Acid Heat Tracing Switchrack Tripped.Caused by Personnel Failure to Respond to Trouble Alarm.Tripped Breaker Replaced | /03L-0:on 811014,status Light Found Off & Breaker for Boric Acid Heat Tracing Switchrack Tripped.Caused by Personnel Failure to Respond to Trouble Alarm.Tripped Breaker Replaced | | | 05000282/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000306/LER-1981-025-01, /01T-0:on 811029,during Test,Containment Purge Supply Penetration Leaked in Excess of Test Equipment Capacity.Probably Caused by Deformed Seating Matl,Small Dirt Accumulations on Valve Seats or Bolt Movement | /01T-0:on 811029,during Test,Containment Purge Supply Penetration Leaked in Excess of Test Equipment Capacity.Probably Caused by Deformed Seating Matl,Small Dirt Accumulations on Valve Seats or Bolt Movement | | | 05000306/LER-1981-025, Forwards LER 81-025/01T-0 | Forwards LER 81-025/01T-0 | | | 05000282/LER-1981-026-03, /03L-0:on 811105,during Surveillance Test,Found Loss of Voltage Relays 27R/B15 & 27S/B15 & Degraded Voltage Relay 27A1/B26 Outside Allowable Tech Spec Limit.Cause Unknown.Relays Recalibr | /03L-0:on 811105,during Surveillance Test,Found Loss of Voltage Relays 27R/B15 & 27S/B15 & Degraded Voltage Relay 27A1/B26 Outside Allowable Tech Spec Limit.Cause Unknown.Relays Recalibr | | | 05000282/LER-1981-026, Forwards LER 81-026/03L-0 | Forwards LER 81-026/03L-0 | | | 05000282/LER-1981-027-03, /03L-0:on 811116,discovered That Pre,Absolute & Charcoal Filter Test Not Done on 11 Shield Bldg Ventilation Sys Replacement on 811112.Caused by Procedural Inadequacies & Poor Communications | /03L-0:on 811116,discovered That Pre,Absolute & Charcoal Filter Test Not Done on 11 Shield Bldg Ventilation Sys Replacement on 811112.Caused by Procedural Inadequacies & Poor Communications | | | 05000282/LER-1981-027, Forwards LER 81-027/03L-0 | Forwards LER 81-027/03L-0 | | | 05000306/LER-1981-028-03, /03L-0:on 811118 & 1218,bistables 2-PC-431 G & I Found Out of Tolerance.Caused by Defective Potentiometer on 811118.On 811218,leads Were Tightened,Correcting Problem | /03L-0:on 811118 & 1218,bistables 2-PC-431 G & I Found Out of Tolerance.Caused by Defective Potentiometer on 811118.On 811218,leads Were Tightened,Correcting Problem | |
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