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LER-1981-036, Corrected LER 81-036/03L-0,changing Sequential Date of LER 81-033/03L-0.On 810528,sample of Emergency Diesel Generator Fuel Oil Storage Tanks Revealed Water in Tank 1-EE-TK-2A |
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IA routine sample of the EDG fuel oil storage tanks revealed water in tank 1-EE-TK-2A.
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The fuel oil transfer pumps were placed under administrative control and the water was ;
i is contrary to T.S. 3.16.A.5 and is reportable in accordance with ;
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is ics1 water from the above grouna storage tank and preventing its entry into the underground The water was drained via the transfer pump suction strainer drains.
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CORRECTED COPY-SEQUENTIAL #033 6-26-81 CHANGED TO #036 ATTACHMENT 1 (PAGE 10F 2)
SURRY POWER STATION, UNIT 2 DOCKET No:
50-281 REPORT NO:
81-03.603L-0 EVENT DATE: 05-28-81 TITLE OF THE EVENT: WATER IN TANK 1-EE-TK-2A 1.
DESCRIPTION OF THE EVENT:
On May 10,1981, fire water was used to leak test the reactor lower Laternals shield tank prior to installation. An open valve from the fire main to the-fire protection foam system allowed water to enter the above ground fuel oil storage tank, 1-HS-TK-1.
The tank was isolated and an estimated 4000 gallons of water drained. Samples were taken from the instrument connection, for 1-HS-TK-1, and found to be free of water. The outlet to the underground tanks were verified closed and as a precaution, the valves were tagged cicaed.
The samples that were taken from the instrument connection on 1-HS-TK-1 were not representative. Although the instrument connection on this tank appears to be the lowest connection, both outlets are, in fact, lower. The outlet to the underground tank being 2 inches lower and the outlet to the hose connection 4" lower. During the week (May 10-15), the above ground tank was sampled for water, from the instrument connection, each day before verifying that the under-ground tanks were full. During this time, water apparently entered the 'A' underground tank.
A week later, while filling a vehicle from the hose connection, wat'er was again discovered. Th'e tank was thea drained from the hose connection until all the water was removed.
At 0530 hrs. on May 28, 1981, a routine sample of the underground fuel oil l
tanks revealed water in tank 1-EE-TK-2A.
The fuel oil transfer pumps', asso-ciated with tank 2A, were placed under administrative control and samples taken from the suction strainers showed that. water had not reached the pumps, l
f However, additional draining from this point and the underground tank's mano-meter connection did produce water at both of these locations.
The wall tanks, located in each EDG room, were sampled and no water was found.
l Tne wall tanks were partially drained and then refilled; from the-underground tank 2A, several times. A small quantity of water was subsequently drained f
from the wall tanks.
I At 1525 hrs., samples o,f the wall tanks, the underground tank make up line, f
and the transfer pump suctions were all free of water. The transfer pumps were returned to automatic and the 2A underground' tank refilled.
Af ter the underground tank was filled,. additional water was drained from the manometer connection. To verify that the water level was below the transfer pump suction,' 45 gallons of fuel oil was drained from ' A' pump and 10 gallons from 'B'
& 'C' pumps. Sanples taken from each pump were free of water. How-ever, for the next three shif ts, water was drained from the manometer connection.
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This event is contrary to Tech. Spec. 3.16.A.5 and is reportable per Tech.
Spec. 6.6.2.b. (2).
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ATTACHliENT 1 (PAGE 2 0F 2)
SURRY POWER STATION, UNIT 2 DOCKET NO:
50-281 REPORT NO:
81-036/03L-0 EVENT DATE:
05-28-81 2.
PROBABLE CONSEQUENCES AND STATUS OF REDUlT:' ANT EQUIPMr23 The emergency diesel generators provide power to vital equipment in the event of a loss of normal power. The outlets of the fuel oil tanks are designed to allow for some accumulation of water. Between 5-10-81 and 5-28-81, the EDG's were operated intermittently for about 8 hrs. total without any problems. The redundant flow path from 2B underground tank was operable and free of water.
Therefore. the health and safety of the public were not affected.
3.
yAUSE:
The cause of this event has been deter dned to be inadequate procedures.
Specifically, the lack of guidance for the sampling of fuel oil tanks.
4.
L M IATE CORRECTIVE ACTION:
The fuel oil trcusfer pumps in the affected train were placed under adminis-trative control and the other train was verified free of. water.
5.
SUBSEQUENTJ ORRECTIVE ACTION:
The water was drained from the transfer pump suctions, the wall tank drains and the anometer connection for '2A' underground tank.
