LER-1981-097, Forwards LER 81-097/03L-0.Detailed Event Analysis Encl |
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7 OFFICIM f'OPY DUKE Powsn COMPANY Powen 13ctLotwo 422 SocTu Cucacu Srazzr, CzuntoTTE, N. C. 28242' wi w A14 O. PA R M E R. J R.
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July 8, 1981 273-4ces Mr. James P. O'Reilly, Director
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U. S. Nuclear Regulatory Commission C'
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McGuire Nuclear Station Unit 1
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Docket No. 50-369 4\\ S '
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Dear Mr. O'Reilly:
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Please find attached Reportable Occurrence Report R0-369/81-97.
This report concerns Technical Specification 3.3.3.l; "As a minimum, the fire detection instrumentar. ion for each fire detection zone shown in Table 3.3-11 shall be operable." This inciG at was considered to be of no significance with respect to th health and safety of the public.
Ve, truly your,
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William O. Parker, PBN/pw Attachment cc:
Director Mr. Till Lavallae Office of Management and Program Analysis Nuclear Safety Analysis Center U. S. Nuclear Regulatory Commission P. O. Box 10412 l
Washington, D. C.
20555 Palo Alto, CA 94303 Ms. M. J. Graham Res*ient Inspector - NRC l
McGuice Nuclear Station s
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McGUIRE NUCLEAR STATION INCIDENT REPORT Report Number:
81-97 Report Date: July 8, 1981 Occurrence Date: June 12, 1981 Facility:
McGuire Nuclear Station, Unit 1, Cornelius, N.C.
Identification of Occurrence:
Several fire zones were declared inoperable due to an insufficient quantity of installed detection instruments.
Condition Prior to Occurrence: Mode 5, Cold Shutdown Description of Occurrence:
On June 12, 1981 it was discovered that the quantity of fire detection equipment installed in five (5) fire zones did not comply with the minimum requirement listed in Table 3.3-11 of McGuire Technical Specifications.
These discrepancies were brought to the attention of the Shift Supervisor who immediately declared the fire protection instrumentation in the affected fire sones inoperable.
This constituted a reportable incident pursuant to Technical Speci-fication 3.3.3.7 and required instituting an hourly fire watch as stipulated by the appropriate action statement.
Apparent Cause:
The discrepancy in one fire zone (#106) was the result of a typographical error in Table 3.3-11.
The other four fire zones (around each of the four Reactor Coolant pumps) were analyzed and the quantity installed was determined to be sufficient.
Analysis of Occurrence: An operations engineer discovered that the quantity of fire detection equipment installed in Fi.re Zone #106 and each of the Reactor Coolant pump zones did not agree with the minimum number required by the Technical Specifications. A check of the blue prints confirmed that the instruments that were installed were in accordance with the number and type stipulated by the drawings.
Design Encineerlag was contacted and asked to determine if additional fire pro-tection equipment was needed.
After being notified of the discrepancies, the Shift Supervisor on duty declared the affected fire zones inoperable until the differences could be resolved. Hourly fire patrols were established as required.
It was discovered that the inconsistency existing in fire ione #106 between the Tectaical Specification Table 3.3-11 and the equipment installed was the result of a typographical error in the Technical Specifications.
i Fire Zones #147, 148, 149 and 150 (each of the four reactor coolant pump areas) were re-evaluated by the Design Engineering group and it wcs decided that the equipment installed met the requirements of the National Fire Protection Association, NFPA-72E-1974.
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^'T Repcrt Number 81-97 Page 2 Steam Production submitted letters to the NRC requesting permission to make ap-propriate changes in Table 3.3-11 to reflect the correct number of fire pro-tection equipment necessary in each area.
Fire Zone #106 was declared operable on June 15, 1981; the remaining fire zones were declared operable on June 19, 1981.
Corrective Action
The initial response to this incident was to establish hourly fire patrols in the affected areas. A re-examination of the installed fire pro-tection equipment revealed a typographical error in Tabla 3.3-11 affecting fire zone #106.
It :ias ascertain-d that the equipment in Zones 147, 148, 149 and 150 was adequate.
