ML20009F501

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LER 81-013/01T-0:on 810630,backup Function of Isolating & Transfer Diodes in Instrumentation & Control Sys Disabled on All Channels on All Units.Caused by Misinterpretation of Tech Specs.Proposed Tech Spec Change Initiated
ML20009F501
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 07/14/1981
From: Jackie Jones
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F495 List:
References
LER-81-013-01T, LER-81-13-1T, NUDOCS 8107310244
Download: ML20009F501 (1)


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