6.
ACTION TAKEN TO PREVENT RECURRENCE:
A sampling procedure will be developed and a sampling frequency established for the above ground tank.
I 7.
GENERIC IMPLICATIONS:
l None.
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| 05000280/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000280/LER-1981-001-01, /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | /01T-0:on 810225,w/unit Defueled for Steam Generator Replacement,Routine Testing Exam of Loop a Main Steam Piping Revealed Linear Indications.Caused by Corrosion Pitting.Subj Areas Will Be Repaired | | | 05000281/LER-1981-001-03, /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | /03L-0:on 810102,one Boric Acid Flow Path to Core Inoperable.Caused by Personnel Inadvertently Closing Valve 2-CH-226.Flow Path Restored & Personnel Reinstructed | | | 05000280/LER-1981-002-03, /03L-0:on 810122,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Shutdown & Defueled Conditions.Activity Levels Verified within Allowable Limits | /03L-0:on 810122,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Shutdown & Defueled Conditions.Activity Levels Verified within Allowable Limits | | | 05000281/LER-1981-002-03, /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced | /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced | | | 05000280/LER-1981-003-03, /03L-0:on 810129,radiation Alarm Setpoint for Component Cooling Sys Found Greater than Twice Background. 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Caused by Air Leakage Through Solenoid Valve.Solenoid & Air Motors Replaced | /03L-0:on 810204,air Motors for Preferred Start 2 of Emergency Diesel Generator 3 Found Engaged to Flywheel. Caused by Air Leakage Through Solenoid Valve.Solenoid & Air Motors Replaced | | | 05000280/LER-1981-006-03, /03L-0:on 810306,alarm Setpoint for Component Cooling Water Radiation Monitor RM-CC-106 Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset to Proper Setpoint & Returned to Svc | /03L-0:on 810306,alarm Setpoint for Component Cooling Water Radiation Monitor RM-CC-106 Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset to Proper Setpoint & Returned to Svc | | | 05000281/LER-1981-006-03, /03L-0:on 810114,at Full Power,C Safety Injection Accumulator Found to Have Boron Concentration of 1943 Ppm, 7 Ppm Below Required Limit.Caused by Leakage Through Check Valve 1-SI-144.Valve Isolated | /03L-0:on 810114,at Full Power,C Safety Injection Accumulator Found to Have Boron Concentration of 1943 Ppm, 7 Ppm Below Required Limit.Caused by Leakage Through Check Valve 1-SI-144.Valve Isolated | | | 05000280/LER-1981-007-03, W/Unit 1 Defueled & 2 at 100% Power,Power for Several Radiation Monitors Lost.Caused by Shorting of Test Lead to Ground Causing Supply Fuse to Blow.Fuse Replaced.Monitors Returned to Svc | W/Unit 1 Defueled & 2 at 100% Power,Power for Several Radiation Monitors Lost.Caused by Shorting of Test Lead to Ground Causing Supply Fuse to Blow.Fuse Replaced.Monitors Returned to Svc | | | 05000281/LER-1981-007-03, /03L-0:on 810114,at 100% power,PT-27 (Heat Tracing) Revealed Amp Readings for Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | /03L-0:on 810114,at 100% power,PT-27 (Heat Tracing) Revealed Amp Readings for Panels 8 & 9 Circuits Were Below Acceptance Criteria.Caused by Excessive Temps Breaking Down Insulation.Defective Heat Tracing Replaced | | | 05000281/LER-1981-008-03, /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | /03L-0:on 810206,output Amperage for RM-CC-106 Reduced in Nonconservative Direction.Caused by Failed Remote Indicator Module in Auxiliary Bldg.Module Isolated & RM-CC-106 Recalibr.Monitor Will Be Repaired | | | 05000280/LER-1981-008-03, /03L-0:on 810410,process Vent Radiation Monitor Found Inoperable.Caused by Broken Pump Drive Belt Due to Misalignment.Drive Belt Replaced & Radiation Monitor Operability Verified | /03L-0:on 810410,process Vent Radiation Monitor Found Inoperable.Caused by Broken Pump Drive Belt Due to Misalignment.Drive Belt Replaced & Radiation Monitor Operability Verified | | | 05000280/LER-1981-009-01, /01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made | /01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made | | | 05000281/LER-1981-009-03, /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 11 Circuit 4C.Caused