Letters were sent to the NRC requesting the approval of the existing equipment and the subsequent changes to the Technical Specifications.
The Technical Specification changes were approved on June 19, 1981.
Safety Analysis
The fire detection equipment is designed to give prompt detection and location of fires in their early stages.
Thus, the pot-sntial for damage to safety-ralated equipment would be minimized.
It was detert,ined that the type and quantity of fire protection equipment installed met the standards of the NFPA-72E-1974; hence the safe operation of the plant and the health and safety of the public were not affected by this incident.
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| 05000369/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000369/LER-1981-001-03, /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. Caused by Const in Area.Fire Watches & Patrols Established | /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. Caused by Const in Area.Fire Watches & Patrols Established | | | 05000369/LER-1981-002-01, /01T-0:on 810130,during Test,Vent Valve VX-41 & Containment Isolation Valve XV-40 Found Open to Atmosphere, in Violation of Tech Spec 4.9.4.1.Caused by Lack of Valve Checklist & Lack of Periodic Test.Valves Closed | /01T-0:on 810130,during Test,Vent Valve VX-41 & Containment Isolation Valve XV-40 Found Open to Atmosphere, in Violation of Tech Spec 4.9.4.1.Caused by Lack of Valve Checklist & Lack of Periodic Test.Valves Closed | | | 05000369/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | | | 05000369/LER-1981-003-03, /03L-0:on 810129,conventional Waste Plant Discharge Flow Monitor Found Inoperable.Caused by Inaccurate Flow Readings Due to Inability of Instrument to Measure Continuous Discharge Flow.New Equipment Ordered | /03L-0:on 810129,conventional Waste Plant Discharge Flow Monitor Found Inoperable.Caused by Inaccurate Flow Readings Due to Inability of Instrument to Measure Continuous Discharge Flow.New Equipment Ordered | | | 05000369/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000369/LER-1981-004-03, /03L-0:on 810129-0212,various Firestops & Fire Doors Found Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established | /03L-0:on 810129-0212,various Firestops & Fire Doors Found Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established | | | 05000369/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000369/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000369/LER-1981-005-03, /03L-0:on 810202,power Supply to Both Excore Range Monitors Was Interrupted.Caused by Maint Personnel Cutting Off Power to Investigate Steam Generator Status Lights & lo-lo Level Alarms.Personnel Instructed | /03L-0:on 810202,power Supply to Both Excore Range Monitors Was Interrupted.Caused by Maint Personnel Cutting Off Power to Investigate Steam Generator Status Lights & lo-lo Level Alarms.Personnel Instructed | | | 05000369/LER-1981-006-03, /03L-0:on 810202,leaking Seal Discovered on RHR Pump.Caused by Improperly Loaded Spring Which Holds Seal Faces Together.Seal Replaced | /03L-0:on 810202,leaking Seal Discovered on RHR Pump.Caused by Improperly Loaded Spring Which Holds Seal Faces Together.Seal Replaced | | | 05000369/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000369/LER-1981-007-03, /03L-0:on 810203,RHR Sys Train a Was Declared Inoperable.Caused by Draining Essential Header to Repair Leaking Valves in Nuclear Svc Water Sys.Valves Repaired & Train a Returned to Svc | /03L-0:on 810203,RHR Sys Train a Was Declared Inoperable.Caused by Draining Essential Header to Repair Leaking Valves in Nuclear Svc Water Sys.Valves Repaired & Train a Returned to Svc | | | 05000369/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000369/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000369/LER-1981-008-03, /03L-0:on 810203,control Area Ventilation Sys Train a Declared Inoperable.Caused by Draining Essential Header to Repair Leaking Valves in Nuclear Svc Water Sys. Valves