05000334/LER-1981-055-03, /03L-0:on 810529,during Maint Surveillance Test, High Level Alarm on Safety Injection Accumulator 1C Was Discovered Above High Limit.Caused by Instrument Drift.Trip Voltage Adjusted

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/03L-0:on 810529,during Maint Surveillance Test, High Level Alarm on Safety Injection Accumulator 1C Was Discovered Above High Limit.Caused by Instrument Drift.Trip Voltage Adjusted
ML20009A531
Person / Time
Site: Beaver Valley
Issue date: 06/29/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009A523 List:
References
LER-81-055-03L, LER-81-55-3L, NUDOCS 8107130279
Download: ML20009A531 (2)


LER-1981-055, /03L-0:on 810529,during Maint Surveillance Test, High Level Alarm on Safety Injection Accumulator 1C Was Discovered Above High Limit.Caused by Instrument Drift.Trip Voltage Adjusted
Event date:
Report date:
3341981055R03 - NRC Website

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[o 121 l During power operation at 1038 hours0.012 days <br />0.288 hours <br />0.00172 weeks <br />3.94959e-4 months <br />, a maintenance surveillance test discovered i that the high level alarm on the 1C Safety Injection Accumulator drifted slightly l Ic lal I

' [ o l.i l l above high limit. This would have resulted in the adding of an additional volume 1

lo # s j l of water prior to receiving the high level alarm. Approximately 2 gallons of I

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I 1 o 17 l 1 public was not ieopardiOed bv this event.

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l1 10 l l The cause of this event has been attributed to Ner mone dri f t. The trin volencel was immediately adjusted to the correct value by 1041 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.961005e-4 months <br />.

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Attachment To LER 81-055/03L Beaver Valicy Power Station 1

Duquesne Light Company Docket No. 50-334

  • No further information is available or needed to satisfy the reporting requirement.

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