by Short in Heat Tape.Defective Heat Tracing Replaced.Design Change Initiated | /03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 11 Circuit 4C.Caused by Short in Heat Tape.Defective Heat Tracing Replaced.Design Change Initiated | | | 05000280/LER-1981-010-03, /03L-0:on 810415,alarm Setpoints for RM-CC-105 & RM-CC-106 Found Greater than Tech Spec Limits on Several Occasions.Caused by Misinterpretation of Background & Insufficient Guidelines for Evaluation of Alarm Setpoint | /03L-0:on 810415,alarm Setpoints for RM-CC-105 & RM-CC-106 Found Greater than Tech Spec Limits on Several Occasions.Caused by Misinterpretation of Background & Insufficient Guidelines for Evaluation of Alarm Setpoint | | | 05000281/LER-1981-010-03, /03L-0:on 810209,svc Water pump,2-SW-P-10B, Developed Low Discharge Pressure.Caused by Eel Lodged in Impeller.Eel Removed & Pump Returned to Svc | /03L-0:on 810209,svc Water pump,2-SW-P-10B, Developed Low Discharge Pressure.Caused by Eel Lodged in Impeller.Eel Removed & Pump Returned to Svc | | | 05000281/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000280/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000281/LER-1981-011-03, /03L-0:on 810119,fire Watch Not Maintained While Fuel Oil Pumphouse Carbon Dioxide Sys Out of Svc for Design Change Mods.Caused by Personnel Leaving Post.Fire Watch re-established & Personnel Disciplined | /03L-0:on 810119,fire Watch Not Maintained While Fuel Oil Pumphouse Carbon Dioxide Sys Out of Svc for Design Change Mods.Caused by Personnel Leaving Post.Fire Watch re-established & Personnel Disciplined | | | 05000280/LER-1981-011-03, /03L-0:on 810426 & 27,process Vent Radiation Monitors Flooded Due to Introduction of Water Into Process Vent Sys.Caused by Failure of Primary Drain Tank Level Control Sys.Monitors Drained & Vacuum Pump Replaced | /03L-0:on 810426 & 27,process Vent Radiation Monitors Flooded Due to Introduction of Water Into Process Vent Sys.Caused by Failure of Primary Drain Tank Level Control Sys.Monitors Drained & Vacuum Pump Replaced | | | 05000281/LER-1981-012-03, /03L-0:on 810118,boric Acid Transfer Pump 1-CH-P-2D Failed.Caused by Bearing Failure Due to Oil Seal Failure.Pump Repaired | /03L-0:on 810118,boric Acid Transfer Pump 1-CH-P-2D Failed.Caused by Bearing Failure Due to Oil Seal Failure.Pump Repaired | | | 05000280/LER-1981-012-03, /03L-0:on 810506,seismic Instrumentation Found Not Calibr According to Tech Specs.Caused by Defective Procedures.Periodic Test Had Been Mislabeled as Calibr Procedure.Instrumentation Calibr Using Approved Procedure | /03L-0:on 810506,seismic Instrumentation Found Not Calibr According to Tech Specs.Caused by Defective Procedures.Periodic Test Had Been Mislabeled as Calibr Procedure.Instrumentation Calibr Using Approved Procedure | | | 05000281/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000281/LER-1981-013-03, /03L-0:on 810119,improperly Sealed Fire Barrier Penetration Discovered.Caused by Improper Matl Being Packed Into Penetration.Penetration Properly Sealed | /03L-0:on 810119,improperly Sealed Fire Barrier Penetration Discovered.Caused by Improper Matl Being Packed Into Penetration.Penetration Properly Sealed | | | 05000280/LER-1981-013-03, /03L-0:on 810527,radiation Monitor Recorder RR-100 Was Found Indicating Decade Lower than Corresponding Monitors.Caused by Dirty Contacts in Circuit Controlling Positioning of Printing Device.Contacts Cleaned | /03L-0:on 810527,radiation Monitor Recorder RR-100 Was Found Indicating Decade Lower than Corresponding Monitors.Caused by Dirty Contacts in Circuit Controlling Positioning of Printing Device.Contacts Cleaned | | | 05000281/LER-1981-014-03, /03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset | /03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset | | | 05000280/LER-1981-014-03, /03L-0:on 810523,auxiliary Bldg Filter Banks Were Found to Be Less Efficient than Required by Tech Spec.Caused by Formation of Void Areas Due to Settling of Charcoal in Filters.Charcoal Added | /03L-0:on 810523,auxiliary Bldg Filter Banks Were Found to Be Less Efficient than Required by Tech Spec.Caused by Formation of Void Areas Due to Settling of Charcoal in Filters.Charcoal Added | | | 05000280/LER-1981-015, Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | Forwards LER 81-015/03L-0,updated