05000269/LER-1981-013-01, /01T-0:on 810630,backup Function of Isolating & Transfer Diodes in Instrumentation & Control Sys Disabled on All Channels on All Units.Caused by Misinterpretation of Tech Specs.Proposed Tech Spec Change Initiated

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/01T-0:on 810630,backup Function of Isolating & Transfer Diodes in Instrumentation & Control Sys Disabled on All Channels on All Units.Caused by Misinterpretation of Tech Specs.Proposed Tech Spec Change Initiated
ML20009F501
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 07/14/1981
From: Jackie Jones
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F495 List:
References
LER-81-013-01T, LER-81-13-1T, NUDOCS 8107310244
Download: ML20009F501 (1)


LER-1981-013, /01T-0:on 810630,backup Function of Isolating & Transfer Diodes in Instrumentation & Control Sys Disabled on All Channels on All Units.Caused by Misinterpretation of Tech Specs.Proposed Tech Spec Change Initiated
Event date:
Report date:
2691981013R01 - NRC Website

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