Repaired & Train a Returned to Svc | /03L-0:on 810203,control Area Ventilation Sys Train a Declared Inoperable.Caused by Draining Essential Header to Repair Leaking Valves in Nuclear Svc Water Sys. Valves Repaired & Train a Returned to Svc | | | 05000369/LER-1981-009-03, /03L-0:on 810205,flow to Reactor Coolant Loops Was Momentarily Lost.Caused by Failure of Throttle Valve to Close Due to Loosening of Nut Holding Linkage to Valve Stem. Linkage Repositioned & Nut Tightened | /03L-0:on 810205,flow to Reactor Coolant Loops Was Momentarily Lost.Caused by Failure of Throttle Valve to Close Due to Loosening of Nut Holding Linkage to Valve Stem. Linkage Repositioned & Nut Tightened | | | 05000369/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000369/LER-1981-010-03, /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | | | 05000369/LER-1981-011-03, /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | | | 05000369/LER-1981-011, Forwards LER 81-011/03T-0 | Forwards LER 81-011/03T-0 | | | 05000369/LER-1981-012-03, /03T-0:on 801211,isolation Valve NV-250 Found Not Verified Closed Under Administrative Control Per Tech Spec. Caused by Lack of Signoff Step in Daily Surveillance Items. Procedure Change Incorporated | /03T-0:on 801211,isolation Valve NV-250 Found Not Verified Closed Under Administrative Control Per Tech Spec. Caused by Lack of Signoff Step in Daily Surveillance Items. Procedure Change Incorporated | | | 05000369/LER-1981-012, Forwards LER 81-012/03T-0 | Forwards LER 81-012/03T-0 | | | 05000369/LER-1981-013-03, /03L-0:on 810212,radiation Detectors EMF 33,35,36, 37,38,39 & 40 Were Declared Inoperable Due to Loss of Sample Flows.Caused by Individual Nonrelated Failures of Each Emf. Repairs Performed & EMFs Declared Operable | /03L-0:on 810212,radiation Detectors EMF 33,35,36, 37,38,39 & 40 Were Declared Inoperable Due to Loss of Sample Flows.Caused by Individual Nonrelated Failures of Each Emf. Repairs Performed & EMFs Declared Operable | | | 05000369/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000369/LER-1981-014-03, /03L-0:on 810212,while in Mode 6,control Room Received High Groundwater Alarm.Caused by Localized Temporary High Groundwater Level.Proper Surveillance Conducted & Alarm Was Cleared within 2 Days | /03L-0:on 810212,while in Mode 6,control Room Received High Groundwater Alarm.Caused by Localized Temporary High Groundwater Level.Proper Surveillance Conducted & Alarm Was Cleared within 2 Days | | | 05000369/LER-1981-015-03, /03L-0:on 810213,various Firestops & Fire Doors Rendered Inoperable for Periods Exceeding 1-h from 810213-27.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established as Required | /03L-0:on 810213,various Firestops & Fire Doors Rendered Inoperable for Periods Exceeding 1-h from 810213-27.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrols Established as Required | | | 05000369/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000369/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000369/LER-1981-016-03, /03L-0:on 810216,several Firestops Inadvertently Left Open W/O Fire Watches Being Posted.Caused by Omission of Stops from Maint List of Those Requiring Seals.Stops Sealed.Seals Will Be Verified Every 18 Months | /03L-0:on 810216,several Firestops Inadvertently Left Open W/O Fire Watches Being Posted.Caused by Omission of Stops from Maint List of Those Requiring Seals.Stops Sealed.Seals Will Be Verified Every 18 Months | | | 05000369/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-018-03, /03L-0:on 810219,annunciator Alarm Indicated Loss of Sample Flow on Radiation Monitor 1-EMF-33.Monitor Vacuum Pump Internally Damaged Due to Water Inside Pump.Pump Vanes & Bearings Replaced & Water Removed | /03L-0:on 810219,annunciator Alarm Indicated Loss of Sample Flow on Radiation Monitor 1-EMF-33.Monitor Vacuum Pump Internally Damaged Due to Water Inside Pump.Pump Vanes & Bearings Replaced & Water Removed | | | 05000369/LER-1981-019-01, /01T-0:on 810306,during ESF