LER-1981-031, /03L-0:on 810624,during Normal Operations 3-A Reactor Recirculation Pump Tripped Due to 2A-K45A Relay Action.Caused by Resistance Temp Detector High Temp Trip. Unit Load Reduced.Ge Motor Generator Set & Restarted |
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| 2961981031R03 - NRC Website |
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o U. S. NUCLE AR REGULATORY COMMISSION NRC DORM 366 LICENSEE EVENT REPORT CONYROL BLOCK: l l
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jg le IS LICENSE NUMBER JS 26 LICENSE TYPE JO 67 GAT 58 H 9 LICENSEE COOF [oj,l
- 'goaf gl 0l 5l 0l 0l 0l 2l 9l 6 @l 0l 6l 2] 4l 8l 1 hl017 i2 Il 18 Il lh CON' T 68 69 EV ENT DATE 74 75 REPORT DATE 80 ho G8 DOCKET NUM8ER 1
a EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h the 3-A reactor recirculation pump tripped l
Jojzjl During normal operation at steady state, due to 2A-K45A relay action.
(See T.S. 3.6.F.1)
There was no danger to the health l
[o ;3 j l lol4ll or safety of the public. There were no redundant systems.
3-B pump was operable.
l BFRO-50-260/81009, 80018, 81023; 296/81028.
l j n I., j l Previous similar events:
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CAUSE
CODE CODE SUSCODE COMPONENT CODE SU8 CODE SUSCODE l_ C] Bl@ W@ W @ l M l C l T l 0 l R l X l@ lZ l@ ] @
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9 10 11 12 IJ 18 19 20 SEQUE NTI AL OCCUR R E NCE REPORT R EVISION LE ReRo EVENT YE AR REPORT NO.
CODE TYPE No.
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31 40 el 42 43 44 47 JJ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Unit load was reduced l
Iiio1l 2A-K45A relay action initiated by RTD high temperature trip.
The high temperature l and the G.E. variable speed M/G set and pump were restarted.
Ii ii l Alam annunciates at 110 degrees l trip setpoint was raised to 120 degrees centigrade.
gl l i l il ] cent igratte.
A special test will be implemented to investigate this problem.
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$sCONv DISCOVERY DESCRIPTION TTN7
, Power OTHER STATUS NA l
lAj@l Operator observed l
I l'-l l Elh l O ! 9 l 8 l@l Al.'rivi s v edelrEnr LOCATION OF RELEASE Of t.E A* E U OF del F Ar.&
AMOUNT OF ACTIVITY
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8107280290 810721 PDR ADOCK 05000296 Gene Holder PH ON E
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Form BF 17
" Tennessee Valley Auttiority 13 F 15. 2 Br..wns Ferry Nuclear Plant h/o1/81 I.F.!! Sl!PPl.10lliNTAI. INi/ollM ATIO 4 Tr. huiad S n cific ation in ceived 3.6.E.L...._ _ __.._
hiItO 50- 2.96_ /.81031 i
liep rted linalter Tc chnical Spr cification o.7.2.b(2)
- Date due N11C:.,7/2.4/81,_ _,
luetc.4 Occurrerm-6/24/81 l'itne of Occurrence _2008,, Unit,,,3,,,__,,_,,.,
Nicnjirie,at hqi an.!,In,periptyn.4 i b:currener 3-A reactor recirculation pump tripped due to 2A-K45A relay action.
4 t %nilitions l'rior to Uccurrence.
j Unit 1 in refueling outage Unit 2 at 1 LOO %
Unit 3 at 98%
m.
Action specifimi in the Technical Specification Surveillance Requirements met W"Lt?. 'D?pggh,le equinment. _ Describe.
Restored 3-A recirculation pump to service within 1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
1 l
l Appart of.Caus.c of ( b cut;tence The reactor recirculation motor generator set tripped due to 2A-K45A relay action initiated by RTD high temperature trip.
2 Analysis <# Oeno reni.
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There was no danger - to tha health or safety of the public, no release of activity, no damage to tl.e plant or equipment, and no resulting significant chain of events.
1 C rrective Action: A special test is being written and will be implemented
.to investigate this problem. Recurrence control will depend on results from these investigations. By 6/27/81, the trip setting for the drive motor high 1
j temperature and gen hi temp relays for each M/G set on all three units were.
raised to trip at 120 C.
Alarm annunciates at 110 C.
Failure.hata: BFRO-50-260/81009, 80018, 81023; 296/81028.
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| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. 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