LER-1981-050, /03L-0:on 810619 & 20,during RCS Cooldown to Cold Shutdown Conditions,Individual Rod Position Indication B Shutdown Bank Rod G-7 & J-9 Deviated from Group Demand Position.Caused by Instrument Drift |
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U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT
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OUR DOCKET NUMBER EVENT DATE REPORT DATE TVENT DESCRIPTION AND PROBABLE CONSEQUENCES (.10)
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/ On June 19 and 20, 1981, during RCS cooldown to cold shutdown conditions, the
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/ individual rod position indication for "B" shutdown bank rod G-7 and J-9,
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/ On each occasion, the reactor trip breakers were immediately opened in compliance /-
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/ with T.S. 3.1.3.3 and tne IRPI was recalibrated, consequently the health and
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/ safety of the general pubic were not affected. This event is reportable pursuant /
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/ to T.S. 6.9.1.9.b.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
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/E/ (13) /I/N/S/T/R/U/ (14)
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SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
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REPORT NUMBER
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED -FORM SUB. SUPPLIER MANUFACTURER
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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/ The cause'of this indicator disagreement was attributed to instrument drift. This/
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I.t both cases, the rod position channel was properly recalibrated /
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FACILITY METHOD OF STATUS
% POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION (32)
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OPERATOR OBSERVATION
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ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
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PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION (39)
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PERSONNEL INJURIES NUMBER DESCRIPTION (41)
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LOSS OF OR DAMAGE TO FACILITY (43)
TYPE
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PUBLICITY ISSUED DESCRIPTION (45)
NRC USE ONLY
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NAME OF PREPARER W. R. CARTWRIGHT PHONE (703) 894-5151 8107280537 810715 050003 gDRADOCK
Virginia Electric and Power Company North Anna Power Station, Unit 2
Attachment:
Page 1 of 1 Docket No. 50-339 Report No. LER 81-050/03L-0 i
Description of Event
on June 19, 1981, an RCS cooldown to cold shutdown conditions was in progress when the Control Room operator observed a greater than 12 step disagreement between he Individual Rod Position Indicator (IRPI) for rod G-7 in shutdown bank "B" and the group demand indication.
On June 20, a greater than 12 step disagreement was also observed on the IRPI for "B" shutdown bank rod J-9.
Probable Consequences of Occurrence Operability of the control rod position indication is required to determine rod position and thereby ensure compliance with the control rod misalignment and insertion limits.
Since neither control rod wa's misaligned and both position indications were properly restored, there was no effect on the safe operation of the plant. As a result, the health and safety of the general public were not affected.
Cause of Event
The cause of the dis.3reement in rod position indication was instru-ment drift.
This drift can be caused by changes in the temperature of the rod drive line., changes in the frequency of the excitation source, and by changes in secondary loadings.
Immediate Corrective Action
On both occasions, the reactor was immediately tripped as per T.S.
3.1.3.3 and the rod position indicator channel was satisfactorily recal-ibrated and returned to service.
Scheduled Corrective Action s
1 A long term investigation into the problems associated with the IRPI system is in progress.
No further corrective action is scheduled until an adequate design modification is developed and proven effective.
Actions Taken to Prevent Reccurrence i
No further actions are required at this time.
l Generic Implications Rod position indicator drift is a generic problem with the Westing-house analog rod position indication system. This system is used in North Anna Units 1 and 2.
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| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. 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Channel Recalibr | | | 05000339/LER-1981-006-03, /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | | | 05000338/LER-1981-007-99, Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | | | 05000339/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000339/LER-1981-007-03, /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. 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Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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