LER 81-035/03X-1 & Corrected LER 81-036/03L-0 | | | 05000280/LER-1981-015-03, /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | /03L-0:on 810603,spent Fuel Pit Overflowed Into New Fuel Handling Area & Outside to Storm Drain.Caused by Leaking Diaphragm Valve & Defeated High Level Alarm Annunciator.Valve Repaired | | | 05000281/LER-1981-015-03, /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor Pump Failed to Rotate.Caused by Failure of Pump Bearings.Pump Replaced | /03L-0:on 810315,PT-26.1 Revealed That Process Vent Radiation Monitor Pump Failed to Rotate.Caused by Failure of Pump Bearings.Pump Replaced | | | 05000281/LER-1981-016-03, /03L-0:on 810119,at 100% Power,Positive Pressure Greater than 0.05 Inches Water Could Not Be Maintained in Control Room.Caused by Deteriorated Seals on Door to Control Room Complex.Defective Doors Repaired | /03L-0:on 810119,at 100% Power,Positive Pressure Greater than 0.05 Inches Water Could Not Be Maintained in Control Room.Caused by Deteriorated Seals on Door to Control Room Complex.Defective Doors Repaired | | | 05000281/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000280/LER-1981-016-03, /03L-0:on 810615,primary Sys Chloride Concentration Exceeded Tech Specs.Apparently Caused by Personnel Working on Minor Repairs to Closure Stud Hole on Reactor Vessel Flange.All Sources of Makeup Water Checked | /03L-0:on 810615,primary Sys Chloride Concentration Exceeded Tech Specs.Apparently Caused by Personnel Working on Minor Repairs to Closure Stud Hole on Reactor Vessel Flange.All Sources of Makeup Water Checked | | | 05000281/LER-1981-017-03, /03L-0:on 810210,intermediate Range Channel N36 High Level Trip Setpoint Found in Excess of Tech Spec.Caused by Setpoint Drift.Setpoint Adjusted | /03L-0:on 810210,intermediate Range Channel N36 High Level Trip Setpoint Found in Excess of Tech Spec.Caused by Setpoint Drift.Setpoint Adjusted | | | 05000280/LER-1981-017-03, /03L-0:on 810702,discovered That No Fire Watch Had Been Posted for Two Unsealed Fire Barrier Penetrations in Cable Spreading Room Area.Caused by Const Personnel Error. Fire Watch Posted & Seal Installed | /03L-0:on 810702,discovered That No Fire Watch Had Been Posted for Two Unsealed Fire Barrier Penetrations in Cable Spreading Room Area.Caused by Const Personnel Error. Fire Watch Posted & Seal Installed | | | 05000280/LER-1981-018-03, Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | Ler 81-018/03L-0:on 810702,power Operated Relief Valves Lifted to Mitigate Overpressurization Transient.Caused by Unisolated Charging Flow Control Valve.Valve Isolated. RCS Pressure Reduced Below Setpoint | | | 05000281/LER-1981-018-03, /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 810318,amp Readings for Heat Tracing Panel 10,circuit 4A,were Below Acceptance Criteria Per PT-27.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | | 05000280/LER-1981-019-01, /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | /01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced | | | 05000281/LER-1981-019-03, /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | /03L-0:on 810218,amp Readings for Heat Tracing Panel 9,circuit 6A Were Low.Caused by Excessive Heat.Heat Tracing Replaced | | | 05000281/LER-1981-020-03, /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | /03L-0:on 810223,during Full power,RM-CC-106 Alert & High Alarm Lights Energized W/O Initiating Required Automatic Action.Caused by Failed Card in Alarm Circuit.Card Replaced & Tested | | | 05000280/LER-1981-020-03, Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | Ae Notified Util of Seven Masonry Block Wall Sections in Fuel Bldg Not Meeting IE Bulletin 80-11 Design Requirements.Cause Not Stated.Block Walls Will Be Replaced | | | 05000281/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000280/LER-1981-021-03, /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | /03L-0:on 810704,chemical Addition Tank Found to Contain 86% of Vol Required,Following Level Transmitter Recalibr.Caused by Use of Pure Water Instead of Sodium Hydroxide Solution in Original Calibr Procedure | | | 05000280/LER-1981-021, Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | Forwards LER 81-021/03L-0.W/o Encl LERs 81-022/03L-0 & 81-028/03L-0 | |
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