Testing,Loss of Ac Power Was Experienced on Half of Station Security Sys.Caused by Blown Security Sys Power Inverter Fuse.Security Procedures Changed to Indicate Info Concerning Power Sys | /01T-0:on 810306,during ESF Testing,Loss of Ac Power Was Experienced on Half of Station Security Sys.Caused by Blown Security Sys Power Inverter Fuse.Security Procedures Changed to Indicate Info Concerning Power Sys | | | 05000369/LER-1981-019, Forwards LER 81-019/01T-0 | Forwards LER 81-019/01T-0 | | | 05000369/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-020-03, /03L-0:on 810219,spurious High Radiation Alarm & Loss of Flow Alarm Sounded in Control Room on EMF-49. Personnel Cleared Radiation Alarm But Overlooked Closed Valve,Causing Loss of Flow Alarm.Monitor Repaired | /03L-0:on 810219,spurious High Radiation Alarm & Loss of Flow Alarm Sounded in Control Room on EMF-49. Personnel Cleared Radiation Alarm But Overlooked Closed Valve,Causing Loss of Flow Alarm.Monitor Repaired | | | 05000369/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-021-03, /03L-0:on 810226,noble Gas Activity Monitor for Condenser Evacuation Sys EMF-33 Not Functioning.Caused by Excessive Amounts of Condensation in Sample Lines.Moisture Removed.Different Type of Moisture Separator to Be Used | /03L-0:on 810226,noble Gas Activity Monitor for Condenser Evacuation Sys EMF-33 Not Functioning.Caused by Excessive Amounts of Condensation in Sample Lines.Moisture Removed.Different Type of Moisture Separator to Be Used | | | 05000369/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000369/LER-1981-022-03, /03L-0:on 810301-16,various Portions of Fire Detection Sys Inoperable for Periods Exceeding 1-h.Caused by Const in Area.Fire Watches & Patrols Established as Required | /03L-0:on 810301-16,various Portions of Fire Detection Sys Inoperable for Periods Exceeding 1-h.Caused by Const in Area.Fire Watches & Patrols Established as Required | | | 05000369/LER-1981-023-03, /03L-0:on 810227-0313,various Firestops & Fire Doors Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrol Established as Required | /03L-0:on 810227-0313,various Firestops & Fire Doors Inoperable for Periods Exceeding 1-h.Caused by Const in & Through Areas Normally Closed Off.Fire Watches & Patrol Established as Required | | | 05000369/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000369/LER-1981-024, Forwards LER 81-024/01T-0 | Forwards LER 81-024/01T-0 | | | 05000369/LER-1981-024-01, /01T-0:on 810316,Unit 1 Wedge Plates Discovered to Be Smaller than Required Size.Cause Not Stated.Calculations Reviewed to Determine Acceptance.Corrective Action Deemed Necessary.Bar Along Length of Washer Plate Added | /01T-0:on 810316,Unit 1 Wedge Plates Discovered to Be Smaller than Required Size.Cause Not Stated.Calculations Reviewed to Determine Acceptance.Corrective Action Deemed Necessary.Bar Along Length of Washer Plate Added | | | 05000369/LER-1981-025-01, /01T-0:on 810319,no Seismic Bracing or Calculations Found for 12 Reactor Bldg safety-related Electrical Cable Tray Hanger Stds.Cause Not Stated.Seismic Calculations Performed on Affected Hangers | /01T-0:on 810319,no Seismic Bracing or Calculations Found for 12 Reactor Bldg safety-related Electrical Cable Tray Hanger Stds.Cause Not Stated.Seismic Calculations Performed on Affected Hangers | | | 05000369/LER-1981-025, Forwards LER 81-025/01T-0 | Forwards LER 81-025/01T-0 | | | 05000369/LER-1981-026-03, /03L-0:on 810305,EMF Sys Panel Alarm in Control Room Indicated Malfunction of EMF-43A.Alarm Could Not Be Cleared & Control Room Outside Air Intake Gaseous Activity Monitor Inoperable.Caused by Broken Bnc Jack | /03L-0:on 810305,EMF Sys Panel Alarm in Control Room Indicated Malfunction of EMF-43A.Alarm Could Not Be Cleared & Control Room Outside Air Intake Gaseous Activity Monitor Inoperable.Caused by Broken Bnc Jack | | | 05000369/LER-1981-026, Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | |
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